Event Notification Report for January 15, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/14/2003 - 01/15/2003 ** EVENT NUMBERS ** 39507 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39507 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 01/14/2003| | UNIT: [1] [] [] STATE: VA |NOTIFICATION TIME: 04:18[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/14/2003| +------------------------------------------------+EVENT TIME: 01:37[EST]| | NRC NOTIFIED BY: ALISON MACKELLAR |LAST UPDATE DATE: 01/14/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: |TERRY REIS NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO HIGH REACTOR COOLANT PUMP SHAFT VIBRATION | | | | "At 0137 hours, with Surry Power Station Unit 1 at 100% reactor power, a | | manual reactor trip was initiated due to elevated shaft vibrations (alert | | and danger) on 'C' Reactor Coolant Pump. | | | | "IRPI indication for one control rod indicated 25 steps following the trip. | | Borated as necessary to ensure adequate shutdown margin. All other control | | rods fully inserted into the core as designed. The IRPI indication for this | | rod is trending down at this time. The shutdown margin for Unit 1 was | | determined to be satisfactory. Auxiliary feedwater automatically initiated | | as designed on low low steam generator level following the trip. Primary | | RCS temperature decreased to approximately 541 degrees following the reactor | | trip and was stabilized at 547 degrees. | | | | "No primary safety or power operated relief valves were actuated during the | | event. As a result of the loss of turbine load, the secondary power operated | | relief valves actuated during the transient. No indication of primary to | | secondary leakage exists, therefore no adverse radiological consequences | | resulted from this event. | | | | "All electrical busses transferred properly following the trip. #1 EDG was | | T/O [tagged out] prior to unit trip. All other emergency diesel generators | | are operable. There were no radiation releases due to this event, nor were | | there any personnel injuries or contamination events. The cause of the | | event is being investigated. | | | | "Unit 1 is currently at Hot Shutdown with RCS temperature being maintained | | at approximately 547 degrees. Unit 2 was not affected by this event and | | remains stable at 100% power operations. This event Is being reported in | | accordance with 10CFR50.72(b)(2)(iv) and 10CFR50.72(b)(3)(iv)." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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