Event Notification Report for January 13, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/10/2003 - 01/13/2003 ** EVENT NUMBERS ** 39494 39498 39500 39501 39502 39503 39504 39505 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39494 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 01/07/2003| |LICENSEE: SPECTRO INSTRUMENTS |NOTIFICATION TIME: 18:32[EST]| | CITY: MARBLE FALLS REGION: 4 |EVENT DATE: 01/07/2003| | COUNTY: STATE: TX |EVENT TIME: 16:24[CST]| |LICENSE#: L02788 AGREEMENT: Y |LAST UPDATE DATE: 01/07/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHUCK CAIN R4 | | |E. WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HELEN WATKINS | | | HQ OPS OFFICER: ARLON COSTA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT ON LEAKING SOURCES | | | | Texas Department of Health received a telephone notification from Spectro | | Instruments that two 50 microcurie Fe-55 sources were leaking. Sources S/N | | 5069LG and S/N 6172LG were leak tested 0.4 microcuries and 0.13 microcuries | | respectively. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39498 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 01/10/2003| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 12:47[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 01/10/2003| +------------------------------------------------+EVENT TIME: 09:00[EST]| | NRC NOTIFIED BY: ALAN RABENOLD |LAST UPDATE DATE: 01/10/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO LOCAL COUNTY EMERGENCY AGENCIES | | | | "At 0905, an injury occurred to a worker when the individual received 2nd | | degree burns to his forearms. The worker was treated by the Company First | | Aid Team and released to Radiation Protection Personnel for deconning the | | individual. The burn area had some contamination of 100 to 400 counts above | | background. The individual was deconned by our Radiation Protection | | Personnel and our Company Medical Personnel and is no longer contaminated. | | The individual was released back to work. | | The local County Emergency Management Agencies were notified of the | | potential for transportation of the individual to a local hospital, but | | transportation will not be required. The individual has requested no | | medical treatment from the local hospital. The local County Emergency | | Management Agencies were re-notified that the individual would not be | | transported." | | | | The State of Ohio and local Counties were informed of this event. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39500 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 01/10/2003| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 16:05[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 01/10/2003| +------------------------------------------------+EVENT TIME: 11:56[CST]| | NRC NOTIFIED BY: AL BAILEY |LAST UPDATE DATE: 01/10/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 91 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL SCRAM DUE TO LOWERING REACTOR VESSEL WATER LEVEL | | | | "This report is being made pursuant to 10CFR50.72(b)(2)(iv)(B), RPS | | Actuation (scram). At 11:56 CDST on January 10,2003, during normal | | operation, unit 2 was manually scrammed due to lowering vessel water level. | | The lowering water level was from the loss of the 2B Condensate pump and the | | 2A & 2C Heater Drain pumps which resulted in a loss of both Turbine Driven | | Feed Pumps. ECCS equipment responded as expected (no automatic injection or | | starts). Hot Standby Mode of Operation was achieved with out difficulties | | and residual heat is being rejected to the condenser. No Safety Relief | | Valves actuated. | | | | "Initial investigation revealed that the 2B condensate pump motor failed and | | may have resulted in an electrical fluctuation on electrical buses resulting | | in tripping some non-essential components. Further investigation, including | | troubleshooting is in progress for activities related to the condensate and | | heater drain pump loss." | | | | All rods properly inserted into the core. The licensee notified the NRC | | Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39501 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 01/11/2003| | UNIT: [1] [2] [] STATE: NJ |NOTIFICATION TIME: 07:15[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/10/2003| +------------------------------------------------+EVENT TIME: 23:20[EST]| | NRC NOTIFIED BY: JOE SULLIVAN |LAST UPDATE DATE: 01/11/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD CONTE R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF ALL METEOROLOGICAL DATA FOR WIND SPEED, DIRECTION, AND TEMPERATURE | | | | This report is from the Salem/Hope Creek site. Both Salem units and the | | Hope Creek unit are in power operation. | | | | "This 8-hour notification is being made to report that the Salem and Hope | | Creek site lost all meteorological data for wind speed, direction and | | temperature at 1520 [EST] on 1/10/03. All three units are operating at 100% | | power. No actuations have taken place related to this event. The cause of | | this loss is being investigated. Procedural guidance is available to obtain | | the necessary data from the national weather service should this data be | | necessary." | | | | The NRC resident inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39502 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 01/11/2003| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 23:45[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/11/2003| +------------------------------------------------+EVENT TIME: 21:45[EST]| | NRC NOTIFIED BY: LARRY TUMBLESON |LAST UPDATE DATE: 01/12/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: |JOHN DAVIDSON IAT | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO FBI AND LOCAL LAW ENFORCEMENT | | | | At 2345 EST on 1/11/03, the licensee reported that they had contacted the | | Charlotte, NC FBI and the Charlotte-Mecklenburg, NC