Event Notification Report for January 6, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/03/2003 - 01/06/2003 ** EVENT NUMBERS ** 39481 39487 39488 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39481 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 12/31/2002| | UNIT: [] [2] [] STATE: AZ |NOTIFICATION TIME: 11:15[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 12/26/2002| +------------------------------------------------+EVENT TIME: 05:18[MST]| | NRC NOTIFIED BY: DAN MARKS |LAST UPDATE DATE: 01/03/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 99 Power Operation |99 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PALO VERDE 2 OFFSITE NOTIFICATION ON COOLING TOWER WATER SPILL | | | | "The following event description is based on information currently | | available. If through subsequent reviews of this event, additional | | information is identified that is pertinent to this event or alters the | | information being provided at this time, a follow-up notification will be | | made via the ENS or under the reporting requirements of 10CFR50.73. | | | | "On Tuesday, December 31, 2002, the Palo Verde Nuclear Generating Station | | Unit 2 will provide a voluntary written report to the Arizona Department of | | Environmental Quality (ADEQ) of an event related to the protection of the | | environment. Specifically, the report will detail an unintentional release | | of an estimated 72,000 gallons of cooling tower water to the unlined ditch | | that carries storm water from the gunite lined storm water collection system | | to Sedimentation Basin #1. The release began at approximately 05:18 Mountain | | Standard Time (MST) on December 26, 2002 and was stopped at approximately | | 05:50 MST on December 28, 2002 following discovery. No news release is | | anticipated." | | | | The NRC Resident Inspector was notified. | | | | ***UPDATE 01/03/03 1551 EST DAN MARKS TO JASON FLEMMING*** | | | | "It has been brought to Palo Verde's attention that this ENS event report | | 39481 has been posted on the NRC website with an error. The release stopped | | at approximately 05:50 MST on December 26, 2002. The webpage incorrectly | | states December 28, 2002." | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39487 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 01/03/2003| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 15:14[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 01/03/2003| +------------------------------------------------+EVENT TIME: 11:01[CST]| | NRC NOTIFIED BY: STEVE HENRY |LAST UPDATE DATE: 01/03/2003| | HQ OPS OFFICER: JASON FLEMMING +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO POWER RANGE NEUTRON FLUX - HIGH NEGATIVE RATE | | TRIP | | | | "On January 3, 2003, Wolf Creek Generating Station Unit 1 was operating at | | 100% reactor power when an automatic reactor trip occurred at 11:01 a.m. | | CST. Scheduled preventative maintenance had been completed on the control | | rod drive motor generator set, and the system was being placed back into | | service when an automatic reactor trip was received due to a Power Range | | Neutron Flux - High Negative Rate trip on all four power range channels. | | | | "An Auxiliary Feedwater Actuation Signal was received and initiated the | | Auxiliary Feedwater System as expected. Plant equipment performed as | | expected. | | | | "Investigation into the cause of the reactor trip is in progress. The plant | | is currently in MODE 3, Hot Standby. This event is being reported in | | accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A)." | | | | The Licensee has notified the NRC Resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39488 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 01/04/2003| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 07:47[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 01/04/2003| +------------------------------------------------+EVENT TIME: 01:13[CST]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 01/04/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOW PRESSURE COOLANT INJECTION DECLARED INOPERABLE | | | | "At 0113 hours CST on 1/4/2003, SR 3.5.1.1 [Surveillance Requirement] | | (monthly fill and vent surveillance) was initiated on U-2 B RHR loop. When | | the high point vents were opened, no flow was observed within the | | established venting criteria required by the surveillance. Based on this, | | neither LPCI [Low Pressure Coolant Injection] subsystem could be ensured | | filled to the injection valves. Both LPCI subsystems were declared | | inoperable and TS 3.5.1 [Technical Specification] Condition D [was] entered. | | At 0204 hours CST, when full flow was observed from the 2B RHR loop, TS | | 3.5.1 Condition D was exited. At 0210 hours CST, 2A RHR loop was | | subsequently vented and full flow was observed immediately. | | | | "This notification is being made in accordance with | | 10CFR50.72(b)(3)(v)[(D)]." | | | | Licensee has informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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