Event Notification Report for January 2, 2003
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
12/31/2002 - 01/02/2003
** EVENT NUMBERS **
39474 39478 39479 39480 39481 39482 39483 39484 39485
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|General Information or Other |Event Number: 39474 |
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| REP ORG: COLORADO DEPT OF HEALTH |NOTIFICATION DATE: 12/26/2002|
|LICENSEE: SCHLUMBERGER TECHNOLOGIES CORP. |NOTIFICATION TIME: 11:35[EST]|
| CITY: RIFLE REGION: 4 |EVENT DATE: 12/26/2002|
| COUNTY: STATE: CO |EVENT TIME: 08:30[MST]|
|LICENSE#: 039-01 AGREEMENT: Y |LAST UPDATE DATE: 12/26/2002|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |LINDA HOWELL R4 |
| |SUSAN FRANT (email) NMSS |
+------------------------------------------------+FRED BROWN (email) NMSS |
| NRC NOTIFIED BY: TIM G. BONZER | |
| HQ OPS OFFICER: ARLON COSTA | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| AGREEMENT STATE NOTIFICATION OF IRRETRIEVABLE WELL-LOGGING SOURCE |
| |
| Timothy Bonzer of the Colorado Radiation Services notified the NRC |
| Operations Center via fax on 12/26/02 at 1135 EST on an incident involving |
| an abandoned well-logging source assembly at a gas well near Rifle, Colorado |
| by Schlumberger Technologies Corp. The sources (Cs and AmBe) were lost at |
| approximately the 8,000 ft level and efforts to retrieve the sources were |
| unsuccessful. They had taken the necessary measures to deflect any future |
| attempt to drill in the same location and will place a stainless steel |
| warning placard at the surface. They intended to abandon the sources and are |
| still planning to use the well for the production of natural gas. |
| |
| The Colorado Emergency Management organization is cognizant of this |
| incident. |
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|Power Reactor |Event Number: 39478 |
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| FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 12/30/2002|
| UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 15:51[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/30/2002|
+------------------------------------------------+EVENT TIME: 14:15[CST]|
| NRC NOTIFIED BY: DAVE BUTLER |LAST UPDATE DATE: 12/31/2002|
| HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
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EVENT TEXT
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| LOSS OF OFFSITE EMERGENCY SIRENS DUE TO LIGHTNING STRIKES |
| |
| All emergency sirens (66 of 66) serving Hood and Somervell Counties, TX are |
| out of service due to lightning strikes on communications repeater |
| equipment. The licensee has notified the Hood and Somervell County Sheriff |
| Departments and will be notifying the NRC resident inspector. Repair crews |
| are responding and expect to make repairs within about 4 hours. |
| |
| ***UPDATE on 12/31/02 at 0113ET by Don Cerny taken by MacKinnon**** |
| |
| All sirens were returned to service December 31, 2002 at midnight. NRC |
| R4DO (Bill Johnson) notified. |
| |
| The NRC Resident Inspector will be contacted by the licensee of this update. |
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|General Information or Other |Event Number: 39479 |
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| REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 12/30/2002|
|LICENSEE: LOR GEOTECHNICAL GROUP |NOTIFICATION TIME: 13:47[EST]|
| CITY: RIVERSIDE REGION: 4 |EVENT DATE: 12/30/2002|
| COUNTY: STATE: CA |EVENT TIME: 10:47[PST]|
|LICENSE#: 5459-33 AGREEMENT: Y |LAST UPDATE DATE: 12/30/2002|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |WILLIAM JOHNSON R4 |
| |DONALD COOL NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: ROBERT GREGER | |
| HQ OPS OFFICER: ARLON COSTA | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| AGREEMENT STATE REPORT - STOLEN MOISTURE DENSITY GAUGE |
| |
| A Humbolt moisture density gauge , Model # HSI5001P, Serial # 838, was |
| stolen from the back of a truck sometime between 12/28/02 and 12/30/02 in |
| Redlands, CA. The gauge contained 10 millicuries of Cs-137 and 40 |
| millicuries Am-241:Be. On Saturday, December 28, 2002, an employee took the |
| gauge back to his residence after performing a job. The gauge was chained |
| and locked in the back of his truck. On Monday morning at approximately |
| 0645 PST the employee noticed that the gauge, chains and lock were missing |
| from the back of his truck. He reported the theft to the Radiation Safety |
| Officer (RSO). The RSO reported the theft to the State of California. The |
