Event Notification Report for December 16, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/13/2002 - 12/16/2002 ** EVENT NUMBERS ** 39303 39381 39443 39444 39445 39446 39447 39448 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39303 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 10/19/2002| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 05:27[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 10/18/2002| +------------------------------------------------+EVENT TIME: 21:30[CDT]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 12/13/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |THOMAS KOZAK R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RCIC HIGH STEAM FLOW ISOLATION INSTRUMENTATION INOPERABLE DUE TO BEING OUT | | OF TOLERANCE | | | | "At 2130 hours CDT on 10/18/2002, the U1 RCIC High Steam Flow Isolation | | Instrumentation was determined to have been inoperable. Both U1 RCIC High | | Steam Flow switches were found to be outside their Technical Specification | | Allowable Value during a calibration surveillance. Both U1 RCIC High Steam | | Flow switches were subsequently recalibrated back to within their Technical | | Specification Allowable Value. | | | | "This notification is being made in accordance with 10CFR50.72(b)(3)." | | | | The NRC Resident Inspector has been notified. | | | | * * * UPDATE 1145EST ON 12/13/02 FROM RON RUSTICK TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | "The purpose of this notification is to retract the ENS report made on | | 10/19/2002 at 05:27 EDT (Event #39303). The initial report concerned the | | Reactor Core Isolation Cooling (RCIC) system high steam flow isolation | | function. On 10/18/2002, both required high steam flow isolation instruments | | were found to be outside of their Technical Specifications Allowable Value | | (AV); therefore, a notification was made under 10CFR50.72(b)(3)(V)(D). | | However, a subsequent review of this event has determined that only one of | | the two required channels actually exceeded the AV and thus one channel was | | OPERABLE and capable of initiating the isolation function (i.e., there was | | no loss of safety function). For this reason, Quad Cities Station has | | concluded that the RCIC high steam flow isolation function was preserved." | | | | The licensee informed the NRC resident inspector. Notified R3DO(Hiland). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39381 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 11/17/2002| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 15:38[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/17/2002| +------------------------------------------------+EVENT TIME: 13:06[EST]| | NRC NOTIFIED BY: RICHARD STONE |LAST UPDATE DATE: 12/13/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LEONARD WERT R2 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI DECLARED INOPERABLE DURING QUARTERLY SURVEILLANCE TESTING | | | | "Unit 1 High Pressure Coolant Injection (HPCI) flow controller indicates 512 | | GPM with system in standby. Found when aligning system for surveillance. | | Cannot assure system will achieve rated flow automatically. HPCI is a | | single train system." | | | | HPCI was declared inoperable placing Unit 1 in a 14-day LCO A/S 3.5.1. The | | licensee intends to troubleshoot the problem including a fill/vent of the | | applicable flow transmitter. The licensee will inform the NRC resident | | inspector. | | | | * * * RETRACTION ON 12/13/02 AT 0958 EST FROM HARRY RUSSELL TO GERRY WAIG * | | * * | | | | The investigation of the problem noted in Report 39381 reported 11/17/2002 | | was determined to be setpoint drift of transmitter 1E41N008 and not an | | inoperable controller. Because this transmitter receives an input of | | differential pressure and the milliamp output is converted to flow using a | | square root function the amount of error in the flow rate measurement is not | | linear throughout the span of the transmitter. The plant has confirmed that | | the "as found" setpoint drift of this single flow measuring device would | | still have allowed the affected flow controller to perform its safety | | function and control flow negligibly lower than the design flowrate (4220 | | versus 4250 gpm), thereby continuing to allow HPCI to fulfill its safety | | function. It did not involve a failure of the flow measuring device and | | would therefore not be indicative of a generic failure problem with similar | | flow measuring devices on other systems. The HPCI system was operable in its | | "as found" condition. Based on the guidance in NUREG 1022, Revision 2, this | | setpoint drift of 1E41N008 is not reportable. | | | | Notified R2DO (Mike Ernstes). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39443 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 12/13/2002| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 10:25[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 12/13/2002| +------------------------------------------------+EVENT TIME: 08:30[EST]| | NRC NOTIFIED BY: LOUIS NOWELL |LAST UPDATE DATE: 12/13/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MIKE ERNSTES R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF MORE THAN 25% OF THE STATIONS ALERT SIRENS | | | | "Loss of more than 25% of the stations total alert sirens have been disabled | | for more than one hour (0830-0930) due to a loss of power. This was due to | | severe weather." | | | | The loss of alert sirens affects offsite response/notification. Efforts to | | restore power to the sirens are in progress at this time. | | | | The licensee has notified the NRC Resident Inspector of this event. | | | | **** UPDATE on December 13, 2002 at 1500 Hours by Louis Nowell taken by | | MacKinnon **** | | | | Less than 25% of the stations total alert sirens are disabled due to a power | | loss. NRC R2DO (Mike Ernstes) notified. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39444 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 12/13/2002| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 17:04[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 12/13/2002| +------------------------------------------------+EVENT TIME: 14:50[EST]| | NRC NOTIFIED BY: DON ROLAND |LAST UPDATE DATE: 12/13/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID LEW R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO DIESEL FUEL SPILL | | | | "At 1450 EST on 12/13/2002, Susquehanna LLC Main Control Room received a | | request for additional information from the Pennsylvania Emergency | | Management Agency (PEMA). PEMA received rumors that a HAZMAT team had been | | dispatched to Susquehanna in response to a spill associated with a potential | | sabotage event. | | | | "At 1158 EST a delivery truck at the owner controlled entrance gate was | | identified to have a saddle tank leak which resulted in a spill of | | approximately 10 gallons. The diesel fuel was contained by site personnel, | | and is in the process of being cleaned by site personnel. None of the oil | | reached a waterway, and therefore does not meet the requirements for a | | reportable spill. The delivery company contacted their contracted spill | | response team, and they responded to the site. They were subsequently | | released without performing any of the cleanup activities. The minor spill | | was not due to sabotage. This information has been provided to PEMA. | | | | "This report is being issued due to the involvement of other government | | agencies, and reportable under 10CFR50.72(b)(2)(xi)." | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39445 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 12/14/2002| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 09:11[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 12/14/2002| +------------------------------------------------+EVENT TIME: 04:20[CST]| | NRC NOTIFIED BY: DAVID LANTZ |LAST UPDATE DATE: 12/14/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KRISS KENNEDY R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON OTDT DURING DOWNPOWER | | | | "At 0420 on 12/14/02, a valid actuation signal was generated that caused an | | Overtemperature Delta T (OTDT) Reactor Trip. The cause of the OTDT trip was | | a downpower at 1% per minute due to an oil leak on the 'C' Condensate Pump. | | A valid actuation signal was generated for the Auxiliary Feedwater Actuation | | System (AFAS), the Feedwater Isolation System (FWIS) and the Steam Generator | | Blowdown System Isolation System (SGBSIS) due to Steam Generator Low Levels. | | After the Turbine Driven Auxiliary Feedwater Actuation Signal (AFAS) was | | reset, a second AFAS was received and the Turbine Driven Auxiliary Pump | | failed to start. All other systems functioned as expected. | | | | "An Event Review Team (ERT) has been assembled to determine the cause of the | | event. Additional corrective action to be taken will be based upon | | recommendations provided by the ERT. | | | | "The Senior NRC Resident Inspector has been notified of the event." | | | | Both motor driven Auxiliary Feedwater Pumps are in service currently | | maintaining SG levels. The Main Condenser is available for removal of | | decay heat via the Main Steam Dump Bypass. All rods fully inserted. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39446 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/15/2002| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 06:28[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/15/2002| +------------------------------------------------+EVENT TIME: 02:30[EST]| | NRC NOTIFIED BY: ALLEN RABENOLD |LAST UPDATE DATE: 12/15/2002| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |PATRICK HILAND R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY - LICENSED OPERATOR UNFIT FOR SCHEDULED WORK | | | | Licensed employee was determined to be under the influence of alcohol during | | a 'for cause' test, did not assume any shift duties and his plant access has | | been terminated. Contact HOO for additional details. | | | | Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Transportation |Event Number: 39447 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SYNCOR INTERNATIONAL CORP. |NOTIFICATION DATE: 12/15/2002| |LICENSEE: SYNCOR INTERNATIONAL CORP. |NOTIFICATION TIME: 08:40[EST]| | CITY: GLASTONBURY REGION: 1 |EVENT DATE: 12/15/2002| | COUNTY: STATE: CT |EVENT TIME: 05:00[EST]| |LICENSE#: 04-26507-01MD AGREEMENT: N |LAST UPDATE DATE: 12/15/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID LEW R1 | | |TOM ESSIG NMSS | +------------------------------------------------+CREWS DOT | | NRC NOTIFIED BY: MATT SVEJK | | | HQ OPS OFFICER: ARLON COSTA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Tc-99m CANISTERS UNDAMAGED DURING TRANSPORTATION ACCIDENT | | | | The NRC Operations Center was notified by the Connecticut Department of | | Environmental Protection (CT DEP) that an vehicle accident involving a | | Syncor delivery to local hospitals and pharmacies had occurred. A follow-up | | discussion with the Radiation Safety Officer (RSO) for Syncor International | | Corporation located at 628 Hebron Avenue, Bldg.4, Glastonbury, CT 06033, | | provided detailed information related to the incident. The company vehicle | | (pickup truck) accidentally rolled over after encountering a patch of black | | ice. Eight canisters (ammo box style) were ejected from the vehicle bed | | during the accident at Route 6 and State Road 384 in Coventry, Connecticut. | | The company driver was in the process of picking up and delivering the | | canisters which house Tc-99m syringes (unit dose) that are enclosed in lead | | pigs. Both the local police and fire departments and the CT DEP responded | | to the accident which happened at approximately 0500 EST on 12/15/02. The | | driver was taken to a local hospital for routine x-rays and treatment. The | | initial assessment of the incident was that the canisters were not breached. | | No contamination was detected by the first responders. Syncor will follow | | up with measurements of the swipes using Multi-Channel Analyzer | | methodology. | | | | | | * * * UPDATE AT 10:18 ON 12/15/02 FROM MATT SVEJK TO ARLON COSTA * * * | | | | The test results of the wiped canisters using a Multi-Channel Analyzer did | | not indicate any counts above background. The total Tc-99m activity of the | | five active canisters (the other three were return canisters) was | | approximately 1,137 millicuries (assay estimate as of 0500 EST on 12/15/02). | | Notified R1DO(Lew) and NMSS(Essig). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39448 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 12/15/2002| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 21:18[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/15/2002| +------------------------------------------------+EVENT TIME: 18:08[CST]| | NRC NOTIFIED BY: GREG JANEK |LAST UPDATE DATE: 12/15/2002| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KRISS KENNEDY R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO HIGH MAIN TURBINE VIBRATIONS | | | | "At 18:08 on 12/15/02, the reactor was manually tripped due to high | | vibrations on the Main Turbine. Investigation into the cause of the Main | | Turbine high vibrations is in progress. | | | | "This is being reported under 10CFR50.72(b)(2)(iv)(b). | | | | "During the reactor trip, all control rods fully inserted. Auxiliary | | Feedwater System automatically actuated as expected on low-low steam | | generator water level, Main Condenser Vacuum was secured to reduce Main | | Turbine speed quicker, Main Steam isolation was manually actuated, and the | | Steam Generator Power Operated Relief Valves automatically opened to | | maintain primary system temperature. | | | | "Primary System temperature and pressure is being maintained at 573 | | degrees/2235 psig. | | | | | | "Technical Specification 3.7.1.3 was entered at 18:11 due to Auxiliary | | Feedwater Storage Tank level less than the minimum required level of 485,000 | | gallons. This requires the level to be restored to above required limit | | within 4 hours or be in Hot Standby within the next 6 hours. Currently | | makeup to the storage tank is in progress." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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