Event Notification Report for January 31, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/30/2003 - 01/31/2003 ** EVENT NUMBERS ** 39439 39539 39546 39547 39548 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39439 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/12/2002| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 00:20[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/11/2002| +------------------------------------------------+EVENT TIME: 18:13[EST]| | NRC NOTIFIED BY: JIM CASE |LAST UPDATE DATE: 01/30/2003| | HQ OPS OFFICER: JASON FLEMMING +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |PATRICK HILAND R3 | |10 CFR SECTION: | | |AINC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RHR B MINIMUM CONTROL FLOW VALVE INOPERABLE | | | | "Scheduled maintenance activities were being performed on RHR B minimum flow | | valve 1E12-F064B which is a containment isolation valve. When the E12-F064 B | | power supply was energized the Control Room indication for the valve | | indicated intermediate. Local indication for the valve indicated the valve | | was closed. When the valve control switch was taken to closed the valve was | | observed to move 1/16 of an inch and the control room indication changed to | | full close. The valve was closed and verified down powered on 12/09/02 to | | comply with Tech Spec 3.6.1.3 Primary Containment Isolation Valves. | | Maintenance test equipment was installed however no maintenance had been | | performed." | | | | Licensee informed NRC resident inspector. | | | | *** RETRACTION ON 01/30/03 AT 1016 ET BY MR. RUSSELL TAKEN BY MACKINNON *** | | | | "Subsequently, an engineering evaluation that utilized the valve as-found | | test data concluded that the valve stem loading was reduced. This resulted | | in the intermediate valve position when the valve breaker was re-energized. | | It was also determined that although the valve stem load was reduced, the | | valve disc remained tightly seated in the closed position. | | | | "The valve provides isolation for a containment penetration that interfaces | | with a closed system outside containment. Since the valve was determined to | | have remained closed, and the closed system outside containment had not been | | breached, there was no loss of the containment accident mitigation function | | and no loss in the control of radiation release function. Since neither of | | these two functions was lost, there was no reportable condition, and this | | Event Notification (EN# 39439) is retracted." R3DO (Mark Ring) notified. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39539 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 01/27/2003| |LICENSEE: ISOTOPE PRODUCTS LABORATORIES |NOTIFICATION TIME: 15:16[EST]| | CITY: BURBANK REGION: 4 |EVENT DATE: 01/23/2003| | COUNTY: LOS ANGELES STATE: CA |EVENT TIME: 16:30[PST]| |LICENSE#: CA-1509 AGREEMENT: Y |LAST UPDATE DATE: 01/27/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JONES R4 | | |FRED BROWN NMSS | +------------------------------------------------+TIM MCGINTY IRO | | NRC NOTIFIED BY: ROBERT GREGER |CREWS NRC | | HQ OPS OFFICER: GERRY WAIG |JOHN HICKEY NMSS | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - CONTAMINATED PACKAGE | | | | The following is taken from a facsimile from the State of California: | | | | "On 1/24/03 the RSO [Radiation Safety Officer] @ IPL [Isotope Products | | Laboratories] reported their receipt of a contaminated package. The package | | had been picked up from LAX & delivered to IPL on 1/23 @ 2:25 pm by Kamino | | Int'l Transport, 2580 Santa Fe, Redondo Beach, contact person [DELETED]. The | | package was wiped upon receipt, and received the results approximately 4:30 | | pm. The RSO was notified the next morning. The contamination appears to be | | H-3, although the licensee needs to perform an energy calibration on their | | liquid scintillation counter to verify both this and their quantification of | | the package wipes. It appears that all sides of the package were | | contaminated, at up to approximately 100,000 dpm/wipe. The latest wipes | | measured up to approximately 40,000 dpm/wipe. | | | | "The package came from a company in Switzerland called RC Tritec AG, who is | | a distributor for a Russian company (unknown name at this time). IPL | | believes that the box was trans-shipped, & was never actually at Tritec, but | | they're still trying to get Lufthansa's paperwork. IPL is also trying to get | | info on the Russian company. | | | | "IPL had the delivery truck return to IPL, & they found a small area of | | contamination, about 12 X 10 inches, on the carpet, where the package was | | located, of about 800 dpm/wipe. After vacuuming, they got nothing. About 11 | | other wipes in the truck were negative. They checked the driver's gloves- | | there's no removable contamination. All wipes @ IPL's Shipping Dept were | | negative. They think there was at least one other package on the truck that | | was destined for an electronics company, but they're still trying to get | | info on that. There was at least one other package for IPL on the truck that | | was not contaminated (they're checking to see if it had come from the same | | Russian company). | | | | "Note: Assuming that the contamination is H-3, the dose consequences of | | 100,000 dpm/wipe are approximately equivalent to the dose consequences of | | 2.5 dpm/wipe of Cs-137." