Event Notification Report for January 28, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/27/2003 - 01/28/2003 ** EVENT NUMBERS ** 39480 39538 39540 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39480 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 12/31/2002| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 01:34[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 12/30/2002| +------------------------------------------------+EVENT TIME: 20:10[CST]| | NRC NOTIFIED BY: JAMES McKAY |LAST UPDATE DATE: 01/27/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AINB 50.72(b)(3)(v)(B) POT RHR INOP | | |AINA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | |AINC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MONTICELLO INITIATED TS REQUIRED PLANT SHUTDOWN DUE TO INOPERABILITY OF BOTH | | EDGs | | | | "With #12 EDG inoperable due to a maintenance issue [on 12/29/02 at 2330 | | CST] , it is required to test #11 EDG within 24 hours. Testing causes #11 | | EDG to be inoperable, therefore both EDGs are inoperable requiring [the | | initiation of] a plant shutdown per T.S. 3.9.B.3.a.2 and a non-emergency | | notification per 10 CFR 50.72/8 hour. #11 EDG subequently tested operable | | and the plant exited T.S. shutdown requirement at 2300 on 12/30/02." | | | | The licensee stated that the period of time both EDGs were inoperable was | | from 2010 to 2300 on 12/30/02. The inoperablity of the #12 EDG was due to | | an equipment problem with the DC fuel oil pump. After fixing the DC fuel | | oil pump on the #12 EDG, the EDG was restarted and the "failure-to-start" | | alarm lit and the "cranking" alarm lit and stayed in for 5 minutes. The | | licensee is currently evaluating these problems. The #12 EDG remains in a 7 | | day limiting LCO action statement. The #11 EDG started and tested | | satisfactorily with no problems. The inoperability of the #11 EDG was due to | | some of the set up conditions for testing when the EDG is considered to be | | inoperable per procedure. | | | | The NRC Resident Inspector was notified. | | | | * * * RETRACTED ON 1/27/03 AT 1714 EST BY DAVID BARNETT TO GERRY WAIG * * * | | | | | | "On 12/29/02 at 2330 CST, the Monticello nuclear power plant notified the | | NRC operations center of the #12 EDG being declared inoperable when | | personnel noted an equipment problem during surveillance testing. In | | addition, the #11 EDG was declared inoperable due to station Technical | | Specification required surveillance testing to prove operability of the #11 | | EDG while the #12 EDG was inoperable. The report was made pursuant to | | 10CFR50.72(b)(3)(v) under Event Notification number 39480. | | | | "Upon further review, Monticello is retracting the event reported based on | | the information in NUREG-1022, Rev. 2, page 56, which states, 'The following | | types of events or conditions generally are not reportable under these | | conditions. Sub-item 3 states: removal of a system or part of a system from | | service as part of a planned evolution for maintenance or surveillance | | testing when done in accordance with an approved procedure and the plant's | | TS (unless a condition is discovered that could have prevented the system | | from performing its function).' | | | | "The station condition reported in Event Report #39480 was determined not to | | be reportable based on the following: | | 1) #11 EDG was inoperable due to the performance of a surveillance test in | | accordance with the station's Technical Specifications and an approved | | procedure; and | | 2) #11 EDG successfully passed the surveillance test to prove operability. | | Additionally, the required TS LCO action statement requiring plant shutdown | | was entered. The appropriate procedure was entered. However the station was | | not required to reduce power or initiate shutdown by inserting negative | | reactivity and additionally the shutdown was not imminent, since the #11 EDG | | was confirmed to be operable." | | | | The licensee has notified the NRC Resident Inspector, State of Minnesota, | | and Local Government of this retraction. | | | | Notified R3DO (Mark Ring) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39538 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 01/27/2003| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 10:05[EST]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 01/27/2003| +------------------------------------------------+EVENT TIME: 08:44[EST]| | NRC NOTIFIED BY: JEFF DEAL |LAST UPDATE DATE: 01/27/2003| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KEN BARR R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 3 MANUALLY TRIPPED DUE TO LOW STEAM GENERATOR LEVELS | | | | The following information was submitted via facsimile: | | | | "Manual reactor trip on Unit 3 due to low steam generator levels caused by a | | loss of instrument air pressure. Instrument air pressure has been | | restored." | | | | Operators manually tripped Unit 3 following the loss of instrument air (IA) | | pressure which resulted in closing of the main feedwater regulating valves. | | IA can be supplied from one of four compressors; two motor driven and two | | diesel driven. When the operating motor driven air compressor breaker | | tripped, both diesel driven compressors received a start signal (the other | | motor driven compressor had been previously removed from service). One of | | the diesel driven compressors failed to start while the other started and | | tripped. IA pressure was restored by manually starting one of the diesel | | units. The licensee has the cause of the IA loss under investigation. | | | | Following the manual reactor trip, all three turbine driven auxiliary | | feedwater pumps started as expected. The licensee is in the process of | | restoring normal feedwater and returning the auxiliary feedwater pumps to | | standby. The atmospheric steam dumps are currently in service to remove | | decay heat (no known primary-secondary leakage). All control rods fully | | inserted. | | | | The licensee will notify the resident inspector and does not plan a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39540 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 01/27/2003| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 17:40[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 01/22/2003| +------------------------------------------------+EVENT TIME: 21:51[CST]| | NRC NOTIFIED BY: HAROLD VINYARD |LAST UPDATE DATE: 01/27/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MARK RING R3 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID AUTOMATIC START OF EMERGENCY DIESEL GENERATOR DURING TESTING | | | | "On January 22, 2003, at 2045 hours, with Unit 2 in Mode 5 (refuel), the 2B | | Emergency Diesel Generator (DG) automatically started during the performance | | of a Unit 2 High Pressure Excess Flow Check Valve Operability Test. The | | apparent cause was an improper manipulation of instrument isolation valves | | during the test, which caused the associated Reactor Vessel Water Level | | Transmitters to sense a low level condition. This invalid low level signal | | resulted in the automatic actuation of the 2B DG (Div. III) which is the | | emergency power supply to the Unit 2 High Pressure Core Spray (HPCS) System. | | The Unit 2 HPCS pump had been properly removed from service prior to the | | event and therefore did not actuate. This system actuation is reportable | | under 10CFR50.73 (a) (2) (iv) (A). | | | | "The 2B DG responded normally and reached normal speed and voltage. It was | | run both loaded and unloaded successfully, and was secured at 0238 on | | January 23, 2003. | | | | "This report is being made in accordance with 10CFR50.73 (a) (1), which | | states that in the case of an invalid actuation reported under | | 10CFR50.73(a)2)(iv), other than an actuation of the RPS when the reactor is | | critical, the licensee may provide a telephone notification to the NRC | | operations center within 60 days after discovery of the event Instead of | | submitting a written LER." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021