| theft was also reported to the local police and the licensee is posting a |
| notice with a reward in local newspapers. |
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|Power Reactor |Event Number: 39480 |
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| FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 12/31/2002|
| UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 01:34[EST]|
| RXTYPE: [1] GE-3 |EVENT DATE: 12/30/2002|
+------------------------------------------------+EVENT TIME: 20:10[CST]|
| NRC NOTIFIED BY: JAMES McKAY |LAST UPDATE DATE: 12/31/2002|
| HQ OPS OFFICER: RICH LAURA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 |
|10 CFR SECTION: | |
|AINB 50.72(b)(3)(v)(B) POT RHR INOP | |
|AINA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | |
|AINC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| MONTICELLO INITIATED TS REQUIRED PLANT SHUTDOWN DUE TO INOPERABILITY OF BOTH |
| EDGs |
| |
| "With #12 EDG inoperable due to a maintenance issue [on 12/29/02 at 2330 |
| CST] , it is required to test #11 EDG within 24 hours. Testing causes #11 |
| EDG to be inoperable, therefore both EDGs are inoperable requiring [the |
| initiation of] a plant shutdown per T.S. 3.9.B.3.a.2 and a non-emergency |
| notification per 10 CFR 50.72/8 hour. #11 EDG subequently tested operable |
| and the plant exited T.S. shutdown requirement at 2300 on 12/30/02." |
| |
| The licensee stated that the period of time both EDGs were inoperable was |
| from 2010 to 2300 on 12/30/02. The inoperablity of the #12 EDG was due to |
| an equipment problem with the DC fuel oil pump. After fixing the DC fuel |
| oil pump on the #12 EDG, the EDG was restarted and the "failure-to-start" |
| alarm lit and the "cranking" alarm lit and stayed in for 5 minutes. The |
| licensee is currently evaluating these problems. The #12 EDG remains in a 7 |
| day limiting LCO action statement. The #11 EDG started and tested |
| satisfactorily with no problems. The inoperability of the #11 EDG was due to |
| some of the set up conditions for testing when the EDG is considered to be |
| inoperable per procedure. |
| |
| The NRC Resident Inspector was notified. |
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|Power Reactor |Event Number: 39481 |
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| FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 12/31/2002|
| UNIT: [] [2] [] STATE: AZ |NOTIFICATION TIME: 11:15[EST]|
| RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 12/26/2002|
+------------------------------------------------+EVENT TIME: 05:18[MST]|
| NRC NOTIFIED BY: DAN MARKS |LAST UPDATE DATE: 12/31/2002|
| HQ OPS OFFICER: RICH LAURA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 99 Power Operation |99 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| PALO VERDE 2 OFFSITE NOTIFICATION ON COOLING TOWER WATER SPILL |
| |
| "The following event description is based on information currently |
| available. If through subsequent reviews of this event, additional |
| information is identified that is pertinent to this event or alters the |
| information being provided at this time, a follow-up notification will be |
| made via the ENS or under the reporting requirements of 10CFR50.73. |
| |
| "On Tuesday, December 31, 2002, the Palo Verde Nuclear Generating Station |
| Unit 2 will provide a voluntary written report to the Arizona Department of |
| Environmental Quality (ADEQ) of an event related to the protection of the |
| environment. Specifically, the report will detail an unintentional release |
| of an estimated 72,000 gallons of cooling tower water to the unlined ditch |
| that carries storm water from the gunite lined storm water collection system |
| to Sedimentation Basin #1. The release began at approximately 05:18 Mountain |
| Standard Time (MST) on December 26, 2002 and was stopped at approximately |
| 05:50 MST on December 28, 2002 following discovery. No news release is |
| anticipated." |
| |
| The NRC Resident Inspector was notified. |
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|Power Reactor |Event Number: 39482 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 12/31/2002|
| UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 21:13[EST]|
| RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 12/31/2002|
+------------------------------------------------+EVENT TIME: 20:13[CST]|
| NRC NOTIFIED BY: DEAN RAASCH |LAST UPDATE DATE: 12/31/2002|
| HQ OPS OFFICER: ARLON COSTA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| LOSS OF COMMUNICATION VIA ENS |
| |
| "At 1535 CST [12/31/02] it was discovered that the ENS Phones in both the |
