Event Notification Report for February 3, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/31/2003 - 02/03/2003 ** EVENT NUMBERS ** 39551 39552 39553 39554 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39551 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 01/31/2003| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 19:55[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/30/2003| +------------------------------------------------+EVENT TIME: 13:00[EST]| | NRC NOTIFIED BY: SOSSON |LAST UPDATE DATE: 01/31/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT IN UNANALYZED CONDITION DUE TO INCORRECT INSTALLATION OF DRAIN SYSTEM | | CLEANOUT PLUG | | | | "At 13:00 EST on 1/31/2003, a system manager discovered a dirty radwaste | | floor drain system cleanout plug installed incorrectly in the Unit 1 A/C RHR | | room. The threads on cleanout plug were found not engaged. The plug was | | immediately installed terminating the condition. No check valves are | | installed in this cleanout line and therefore significant back leakage could | | occur into the RHR room. | | | | "This event resulted in a condition that could have rendered all trains of | | the RHR system inoperable during a flooding event by bypassing the normal | | floor drain system. | | | | "The time that this condition began is not currently known, pending | | investigation. A walk down of similar drains on both units is being | | conducted." | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39552 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 02/01/2003| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 04:35[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/01/2003| +------------------------------------------------+EVENT TIME: 02:33[CST]| | NRC NOTIFIED BY: ROBERT TEMPLE |LAST UPDATE DATE: 02/01/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MARK RING R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 50 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM DUE TO CONDENSER TUBE LEAK | | | | "Inserted a manual reactor scram due to a condenser tube leak resulting in | | high condenser, feedwater and reactor water conductivity. " | | | | All control rods inserted into the core. There were no openings of | | power-operated relief valves, relief valves, code safeties, or dump valves. | | Cooldown is being accomplished via the Reactor cleanup to condenser system. | | All safety systems operated as expected. The switchyard is in a stable | | condition. | | | | The NRC Resident Inspector was notified by the Licensee. | | | | *** UPDATE ON 2/2/03 AT 0044 EST FROM MARK GILBERT TO HOWIE CROUCH VIA | | FACSIMILE *** | | | | "DAEC [Duane Arnold Energy Center] is making an addendum to EN [Event | | Number] #39552 made on 2/1/2003 at 0233. EN #39552 reported the insertion of | | a manual scram due to a condenser tube leak which was reportable under 10 | | CFR 50.72(b)(2)(iv)(B) for an RPS actuation. Following the insertion of the | | reactor scram, reactor water level dropped below 170 [inches] and PCIS | | [Primary Containment Isolation Signal] groups 2,3, and 4 were received. All | | isolations went to completion. The reactor water level drop is normal | | following a reactor scram due to the void collapse in the reactor vessel. | | Reactor water level was restored. Currently the plant is stable in Mode 4 | | and maintaining a normal reactor water level band. DAEC is currently making | | plans to determine the source of the condenser tube leak. | | | | "This addendum report is being made under [10 CFR] 50.72(b)(3)(iv)(A), 'Any | | event or condition that results in valid actuation of any systems listed in | | paragraph (b)(3)(iv)(B) of this section.' as a result of the PCIS groups 2 | | (Radwaste and TIP [Tranverse Incore Probe] system) and 3 (Containment | | atmosphere control system)." | | | | The NRC Resident Inspector was notified of the addendum by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39553 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 02/01/2003| | UNIT: [] [2] [] STATE: CA |NOTIFICATION TIME: 09:25[EST]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 02/01/2003| +------------------------------------------------+EVENT TIME: 03:10[PST]| | NRC NOTIFIED BY: MATTHEW THURBURN |LAST UPDATE DATE: 02/01/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JONES R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MAIN GENERATOR LOSS OF EXCITATION CAUSES A TURBINE TRIP THEN A REACTOR TRIP | | | | A loss of main generator excitation caused a turbine trip and, subsequent to | | that, a reactor trip. During the trip sequence, a non-1E electrical bus | | experienced low voltage and automatically transferred to an auxiliary bus. | | During the transfer, both Main Feedwater Pump (MFP) oil pumps tripped | | causing a trip of both MFPs. The loss of Main Feedwater caused low steam | | generator levels which initiated the Emergency Feedwater Actuation System | | (EFAS). EFAS restored steam generator levels to normal. | | | | All control rods inserted into the core. No power-operated relief valves, | | relief valves or code safeties lifted during the trip. The plant is | | removing decay heat via the steam dump to condenser system. The electrical | | grid is stable. The other at the site was not affected. | | | | The cause of the loss of generator excitation is under investigation. | | | | The NRC Resident Inspector was notified of the event by the Licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39554 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 02/01/2003| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 09:41[EST]| | RXTYPE: [2] GE-4 |EVENT DATE: 02/01/2003| +------------------------------------------------+EVENT TIME: 01:45[EST]| | NRC NOTIFIED BY: JEFF GROFF |LAST UPDATE DATE: 02/01/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MARK RING R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF A SAFETY FUNCTION DUE TO ALL FOUR EMERGENCY DIESEL GENERATORS BEING | | DECLARED INOPERABLE | | | | The following information was received from the Licensee via facsimile: | | | | "At 0145 hours [EST] on 2/1/2003, all four Emergency Diesel Generators | | (EDGs) were declared inoperable following discovery of a Fuel Oil leakage | | drain path change that was installed to prevent Fuel Oil leakage from | | reaching the ground water. | | | | "This change involved the installation of plastic sleeves on the fuel oil | | drains for all four EDGs to reroute the fuel oil drains to a catch basin. | | The normal drain path is through the RHR [Residual Heat Removal] Complex | | (which houses the EDGs) drain system to the chemical pond. This change was | | installed after a crack was discovered in a 21 inch concrete line in the | | drain path from the RHR Complex Drain Sump to the Chemical Pond. This change | | was installed on 01/17/03. | | | | "While running EDG 11 for post maintenance testing following a scheduled | | maintenance outage, fuel oil in a drain sleeve backed up and spilled out of | | a vent on the fuel oil drain header. This spillage resulted in a small | | lagging fire. EDG 11 was immediately shutdown and the fire was extinguished | | within a few minutes. No significant damage to EDG 11 was caused by the | | fire. Since all four EDGs had a similar fuel oil drain configuration, they | | were declared inoperable at 0145 hours and Technical Specification 3.8.1, | | Condition B was entered, which requires restoration of one division of the | | EDGs within 2 hours. | | | | "At 0329 hours, the normal fuel oil drain configuration was restored for EDG | | 13 and EDG 14 (Division 2) and Technical Specification 3.8.1, Condition B | | was exited. At 0345 hours, the normal fuel oil drain configuration was | | restored for EDG 12 (Division 1). EDG 11 remains inoperable until the | | completion of post maintenance testing. | | | | "This notification is being made in accordance with 10CFR50.72(b)(3)(v)[(D)] | | due to all four EDGs being inoperable causing the loss of a safety | | function." | | | | The fire was extinguished without offsite assistance and there were no | | injuries due to the fire. | | | | The Licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021