Event Notification Report for January 21, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/17/2003 - 01/21/2003 ** EVENT NUMBERS ** 39508 39519 39520 39521 39522 39523 39525 39526 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39508 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OK DEQ RAD MANAGEMENT |NOTIFICATION DATE: 01/14/2003| |LICENSEE: ST FRANCIS HOSPITAL |NOTIFICATION TIME: 15:02[EST]| | CITY: TULSA REGION: 4 |EVENT DATE: 01/13/2003| | COUNTY: STATE: OK |EVENT TIME: 19:30[CST]| |LICENSE#: OK-07163-01 AGREEMENT: Y |LAST UPDATE DATE: 01/15/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SANBORN R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MIKE BRODERICK | | | HQ OPS OFFICER: JASON FLEMMING | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING LOST SOURCES | | | | The Licensee reported the loss of five 0.355 microcurie, I-125 brachytherapy | | seeds. The seeds were model # IAI-125A and they were inventoried upon | | receipt from the manufacturer, Iso-Aid. The seeds were being washed prior | | to sterilization (this is a deviation from procedure) and the licensee | | believes they were washed down the drain to the public sewer system. The | | Licensee reports that surveys do not indicate that they are in the sink or | | trap. | | | | ***UPDATE 01/15/03 1202 EST MIKE BRODERICK TO MIKE NORRIS*** | | | | The seeds are actually 0.355 millicurie sources. Notified NMSS (Brown) and | | R4DO (Sanborn). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39519 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 01/17/2003| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 14:35[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/17/2003| +------------------------------------------------+EVENT TIME: 11:30[EST]| | NRC NOTIFIED BY: KEN TIEFENTHAL |LAST UPDATE DATE: 01/17/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO VIOLATION OF DISCHARGE PERMIT | | | | The following information was obtained from a facsimile from the Licensee: | | | | "On 1/17/2003 at 1130 hours, the Beaver Valley Power Station received | | notification that an operator found raw sewage running from the Unit 2 | | Sewage Treatment Plant through a slightly open connection and immediately | | closed the isolation valve, stopping the flow. | | | | "Assessment by the Beaver Valley response determined that a sewage removal | | vendor had previously attempted to pump sludge from a plant sewage system, | | but nothing came out. He then apparently only partially closed the | | isolation valve and left the site. Subsequently, sewage began to flow out. | | Approximately 750 gallons of sewage was released down a storm sewer [drain]. | | An unknown quantity of sewage entered the Ohio River via Peggs Run. | | Approximately 50 gallons of sewage remaining on the surface at the local | | location is being cleaned up. | | | | "Pennsylvania Department of Environmental Protection (DEP) has been | | notified. | | | | "This event is being reported pursuant to 10 CFR 50.72(b)(2)(xi) as a | | situation related to the protection of the environment for which | | notification to other government agencies have been made. The NRC resident | | has been notified." | | | | The notification to the Pennsylvania DEP was made due to a violation of the | | plant's discharge permit. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39520 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 01/17/2003| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 16:28[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 01/17/2003| +------------------------------------------------+EVENT TIME: 14:43[EST]| | NRC NOTIFIED BY: PHILLIP ROSE |LAST UPDATE DATE: 01/17/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAY HENSON R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |95 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION REQUIRED SHUTDOWN DUE TO FAILED SURVEILLANCE ON | | REACTOR TRIP BREAKER | | | | The following information was obtained from the licensee via facsimile: | | | | "At 11:40 [EST] on January 17, 2003, during surveillance testing of the 'B' | | train Reactor Trip Breaker (RTB), the breaker spuriously opened. This | | caused the RTB to fail its surveillance test and be declared inoperable. | | The facility Technical Specifications (TS), LCO 3.3.1 (Reactor Trip System | | Instrumentation), Action 8 of Table 3.3-1 requires 6 hours to Mode 3, Hot | | Standby. Rework activities were begun but the station commenced a power | | decrease at 14:43 [EST] to comply with the requirements of the TS. | | | | "At 15:10 [EST] on January 17, 2003, the activities, including retesting | | were completed and the breaker was declared operable at which time the plant | | exited from the TS Limiting Condition for Operability Action. At this time | | the power decrease was stopped. Power was held stable at 95% awaiting | | completion of all paperwork associated with this surveillance test. Power | | ascension commenced at 15:55 [EST]." | | | | Determined from the Licensee that the Reactor Trip Breaker spuriously opened | | after it was closed during the test. The breaker was replaced with another | | breaker and the surveillance test was performed on the new breaker | | successfully. | | | | The Licensee has informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39521 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 