| Control Room and TSC were not functioning. Minimum required backup |
| communication systems were verified operable. Repairs were initiated and |
| the phone systems were restored to an operable status at 2000 CST. |
| |
| The Licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
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|Power Reactor |Event Number: 39483 |
+------------------------------------------------------------------------------+
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| FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 12/31/2002|
| UNIT: [1] [2] [] STATE: AR |NOTIFICATION TIME: 22:37[EST]|
| RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 12/31/2002|
+------------------------------------------------+EVENT TIME: 19:30[CST]|
| NRC NOTIFIED BY: DAVID THOMPSON |LAST UPDATE DATE: 12/31/2002|
| HQ OPS OFFICER: ARLON COSTA +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| OFFSITE NOTIFICATION DUE TO INADVERTENT ACTUATION OF SIRENS |
| |
| "At 19:30 [CST] on December 31, 2002, ANO Security received an offsite call |
| from the Pope County Emergency Services Office regarding actuation of |
| emergency sirens in the Russellville area. The sirens silenced automatically |
| approximately 3 minutes later after they timed out. Information provided by |
| Pope County Emergency Services indicated the cause of the actuation of the |
| sirens was attributed to a damaged transformer in the vicinity of the siren |
| stations as reported by one caller. At 20:02 Channel 11 News in Little Rock |
| called security inquiring about this event." |
| |
| The Licensee reported that the sirens are currently operable. The NRC |
| Resident Inspector was notified and State Agencies will be notified of this |
| incident. |
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|Power Reactor |Event Number: 39484 |
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| FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 01/01/2003|
| UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 09:05[EST]|
| RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 01/01/2003|
+------------------------------------------------+EVENT TIME: 05:57[CST]|
| NRC NOTIFIED BY: MIKE MILLEN |LAST UPDATE DATE: 01/01/2003|
| HQ OPS OFFICER: ERIC THOMAS +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS OF ENS PHONES |
| |
| "At 0557 CST it was discovered that the ENS Phones in both the Control Room |
| and TSC were not functioning. Minimum required backup communications |
| systems were verified operable. Repairs have been initiated." |
| |
| The licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
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|Power Reactor |Event Number: 39485 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 01/01/2003|
| UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 10:09[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/01/2003|
+------------------------------------------------+EVENT TIME: 06:26[EST]|
| NRC NOTIFIED BY: MICHAEL HOWARD |LAST UPDATE DATE: 01/01/2003|
| HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |THOMAS DECKER R2 |
|10 CFR SECTION: | |
|AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 A N 0 Cold Shutdown |0 Cold Shutdown |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| REACTOR TRIP AND AUXILIARY FEEDWATER ACTUATION START SIGNALS RECEIVED DURING |
| DRAINING OF THE LOOP # 2 STEAM GENERATOR. |
| |
| "At 0626 EDT on 01/01/03, Sequoyah Unit 2 received reactor trip and |
| Auxiliary Feedwater (AFW) start signals while draining the loop 2 Steam |
| Generator (S/G). The low-low level trip inputs to the RPS (reactor |
| protection system) were blocked in accordance with the procedure. However, |
| the EAM/TTD [environmental adverse monitor/trip time delay] low-low level |
| trip inputs were not blocked prior to commencing the drain down [the |
| procedural step had been N/A'd]. The setpoint for the trip is 15% on 2/3 |
| Level Transmitters with an increasing time delay based on core delta T [with |
| reactor power less than 50%]. |
| |
| "Unit 2 was in Mode 5 [cold shutdown] prior the actuation with all rods |
| inserted. The reactor coolant system was at 115 [degrees] F and 5 psig. |
| The AFW pumps were in pull-to-lock and did not start as a result of the |
| signal. No other equipment started or repositioned as a result of the |
| low-low level signal. |
| |
| "The first out annunciation cleared at 0939 EDT after blocking the EAM/TTD |
| low-low level inputs." |
| |
| |
| The NRC Resident Inspector will be notified of this event by the licensee. |
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