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39546 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 01/29/2003| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 20:57[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/29/2003| +------------------------------------------------+EVENT TIME: 20:32[EST]| | NRC NOTIFIED BY: VAL MANCE |LAST UPDATE DATE: 01/30/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |J. BRADLEY FEWELL R1 | |10 CFR SECTION: |WILLIAM RULAND NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |JOSEPH HOLONICH IRO | | |DORA HEYMAN FEMA | | |P.O. BAUMGARTNER EPA | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOUE DECLARED AT SUSQUEHANNA DUE TO NON-ROUTINE RADIOACTIVE GAS RELEASE | | | | "At 8:32 pm EST PPL Susquehanna , LLC, declared an Unusual Event for an | | Airborne Release. The EAL entered was 15.1.a A.2, I-131 > 2.08E+2 | | microcuries/minute. Chemistry sample did not indicate any Iodine in the | | release steam, however Cs-138 was detected in the sample which may have | | affected the vent stack monitor. Investigation continues. The release is | | being monitored by the plant Vent Stack monitoring system. The source of the | | release is unknown at this time. Plant procedures are being implemented to | | determine and isolate the source. Offsite monitors have been activated to | | monitor offsite dose rates. Activation of the Emergency plan and Offsite | | releases are reportable under 10CFR50.72(a)(1) and 10CFR50.73(a)(2)(viii)." | | | | The licensee has notified state and local officials and will notify the NRC | | Resident Inspector. A media/press release is planned. | | | | *** UPDATE at 0132 ET on 01/30/03 by Dave Flyte/ Phil Brady taken by | | MacKinnon **** | | | | Unusual Event was terminated at 0125 ET on 01/30/03. Investigation found | | that the release was from the off gas system via a drain trap which entered | | the ventilation system which then exited out the vent stack. According to | | licensee's records, the release was greater than 2 times their Technical | | Specification limit (208 microcuries per minute) from 1940 hours until 2111 | | hours. Max level detected was 600 microcuries per minute. No iodine was | | released just noble gases. NRC R1DO (Brad Fewell), FEMA (Nora Heyman), | | NRC/DOT (Petty Officer Baumgartner), Office of Homeland Security (Damon | | Edwards), and NRR EO (Bill Ruland) notified. | | | | The NRC Resident Inspector was notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39547 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 01/30/2003| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 14:23[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 01/30/2003| +------------------------------------------------+EVENT TIME: 11:30[MST]| | NRC NOTIFIED BY: DAN MARKS |LAST UPDATE DATE: 01/30/2003| | HQ OPS OFFICER: YAMIR DIAZ +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JONES R4 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INFORMATION CALL CONCERNING PRESS RELEASE ON SAFEGUARDS EVENT | | | | Press release regarding a safeguards event involving a flyover at Palo | | Verde. The press release was made by a local radio station, KTAR. | | | | The NRC resident inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39548 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 01/30/2003| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 14:42[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/30/2003| +------------------------------------------------+EVENT TIME: 10:54[CST]| | NRC NOTIFIED BY: BEARD |LAST UPDATE DATE: 01/30/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JONES R4 | |10 CFR SECTION: | | |ACCS 50.72(b)(2)(iv)(A) ECCS INJECTION | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM ON DECREASING REACTOR VESSEL LEVEL | | | | "At 10:54 CDT Grand Gulf Nuclear Station inserted a manual scram on | | decreasing vessel level as a result of the loss of all 3 condensate booster | | pumps. Loss of the booster pumps resulted in loss of normal feedwater to the | | vessel. Vessel level decreased to the auto initiation set point for High | | Pressure Core Spray (HPCS), Reactor Isolation Cooling System (RCIC), and | | Containment Isolation System. HPCS and RCIC started and injected to the | | vessel and the containment isolated. The HPCS initiation also included an | | auto start of the HPCS Diesel as expected. Reactor level was restored by | | injection of HPCS and RCIC. Vessel pressure was maintained by the turbine | | bypass valves. At present vessel level has been restored to normal. Systems | | affected by the containment isolation have been restored as needed. The | | cause of the condensate booster trips is under investigation. A review of | | plant data is underway to confirm proper response by equipment." | | | | There was an ECCS injection for 5 - 10 minutes. All control rods inserted | | and no relief valves lifted. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021