01/19/2003| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 12:19[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/19/2003| +------------------------------------------------+EVENT TIME: 10:11[EST]| | NRC NOTIFIED BY: DAVID WALSH |LAST UPDATE DATE: 01/19/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD BARKLEY R1 | |10 CFR SECTION: |TAD MARSH NRR | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS |MOHAMED SHANBAKY R1 | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 77 Power Operation |50 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SUSQUEHANNA UNIT 1 SHUTDOWN REQUIRED BY TECHNICAL SPECIFICATIONS | | | | The following is taken from a facsimile sent by the licensee: | | | | "At 10:11 hrs on 1/19/2003 Susquehanna Unit 1 began a shut down required by | | Technical Specifications. | | | | "At 13:06 hrs on 1/16/2003 the 'B' diesel generator was being returned to | | service following maintenance. This placed Unit 1 and Unit 2 into a 72 hour | | LCO (3.8.1 Cond. B). During its operability run, the governor exhibited | | erratic operation and the diesel was shut down. The 'E' diesel generator was | | re-substituted for the 'B' and an operability run was initiated. During the | | run, the 'E' diesel generator tripped on reverse power. Station personnel | | continue to troubleshoot the unrelated problems with the diesel generators. | | Initial engineering analysis has determined that there is no common mode | | failure with these 2 problems or with the remaining 3 operable diesel | | generators. | | | | "The 72 hour LCO for inoperability of 1 Diesel Generator (3.8.1 Cond. B) | | will expire at 13:06 hrs today. This will require both Unit 1 and Unit 2 to | | enter LCO 3.8.1 Cond. F, which requires both units to be in Hot Shutdown | | within 12 hours and Cold Shutdown within 36 hours. | | | | "An additional ENS report will be made when power reduction begins on Unit | | 2." | | | | The licensee has notified the NRC Resident Inspector of this event and plans | | to make a press release. | | | | * * * UPDATE 1600EST ON 1/19/03 FROM DAVID WALSH TO S. SANDIN * * * | | | | "At 15:38 hrs on 1/19/2003 the 'E' diesel generator was declared operable. | | This returned the station to 4 operable diesel generators and allowed | | exiting the LCO 3.8.1 Cond. B and Cond. F. Power reduction on Unit 1 was | | halted at approximately 50%. Unit 2 remained at 100% power. Current plans | | are to return Unit 1 to 100% power." | | | | The licensee is reviewing whether a press release will be made. Also, the | | licensee informed the NRC resident inspector of this update. Notified | | R1DO(Barkley) and NRR EO(Marsh). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39522 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 01/19/2003| | UNIT: [] [2] [] STATE: VA |NOTIFICATION TIME: 14:59[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/19/2003| +------------------------------------------------+EVENT TIME: 12:52[EST]| | NRC NOTIFIED BY: B. J. BROWN |LAST UPDATE DATE: 01/19/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAY HENSON R2 | |10 CFR SECTION: | | |AMED 50.72(b)(3)(xii) OFFSITE MEDICAL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAMINATED, INJURED WORKER TRANSPORTED TO LOCAL MEDICAL FACILITY | | | | The following is taken from a facsimile from the licensee: | | | | "At 1252 today, a worker in a Contaminated Area in Unit 2 Containment became | | overheated and required medical attention. The first aid team responded and | | required that the individual be transported while he was still contaminated. | | The individual has 100K [100,000] dpm by direct frisk on his skin in the | | area of his face and 10K [10,000] dpm by direct frisk on his clothing he was | | wearing. He was transported by local Rescue Squad. While in the ambulance he | | was decontaminated by HP [Health Physics] personnel that were assisting. | | Medical College of Virginia (MCV) was notified of a potentially contaminated | | person that was enroute. The individual is still being transported to MCV | | where he will receive medical treatment. The individual and ambulance are | | now clean and all contaminated material will be transported back to NAPS | | [North Anna Power Station]" | | | | The contaminated, injured worker was working on the installation of the | | blind flange on the fuel transfer tube. The North Anna Unit 2 reactor is | | refueled. | | | | The licensee will notify the NRC Resident Inspector of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39523 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 01/19/2003| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 21:25[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/19/2003| +------------------------------------------------+EVENT TIME: 12:55[CST]| | NRC NOTIFIED BY: GREG JANAK |LAST UPDATE DATE: 01/19/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GARY SANBORN R4 | |10 CFR SECTION: |TAD MARSH NRR | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N N 0 Hot Standby |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VARIOUS SYSTEM ACTUATIONS AS A RESULT OF THE LOSS OF OFFSITE POWER | | | | The following information was received via facsimile: | | | | "At 1255 hrs on January 19, 2003, Unit 1 was in Mode 1 at 100% power and | | Unit 2 was in Mode 3 with Trains A and D reactor coolant pumps (RCP) | | running. While placing a surge reactor in the