Event Notification Report for February 6, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/05/2003 - 02/06/2003 ** EVENT NUMBERS ** 39550 39561 39562 39563 39564 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39550 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/31/2003| |LICENSEE: UNIVERSITY OF TEXAS AT AUSTIN |NOTIFICATION TIME: 14:00[EST]| | CITY: AUSTIN REGION: 4 |EVENT DATE: 01/30/2003| | COUNTY: STATE: TX |EVENT TIME: [CST]| |LICENSE#: L00485-000 AGREEMENT: Y |LAST UPDATE DATE: 01/31/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JONES R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN | | | HQ OPS OFFICER: YAMIR DIAZ | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TEXAS AGREEMENT STATE REPORT FOR LEAKING SOURCE | | | | "The University of Texas ordered a Sodium 22 (Na-22) positron source for | | research use. The Type A package arrived during the evening of January 30, | | 2003, and was unpackaged. During un-packaging it was noted that the Source | | was either leaking or contaminated. Attempts to decontaminate the source | | only resulted in higher reading. Leakage was measured at 30,000 DPM, | | therefore, over the 0.0005 uCi [microcurie] leakage limit. | | | | "The source arrived from the manufacturer: National Accelerator Center, | | Somerset West, South Africa. The report was made IAW 25 TAC 289.202 (bbb). | | A follow-up written report will follow by facsimile within 5 days. Chemical | | form of the source is solid sodium bicarbonate sealed in a titanium body. | | Source was leak tested due to the lack of a leak test certificate with the | | shipment. The inner packaging of the Type A container is also contaminated. | | No Model # or Serial # is readily apparent." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39561 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 02/05/2003| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 00:12[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/04/2003| +------------------------------------------------+EVENT TIME: 22:40[EST]| | NRC NOTIFIED BY: ART BREADY |LAST UPDATE DATE: 02/05/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF METEOROLOGICAL DATA AT SALEM AND HOPE CREEK STATIONS | | | | "THIS 8-HOUR NOTIFICATION IS BEING MADE TO REPORT THAT THE SALEM AND HOPE | | CREEK SITE LOST ALL METEOROLOGICAL DATA FOR WIND SPEED, DIRECTION AND | | TEMPERATURE AT 1440 ON 2/04/03. ALL THREE UNITS ARE OPERATING AT 100% POWER. | | NO ACTUATIONS HAVE TAKEN PLACE RELATED TO THIS EVENT. THE CAUSE OF THIS LOSS | | IS BEING INVESTIGATED. PROCEDURAL GUIDANCE IS AVAILABLE TO OBTAIN THE | | NECESSARY DATA FROM THE NATIONAL WEATHER SERVICE SHOULD THIS DATA BE | | NECESSARY." | | | | The licensee will notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39562 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 02/05/2003| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 12:00[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 02/05/2003| +------------------------------------------------+EVENT TIME: 08:45[EST]| | NRC NOTIFIED BY: CALVIN WARD |LAST UPDATE DATE: 02/05/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOEL MUNDY R2 | |10 CFR SECTION: |FRED BROWN NMSS | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION |NATIONAL RESP CTR EPA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTIFICATION TO STATE OF RADIOACTIVE MATERIAL FOUND IN SCRAPYARD | | | | "At 0845, Florida Power and Light Company (FPL) notified the Florida Bureau | | of Radiation Control of an item found at a scrap yard facility in Coral | | Springs, FL. The item was an Eberline model RD-A2A radiation detector, | | serial number 2555, with the label indicating a sealed source with 50 | | nanoCuries of Am-241 (exempt quantity). The detector was removed from the | | facility, surveys were performed by FPL personnel and no other radioactive | | material was found. An investigation is in progress to determine the origin | | of the material." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39563 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 02/05/2003| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 15:50[EST]| | RXTYPE: [2] GE-4 |EVENT DATE: 02/05/2003| +------------------------------------------------+EVENT TIME: 12:25[EST]| | NRC NOTIFIED BY: PATRICK FALLON |LAST UPDATE DATE: 02/05/2003| | HQ OPS OFFICER: YAMIR DIAZ +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KENNETH RIEMER R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION | | | | "On February 5, 2003 at 1225 hours, reports were made to the National Spill | | Response Center, the EPA Regional Response Center, the Michigan State Police | | Operations Center and the State of Michigan Dept of Environmental Quality | | concerning a leak (approximately 500 pounds) of ethylene glycol, which is | | used in the cooling tower de-icing system, to the environment. Media | | interest may be expected." | | | | The licensee will not issue a press release unless media interest is | | generated. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39564 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 02/06/2003| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 00:12[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/05/2003| +------------------------------------------------+EVENT TIME: 20:58[EST]| | NRC NOTIFIED BY: DEAN BRUCK |LAST UPDATE DATE: 02/06/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KENNETH RIEMER R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO LOW STEAM GENERATOR WATER LEVEL | | | | "In accordance with 10 CFR 50.72(b)(2)(iv)(B) 'Any event or condition that | | results in actuation of the Reactor Protection System (RPS) when the reactor | | is critical except when the actuation results from and is part of a | | pre-planned sequence during testing or reactor operation', DC Cook Unit 2 is | | making a 4 hour non-emergency report. | | | | "On 2-5-03, at 2058, Cook Unit 2 tripped due to a failed 24 VDC control | | group #3 power supply. This caused the feedwater regulating valve for Steam | | Generator #3 to fail closed and the reactor tripped on Feed-flow/Steam-flow | | mismatch coincident with low level on loop 3. All control rods inserted, the | | turbine tripped and auxiliary feedwater pumps started as designed. The Main | | Steam Stop Valves were manually closed during the implementation of the | | Emergency Procedures to stop the RCS cooldown. There were no other notable | | occurrences as a result of the trip. | | | | "The RCS is currently stable in Mode 3 at normal operating pressure and | | temperature. Activities are in progress to determine the cause of the power | | supply failure and the extent of condition." | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021