police department | | concerning a report they received at 2145 EST on 1/11/03 from the Mt. | | Gilead, NC Volunteer Fire Department concerning a plastic traffic cone that | | was set on fire on Highway 73 approximately one-eighth mile east of the main | | entrance road to the McGuire Station and approximately one-half mile from | | the owner-controlled area checkpoint on the entrance road. | | | | The licensee will be informing the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39503 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 01/12/2003| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 18:14[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/12/2003| +------------------------------------------------+EVENT TIME: 13:10[PST]| | NRC NOTIFIED BY: MR HARBOR |LAST UPDATE DATE: 01/12/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHUCK CAIN R4 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF MET TOWER DATA | | | | "Event: On January 7, 2003 the Primary Meteorological (Met) Tower was | | removed from service to repair | | the 76-meter wind direction function. Removing the primary tower from | | service results in all | | functions (i.e. wind speed, wind direction, and air temperature) being | | declared INOPERABLE. | | On January 12, 2003 at 1310, the 60-meter air temperature for the Back-up | | Meteorological Tower | | was declared INOPERABLE due to faulty readings. | | | | "Effects on Plant: This has resulted in a loss of the capability to | | determine differential temperature for emergency | | assessment (plume}. | | | | "Cause: The cause of the faulty Back-up Met Tower 60-meter temperature | | indication is under | | investigation. The Primary Met tower is INOPERABLE because it is disabled to | | correct the 76- | | meter wind direction function. | | | | "Actions Taken or Planned: 1) The portable meteorological monitoring system | | is being placed in-service per Diablo Canyon Power Plant (DCPP) Equipment | | Control Guideline (ECG) 40.l-B.1. This restores differential temperature | | monitoring capability. 2) DCPP maintenance personnel have been dispatched to | | repair either the primary or back-up tower. The plant will remain in a 7 day | | ECG until either towers air temperature monitoring function has been | | restored to OPERABLE status." | | | | The NRC Resident Inspector. has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39504 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 01/12/2003| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 18:40[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/12/2003| +------------------------------------------------+EVENT TIME: 15:53[EST]| | NRC NOTIFIED BY: DAN HARDIN |LAST UPDATE DATE: 01/12/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 94 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC SCRAM ON LOWERING REACTOR VESSEL WATER LEVEL DUE TO FEED PUMP | | TRIP | | | | "Unit 1 was operating at 94 percent power (presently max power) when 1B | | Reactor Feed Pump (RFP) low oil pressure annunciator was received coincident | | with 1B RFP trip at 1552. Reactor water level lowered and initiated an | | automatic SCRAM as the Reactor Operator was inserting a manual SCRAM at | | 1553. All systems initiated and isolated as required. A group 6 [containment | | atmospheric and sampling] and Group 2 [drywell floor equipment drain | | isolation valves] isolation was received on low Reactor water level and | | verified. The Emergency Diesel Generators started as expected due to a | | reverse power lockout of the main generator. After the SCRAM the 1A RFP | | tripped on high water level. Prior to restarting a RFP a second SCRAM signal | | was received on low level. The Reactor Core Isolation Cooling (RCIC) system | | was manually started to restore level while the reactor feed pump was being | | restarted. The preliminary investigation indicates that the running lube oil | | pump on the 1B RFP tripped. The standby lube oil pump started however, | | apparently, did not recover lube oil pressure in time to prevent a trip of | | 1B RFP." | | | | All control rods properly inserted into the reactor core. The NRC Resident | | Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39505 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 01/13/2003| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 02:48[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/12/2003| +------------------------------------------------+EVENT TIME: 23:04[EST]| | NRC NOTIFIED BY: RITA BRADDICK |LAST UPDATE DATE: 01/13/2003| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RICHARD CONTE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OPEN DUCTWORK ACCESS PANEL PREVENTED MAINTAINING CONTROL ROOM POSITIVE | | PRESSURE | | | | "On January 12, 2003 at 2304, control room pressure was observed to be | | negative. At the time the "A" Control Room Emergency Filtration (CREF) | | system was tagged out for scheduled maintenance. The event was initiated | | when technicians opened an access panel on the "A" CREF control room air | | supply duct within the control room boundary to repair a gasket. This | | resulted in both "A" and "B" trains of CREF unable to perform its design | | safety function: specifically, maintaining the control room at a 1/8 inch | | water gauge positive pressure relative to adjacent areas. Without assurance | | of CREF system providing positive pressure in the control room, mitigating | | the consequences of an accident could have been prevented. Upon discovering | | the cause, technicians were ordered to close the access panel. Control room | | pressure promptly returned to a normal, positive value. Total time at | | negative pressure was ten minutes. No unexpected response was experienced. | | In addition to the "A" CREF train, the "A" Hydrogen/Oxygen analyzer was | | inoperable at the time of the event." | | | | The licensee has notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021