switchyard in service the Unit | | 1 standby transformer received a lockout and total loss of the North bus. | | | | "Unit 1 experienced a loss of offsite power (LOOP) to ESF Trains B & C. Both | | the Train B & Train C emergency diesel generators (EDG) started as expected. | | The Train C sequencer operated as expected and the Train C components | | automatically loaded, However, the Train B sequencer failed resulting in the | | manual loading of the Train B components in accordance with station | | off-normal procedures. This resulted in TS 3.0.3 entry in Unit 1 due to the | | loss of two (2) offsite power sources and the B train EDG (due to the | | failure of the B Train sequencer). There was a loss of letdown in Unit 1 | | when Train C isolated. Letdown was restored at 1313 hrs. At 1345 Unit 1 | | exited TS 3.0.3 when offsite power was restored to B Train. At 1406, offsite | | power was restored to C Train. The cause of the fault in the switchyard and | | failed Train B sequencer are under Investigation. | | | | "In Unit 2, Train A was aligned to the Unit 1 Standby transformer therefore, | | Unit 2 experienced a LOOP to ESF Train A. Train A emergency diesel generator | | automatically started and loaded as expected. As a result of the LOOP, Unit | | 2 experienced a loss of circulating water and loss of condenser vacuum. The | | Steam Generators (SGs) were already being supplied by the Auxiliary | | Feedwater system therefore no interruption to SG cooling. In addition, both | | Train A and Train D reactor coolant pumps tripped resulting in entry into TS | | 3.4.1.2, action B & C (boron control limitations and ensure Rx trip breakers | | open). There was a loss of charging due to the LOOP resulting in a Loss of | | RCP seal injection, however, component cooling water flow to the thermal | | barrier maintained seal cooling. Charging has been restored to supply seal | | injection. At 1840, when starting RCP 2A, pressurizer PORV 655A opened and | | reseated due to a pressure spike. Unit 1 remains at 100% power and Unit 2 | | remains in Mode 3." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39525 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 01/20/2003| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 14:40[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/20/2003| +------------------------------------------------+EVENT TIME: 10:40[EST]| | NRC NOTIFIED BY: DENNIS MOORE |LAST UPDATE DATE: 01/20/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAY HENSON R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RANDOM FITNESS FOR DUTY TEST FAILURE | | | | "A non-licensed contract supervisor tested positive during a random test. | | The employee's access to the plant has been restricted." Contact the HOO for | | additional details. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39526 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 01/20/2003| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 20:13[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/20/2003| +------------------------------------------------+EVENT TIME: 14:30[EST]| | NRC NOTIFIED BY: JAMES WITTER |LAST UPDATE DATE: 01/20/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN ROGGE R1 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SERVICE WATER SYSTEM VALVE PIT PIPING PENETRATION SEAL | | | | "On 1/20/2003 at 1430 hours, the Beaver Valley Power Station control room | | was notified by Engineering that a penetration seal previously installed in | | a wall which separates two service water system valve pits may have not been | | adequate. A review of the supporting analysis shows that this penetration | | seal may not be qualified to withstand the hydraulic pressure which could | | result from a postulated internal flooding event occurring due to a service | | water system pipe failure filling the valve pit and its above compartment | | prior to operator intervention. A failure of this seal during a postulated | | internal flooding event may result in the loss of motor operated valve | | movement in both trains of the service water system that would be needed | | following a design basis accident (DBA). | | | | "This design basis calculation and the penetration seal capability are | | continuing to be evaluated. However, this seal could potentially have | | prevented the service water system from meeting single failure criterion | | during a postulated service water system pipe failure. Therefore, Technical | | Specification (TS) 3.7.4.1 was entered due to less than two trains of | | service water system being operable as a conservative decision based upon | | the limited information immediately available to show acceptable seal | | integrity at the postulated conditions. The TS Action requires restoration | | of two independent service water system trains within 72 hours. Actions are | | in progress to install a qualified seal which will prevent the unacceptable | | flooding conditions from being able to occur. | | | | "This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii) as an | | unanalyzed condition that significantly degraded plant safety since this | | seal has been installed for five months and may have invalidated the | | independence between the two service water system trains. The NRC resident | | has been notified of the degraded condition." | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021