Event Notification Report for February 5, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/04/2003 - 02/05/2003 ** EVENT NUMBERS ** 39550 39559 39560 39561 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39550 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/31/2003| |LICENSEE: UNIVERSITY OF TEXAS AT AUSTIN |NOTIFICATION TIME: 14:00[EST]| | CITY: AUSTIN REGION: 4 |EVENT DATE: 01/30/2003| | COUNTY: STATE: TX |EVENT TIME: [CST]| |LICENSE#: L00485-000 AGREEMENT: Y |LAST UPDATE DATE: 01/31/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JONES R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN | | | HQ OPS OFFICER: YAMIR DIAZ | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TEXAS AGREEMENT STATE REPORT FOR LEAKING SOURCE | | | | "The University of Texas ordered a Sodium 22 (Na-22) positron source for | | research use. The Type A package arrived during the evening of January 30, | | 2003, and was unpackaged. During un-packaging it was noted that the Source | | was either leaking or contaminated. Attempts to decontaminate the source | | only resulted in higher reading. Leakage was measured at 30,000 DPM, | | therefore, over the 0.0005 uCi [microcurie] leakage limit. | | | | "The source arrived from the manufacturer: National Accelerator Center, | | Somerset West, South Africa. The report was made IAW 25 TAC 289.202 (bbb). | | A follow-up written report will follow by facsimile within 5 days. Chemical | | form of the source is solid sodium bicarbonate sealed in a titanium body. | | Source was leak tested due to the lack of a leak test certificate with the | | shipment. The inner packaging of the Type A container is also contaminated. | | No Model # or Serial # is readily apparent." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39559 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 02/04/2003| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 11:24[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/04/2003| +------------------------------------------------+EVENT TIME: 09:58[EST]| | NRC NOTIFIED BY: JIMMY BURGESS |LAST UPDATE DATE: 02/04/2003| | HQ OPS OFFICER: YAMIR DIAZ +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOEL MUNDY R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP CAUSE BY A HI-HI LEVEL CONDITION IN STEAM GENERATOR | | | | "While replacing a feedwater transmitter, digital feedwater control for CFPT | | (condensate feedwater pump turbines) and all 4 S/G (steam generators) went | | to manual. The corresponding feedwater swing caused a Hi-Hi level condition | | in 1B S/G which resulted in a turbine trip, subsequent reactor trip and | | auxiliary feedwater auto start. All systems functioned normally." All rods | | fully inserted and auxiliary feedwater pumps operated properly. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39560 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 02/04/2003| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 16:05[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 02/04/2003| +------------------------------------------------+EVENT TIME: 14:34[EST]| | NRC NOTIFIED BY: MARK TURKAL |LAST UPDATE DATE: 02/04/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOEL MUNDY R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 94 Power Operation |94 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY | | | | "A licensed operator tested positive for a controlled substance as a result | | of a random test. The employee's access to the protected area has been | | terminated. The employee has requested split sample testing. The NRC | | Resident Inspector has been notified." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39561 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 02/05/2003| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 00:12[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/04/2003| +------------------------------------------------+EVENT TIME: 22:40[EST]| | NRC NOTIFIED BY: ART BREADY |LAST UPDATE DATE: 02/05/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF METEOROLOGICAL DATA AT SALEM AND HOPE CREEK STATIONS | | | | "THIS 8-HOUR NOTIFICATION IS BEING MADE TO REPORT THAT THE SALEM AND HOPE | | CREEK SITE LOST ALL METEOROLOGICAL DATA FOR WIND SPEED, DIRECTION AND | | TEMPERATURE AT 1440 ON 2/04/03. ALL THREE UNITS ARE OPERATING AT 100% POWER. | | NO ACTUATIONS HAVE TAKEN PLACE RELATED TO THIS EVENT. THE CAUSE OF THIS LOSS | | IS BEING INVESTIGATED. PROCEDURAL GUIDANCE IS AVAILABLE TO OBTAIN THE | | NECESSARY DATA FROM THE NATIONAL WEATHER SERVICE SHOULD THIS DATA BE | | NECESSARY." | | | | The licensee will notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021