Event Notification Report for February 28, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/27/2003 - 02/28/2003 ** EVENT NUMBERS ** 39613 39615 39623 39624 39625 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39613 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 02/24/2003| |LICENSEE: SPECTRO ANALYTICAL INSTRUMENTS |NOTIFICATION TIME: 12:06[EST]| | CITY: MARBLE FALLS REGION: 4 |EVENT DATE: 02/13/2003| | COUNTY: STATE: TX |EVENT TIME: [CST]| |LICENSE#: L-02788-003 AGREEMENT: Y |LAST UPDATE DATE: 02/24/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID GRAVES R4 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM OGDEN | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LEAKING SEALED SOURCE | | | | The following information was obtained from the Texas Department of Health | | via facsimile: | | | | "During routine service of an ASOMA (SPECTRO) Model 200, Serial No 4390, a | | wipe test was performed on a 20 millicurie Am-241 source, Serial No 13730W. | | Contamination of 0.035 microcuries was detected on the wipe. The source is | | an AEA Technology (Amersham) Model AMC.D2 with a source product code | | AMCK2175. It is encapsulated in an X10/2 capsule. The source was removed | | and is being returned to the manufacturer for evaluation. All other | | interior components and exterior surfaces of the instrument were wipe tested | | and found to have no contamination above the Licensee's minimum detection | | limit of 360 picocuries. Agency was notified by telephone of the leaking | | source on February 13, 2003. A written report was sent to this Agency that | | same date. This incident was closed February 24, 2003. No violations have | | been cited. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39615 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 02/24/2003| |LICENSEE: SPECTRO ANALYTIC INSTRUMENTS |NOTIFICATION TIME: 16:46[EST]| | CITY: MARBLE FALLS REGION: 4 |EVENT DATE: 02/24/2003| | COUNTY: STATE: TX |EVENT TIME: 14:00[CST]| |LICENSE#: L-02788-003 AGREEMENT: Y |LAST UPDATE DATE: 02/24/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID GRAVES R4 | | |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM OGDEN | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LEAKING SEALED SOURCE | | | | The following information was obtained from the Texas Department of Health | | via facsimile: | | | | "Leaking source was discovered during routine servicing of an ASOMA Model | | 200 analytical instrument, Serial No 4668. The instrument contained a sealed | | Amersham 13 millicurie, Cm-244 source, Serial No 2695LM, Amersham Model No. | | CLCL. Last assay date was 08/15/95. Leakage detected was from a routine | | wipe test which resulted in 0.0077 microcuries of removable contamination. | | The source is being prepared for return to the manufacturer for evaluation | | and disposal. All other interior components and exterior surfaces of the | | instrument were wipe tested and found to have no contamination above the | | Licensee's minimum detection limit of 360 picocuries." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39623 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 02/27/2003| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 17:15[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 02/27/2003| +------------------------------------------------+EVENT TIME: 13:01[EST]| | NRC NOTIFIED BY: PETE SENA |LAST UPDATE DATE: 02/27/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 58 Power Operation |43 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC ACTUATION OF THE #2 EMERGENCY DIESEL GENERATOR | | | | "This provides notification of an automatic actuation of the No. 2 Emergency | | Diesel Generator (EDG) at Beaver Valley Power Station (BVPS) Unit No. 1 | | | | "On 2/27/2003 at 1301 hours, BVPS Unit No. 1 was at 58 % power following a | | startup from a recent forced outage. The 'B' Main Feedwater Pump (MFP) | | tripped on overcurrent shortly after it was started. Concurrent with the MFP | | trip, the breaker which feeds the non-safety related 'D' bus from the | | offsite power source also tripped, de-energizing the 'D' bus. [The 'D' bus | | supplies power to the 'B' MFP.] The loss of the 'D' bus caused the loss of | | power to the safety related Emergency 'DF' bus, which caused the No. 2 EDG | | to start and re-energize the Emergency 'DF' bus with all equipment properly | | loaded. | | | | "Control Room personnel entered Abnormal Operating Procedure 1.36.2, 'Loss | | of 4KV Emergency Bus.' Reactor Power was manually ramped back to 43 % power | | in response to this transient. Actions are being taken to re-energize the | | non-safety related 'D' bus from its offsite source. The EDG remains in | | operation with no abnormalities. The cause of the 'B' MFP trip is being | | investigated. | | | | "This condition is being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A) as | | an actuation of an emergency diesel generator which is part of the onsite | | emergency AC electrical power system. The NRC resident has been notified." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39624 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 02/27/2003| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 19:50[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 02/27/2003| +------------------------------------------------+EVENT TIME: 17:31[CST]| | NRC NOTIFIED BY: RANDY HASTINGS |LAST UPDATE DATE: 02/27/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |THOMAS KOZAK R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |92 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SHUTDOWN REQUIRED BY TECHNICAL SPECIFICATIONS | | | | "On 02/27/03 at 1731[CST] hours, Point Beach Unit 1 commenced an orderly | | reactor shutdown in response to TS [Technical Specifications] Action | | Statement 3.6.3.D.1, which requires the unit to be taken to Mode 3 in 6 | | hours when two containment isolation valves are inoperable for greater than | | 1 hour. Valves 1SC-953 and 1SC-966B, pressurizer liquid space sampling | | containment isolation valves, were declared inoperable when leakage was | | evident past the shut valves. At 1748 hours, the pressurizer liquid space | | penetration flow path was verified as being isolated by shutting manual | | valve 1SC-952. The shutdown was terminated at 1751[CST] hours. | | | | "Earlier in the afternoon, it had been reported to the Control Room that the | | reactor coolant primary sampling containment isolation valves (1SC-955 and | | 1SC-966C) were leaking through. The penetration flow path for these valves | | was isolated via shutting valve 1SC-954B. Further investigation revealed | | that leakage was still present. The leakage was isolated by shutting | | 1SC-952. | | | | "The 1D Pressurizer Heater Bank tripped during attempt to manually energize | | pressurizer heaters. Minimum required pressurizer heater capacity is | | maintained. Investigation is in progress." | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39625 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COLUMBIA GENERATING STATIREGION: 4 |NOTIFICATION DATE: 02/27/2003| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 23:37[EST]| | RXTYPE: [2] GE-5 |EVENT DATE: 02/27/2003| +------------------------------------------------+EVENT TIME: 19:45[PST]| | NRC NOTIFIED BY: CRAIG SLY |LAST UPDATE DATE: 02/27/2003| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID GRAVES R4 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |80 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT COMMENCED TECH SPEC REQUIRED SHUTDOWN DUE TO INOPERABLE EDG | | | | "This ENS notification is made to report initiation of a plant shutdown | | required by the Columbia Generating Station Technical Specifications (TS's) | | pursuant to 10CFR 50.72(b)(2)(i). This plant shutdown was initiated due to | | the inability to restore the Division I Emergency Diesel Generator (DG-1) to | | operable status prior to exceeding the expiration of the Completion Time of | | TS LCO 3.8.1, Condition B.4. Columbia Generating Station was granted | | enforcement discretion (NOED 03-4-001) from compliance with the completion | | time requirements of TS 3.8.1, Condition B.4, for an eleven-day period | | beginning on February 16, 2003 and ending February 27, 2003 at 9 p.m. (PST). | | The enforcement discretion was granted to allow the replacement of a | | degraded DG-1 generator bearing. Both generator bearings were replaced. | | However, during post maintenance tests to validate operability of DG-1, | | vibration levels for the new bearings showed evidence of an increasing | | trend. Based on this, DG-1 is currently considered inoperable. Even | | though the current vibration levels are very low, the plant has decided | | further testing and diagnosis is necessary to support a decision on DG-1 | | operability. Although the Completion Time of TS 3.8.1, Required Action B.4 | | expires at 9 p.m., plant shutdown commenced at approximately 7:45 p.m. | | (PST), on February 27, 2003." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021