Event Notification Report for January 14, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/13/2003 - 01/14/2003 ** EVENT NUMBERS ** 39505 39506 39507 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39505 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 01/13/2003| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 02:48[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/12/2003| +------------------------------------------------+EVENT TIME: 23:04[EST]| | NRC NOTIFIED BY: RITA BRADDICK |LAST UPDATE DATE: 01/13/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD CONTE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OPEN DUCTWORK ACCESS PANEL PREVENTED MAINTAINING CONTROL ROOM POSITIVE | | PRESSURE | | | | "On January 12, 2003 at 2304, control room pressure was observed to be | | negative. At the time the "A" Control Room Emergency Filtration (CREF) | | system was tagged out for scheduled maintenance. The event was initiated | | when technicians opened an access panel on the "A" CREF control room air | | supply duct within the control room boundary to repair a gasket. This | | resulted in both "A" and "B" trains of CREF unable to perform its design | | safety function: specifically, maintaining the control room at a 1/8 inch | | water gauge positive pressure relative to adjacent areas. Without assurance | | of CREF system providing positive pressure in the control room, mitigating | | the consequences of an accident could have been prevented. Upon discovering | | the cause, technicians were ordered to close the access panel. Control room | | pressure promptly returned to a normal, positive value. Total time at | | negative pressure was ten minutes. No unexpected response was experienced. | | In addition to the "A" CREF train, the "A" Hydrogen/Oxygen analyzer was | | inoperable at the time of the event." | | | | The licensee has notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39506 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 01/13/2003| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 08:47[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 01/13/2003| +------------------------------------------------+EVENT TIME: 06:18[EST]| | NRC NOTIFIED BY: ANDREW BARTLIK |LAST UPDATE DATE: 01/13/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD BARKLEY R1 | |10 CFR SECTION: |JOHN HANNON NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO LOSS OF CONDENSER CIRCULATING WATER PUMP | | | | At 0618 EST the #35 Circulating Water Pump tripped. The other circulating | | water pump supplying the same condenser section was out of service for | | maintenance. The resulting loss of all circulating water to one condenser | | section produced a high differential pressure between sections. The reactor | | was manually tripped in accordance with plant procedures. All controlled | | rods fully inserted. The Auxiliary Feedwater Pump automatically started as | | expected. During the transient, the #32 Reactor Coolant Pump tripped due to | | an unknown cause and is being investigated. Additionally, the # R14 Plant | | Vent Gas radiation monitor went into alarm and then immediately returned to | | normal, however the redundant monitor did not show any increase in | | radiation. Additionally, the #32 Source Range Detector did not come on | | scale on the reactor trip, however the redundant detector functioned | | normally. The electrical system responded normally. There were no releases | | associated with this event. The cause of the circulating water pump trip is | | under investigation. | | | | The licensee has notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39507 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 01/14/2003| | UNIT: [1] [] [] STATE: VA |NOTIFICATION TIME: 04:18[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 01/14/2003| +------------------------------------------------+EVENT TIME: 01:37[EST]| | NRC NOTIFIED BY: ALISON MACKELLAR |LAST UPDATE DATE: 01/14/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO HIGH REACTOR COOLANT PUMP SHAFT VIBRATION | | | | "At 0137 hours, with Surry Power Station Unit 1 at 100% reactor power, a | | manual reactor trip was initiated due to elevated shaft vibrations (alert | | and danger) on "C" Reactor Coolant Pump. | | | | IRPI indication for one control rod indicated 25 steps following the trip. | | Borated as necessary to ensure adequate shutdown margin. All other control | | rods fully inserted into the core as designed. The IRPI indication for this | | rod is trending down at this time. The shutdown margin for Unit 1 was | | determined to be satisfactory. Auxiliary feedwater automatically initiated | | as designed on low low steam generator level following the trip. Primary | | RCS temperature decreased to approximately 541 degrees following the reactor | | trip and was stabilized at 547 degrees. | | | | "No primary safety or power operated relief valves were actuated during the | | event. As a result of the loss of turbine load, the secondary power operated | | relief valves actuated during the transient. No indication of primary to | | secondary leakage exists, therefore no adverse radiological consequences | | resulted from this event. | | | | "All electrical busses transferred properly following the trip. #1 EDG was | | T/O [tagged out] prior to unit trip. All other emergency diesel generators | | are operable. There were no radiation releases due to this event, nor were | | there any personnel injuries or contamination events. The cause of the | | event is being investigated. | | | | "Unit 1 is currently at Hot Shutdown with RCS temperature being maintained | | at approximately 547 degrees. Unit 2 was not affected by this event and | | remains stable at 100% power operations. This event Is being reported In | | accordance with 10CFR50.72(b)(2)(iv) and I0CFR50.72(b)(3)(iv)." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021