Event Notification Report for November 18, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/15/2002 - 11/18/2002 ** EVENT NUMBERS ** 39205 39366 39375 39376 39377 39378 39379 39380 39381 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39205 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 09/20/2002| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 16:30[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/20/2002| +------------------------------------------------+EVENT TIME: 10:02[EDT]| | NRC NOTIFIED BY: BOB LANCE |LAST UPDATE DATE: 11/15/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI INOPERABLE DUE TO PRESSURE AND SPEED FLUCTUATIONS | | | | "On 9/20/02 at 10:02 AM EDT, the Unit 1 HPCI system was declared inoperable | | due to observation of speed and pressure fluctuations while operating in the | | manual mode. HPCI was being run for the quarterly surveillance test. Site | | engineering is currently troubleshooting. This report is being made pursuant | | to 10CFR50.72(b)(3)(v)(D) for failure of a single train accident mitigation | | system." | | | | The NRC resident inspector was notified. | | | | *** UPDATE ON 11/15/02 AT 1032 EST BY PETER GARDNER TO HOWIE CROUCH *** | | | | "Troubleshooting identified that the output of the Ramp Generator and Signal | | Converter (RGSC) was fluctuating. The HPCI RGSC and Electronic Governor | | [-Motor] (EG-M) were replaced and the post maintenance testing (PMT) was | | successfully completed. | | | | The HPCI safety function requires the system to provide adequate coolant | | makeup to the reactor pressure vessel (RPV) in the automatic mode for the | | spectrum of analyzed events. The small break LOCA [Loss of Coolant | | Accident] event (one-inch diameter pipe break) requires the greatest HPCI | | flowrate. HPCI must provide adequate RPV coolant makeup to maintain core | | coverage and prevent an actuation of ADS [Automatic Depressurization System] | | during this event. | | | | HPCI successfully completed the portion of the surveillance test that | | required operation in the automatic mode just prior to the observed speed | | fluctuation. Two successful HPCI runs were performed following the | | replacement of the RGSC and EG-M in June 2002. The speed fluctuation | | occurred intermittently in the manual mode of operation following a | | reduction in speed to 3150 rpm. Failure analysis of the RGSC and EG-M did | | not reveal any condition that would have prevented HPCI from providing the | | required coolant makeup." | | | | Therefore, the licensee is retracting this event. | | | | Licensee notified the NRC resident of the retraction. | | | | NRC region 1 duty officer (Harold Gray) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39366 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: KENTUCKY DEPT OF RADIATION CONTROL |NOTIFICATION DATE: 11/12/2002| |LICENSEE: HUNTINGTON TESTING AND TECHNOLOGY INC|NOTIFICATION TIME: 16:30[EST]| | CITY: GHENT REGION: 2 |EVENT DATE: 10/18/2002| | COUNTY: STATE: KY |EVENT TIME: 07:30[CST]| |LICENSE#: 201-551-05 AGREEMENT: Y |LAST UPDATE DATE: 11/12/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LEONARD WERT R2 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BOB JOHNSON | | | HQ OPS OFFICER: RICH LAURA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | KY AGREEMENT STATE REPORT INVOLVING AN OVER EXPOSURE OF A RADIOGRAPHER | | | | "This letter is notification of an overexposure incident that occurred on | | October 8, 2002 in Ghent, Kentucky. The licensee involved was Huntington | | Testing & Technology Inc.. Kentucky Radioactive Material License Number | | 201-551-05. The incident occurred while performing radiography at Kentucky | | Utilities. The radiography source was 103 Ci [Curies] of Ir-192 [Iridium], | | housed in a 660 B Camera, S/N B2954. The licensee's interpretation of the | | reporting criteria resulted in late notification thirty (30) days after the | | incident. That information was not only delayed, but also incomplete | | requiring further development before the State of Kentucky could forward | | this report. | | | | "At approximately 7:00 a.m., on October 18, 2002, when reeling in the | | radiography source after an exposure, it was not fully retracted, nor | | recognized for approximately three (3) minutes by the radiographer who had | | entered the area. Upon realization that the source was not fully retracted, | | the radiographer immediately left the area, extended the source and then | | retracted it to the housed position. The RSO [Radiation Safety Officer] was | | contacted and the radiographer removed from any radiological work. | | | | "The radiographer's dosimetry was immediately sent to Landauer for | | processing. The result of his exposure was 4.86 Rem whole body, in addition | | to his year-to-date exposure of 1.4 Rem, for total yearly whole body | | exposure of 6.26 Rem. These numbers appear to be close estimates, ending | | further evaluation of the radiographer's position in relation to the exposed | | source. Initial reports indicate a survey instrument failure, and failure of | | the radiographer to monitor the instrumentation and position indicator to | | ensure retraction of the radiography source. | | | | "Further evaluation of the cause of this incident and final dose estimates | | will be forwarded ending further investigation." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39375 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 11/15/2002| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 11:49[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 11/15/2002| +------------------------------------------------+EVENT TIME: 09:57[EST]| | NRC NOTIFIED BY: RUSS LONG |LAST UPDATE DATE: 11/15/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |HAROLD GRAY R1 | |10 CFR SECTION: |TERRY REIS NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 3 EXPERIENCED AN AUTOMATIC REACTOR TRIP DUE TO A GENERATOR LOCKOUT | | | | "At 0957 EST, 345 Kv Breaker 3 failed open resulting in breakers 1, 5 and 6 | | opening. This electrically isolated Unit 3 resulting in the Main Generator | | primary and backup lockout relays (86P and 86 Bu) tripping. This resulted | | in an immediate reactor trip. All equipment operated as expected with the | | following exceptions: | | | | 1. 32 Source Range failed to come on scale as required | | | | 2. 34 Circulating Water Pump transferred to standby drive when normal drive | | tripped | | | | 3. 36 Circulating Water Pump tripped | | | | "The plant is stable in mode 3. Post trip review is in progress and will be | | completed prior to restart. The Public Service Commission has been | | notified." | | | | There was no maintenance or other activities in progress in the switchyard | | at the time the 345 Kv Breaker 3 catastrophically failed. Unit 3 is | | currently removing decay heat via the steam dump bypass to the main | | condenser. Both motor driven auxiliary feedwater pumps autostarted and are | | in-service. The steam generator atmospheric dumps may have lifted during | | the transient. There is no known primary-secondary tube leakage. The | | licensee notified the NRC resident inspector and plans on issuing a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39376 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 11/16/2002| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 00:17[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/15/2002| +------------------------------------------------+EVENT TIME: 20:20[CST]| | NRC NOTIFIED BY: BRIAN JOHNSON |LAST UPDATE DATE: 11/16/2002| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRUCE BURGESS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 12 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO HIGH FEEDWATER HEATER LEVEL | | | | "While reducing power for a planned refueling outage, at 2020, U1 reactor | | was manually tripped at 12% power due to Hi Hi Level in 13 'A' Feedwater | | heater. An existing problem with an extraction bellows in 13 'A' Feedwater | | heater had been previously identified and contingency plans were in place | | for monitoring the level during the load decrease. Levels were being | | monitored locally by Engineering and Operations during the load decrease in | | anticipation of level control problems. Control Room Operators made the | | decision as planned, to manually trip the reactor per annunciator response | | procedures, when it was determined that level in 13 'A' Feedwater heater | | could not be reduced. During performance of reactor trip recovery | | procedures, 11 Turbine Driven Auxiliary Feedwater Pump auto started when the | | running Main Feedwater Pump was secured. 11 Turbine Driven Aux Feedwater | | Pump was secured and Steam Generator levels are being maintained with 12 | | Motor Driven Aux Feedwater Pump." | | | | Additionally, the Licensee stated that all control rods properly inserted | | into the core and that all safety systems responded as required. | | | | The Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 39377 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/15/2002| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:44[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/15/2002| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 03:15[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/16/2002| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRUCE BURGESS R3 | | DOCKET: 0707001 |ERIC LEEDS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: E.G. WALKER | | | HQ OPS OFFICER: ARLON COSTA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 CRITICALITY CONTROL ISSUE AT PADUCAH | | | | "At 0315 on 11-15-02, the Plant Shift Superintendent (PSS) was notified that | | the pressure chart recorder for the C-333 'C' surge drum bank had failed, | | violating an SRI in NCSE.016. As a result of this failure, the shiftly | | pressure checks performed prior to this discovery were performed using a | | failed AQ-NCS pressure instrument and therefore were not valid. The purpose | | of this pressure check is to identify if wet air inleakage has begun on the | | surge drum bank. Following identification and remediation of failure, | | pressure checks were performed and it was determined that no wet air | | inleakage had occurred and double contingency was restored. | | | | "The NRC Resident Inspector has been notified of this event. | | | | "SAFETY SIGNIFICANCE: Although pressure readings were taken using a failed | | AQ-NCS pressure instrument, there are several important mitigating factors. | | First the integrity of the drum bank has been maintained. Second, the drum | | contained non-fissile material. Third, the UF6 has maintained in the gas | | phase. Because the drum contained non-fissile material, the NCS controls | | were not necessary to prevent a criticality from occurring. | | | | "POTENTIAL CRITICALITY PATHWAYS: These drums are used to store gases. | | Therefore, in order for a criticality to be possible, the drum would have to | | contain fissile UF6. Wet air would have to react with any UF6 in the drum. | | Wet air inleakage would have to occur over a long period of time in order to | | create a large mass of UO2F2 and then sufficiently moderate the material. | | | | "CONTROLLED PARAMETERS: Double contingency is maintained by implementation | | of two controls on moderation. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL: Drum bank contains | | gaseous UF6 enriched to [ ]. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: The first leg of double contingency is | | based on maintaining the integrity of the surge drum against wet air | | inleakage. This integrity is insured by an SRI for the unlikely breach of | | the surge drum system. Structural integrity of the drum is intact, therefore | | this SRI was maintained. | | | | "The second leg of double contingency is based performance of shiftly checks | | using an AQ-NCS instrument as an indication of wet air inleakage. The | | required checks were performed using a failed instrument. Since a failed | | instrument was used, the shiftly checks were invalid resulting in a loss of | | this control. Since there are two controls on one parameter, double | | contingency was not maintained. | | | | "Even though moderation control was maintained, double contingency is based | | on two controls on moderation. Therefore double contingency was not | | maintained. The drum contained a non-fissile material. It should be noted | | that a second parameter, assay (not controlled in the NCSA), was maintained | | since the drum bank contained non-fissile material. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS IMPLEMENTATION: Approximately | | one hour after discovery, AQ-NCS Instrumentation was connected to surge drum | | manifold and pressure was verified to less than NCS limit. Readings are | | being obtained from this instrumentation pending calibration of recorder. | | | | "DESCRIPTION OF OCCURRENCE: The pressure chart recorder for the C-333 'C' | | surge drum bank failed, violating an SRI in NCSE.016. As a result of this | | failure the shiftly pressure checks were performed using a failed AQ-NCS | | pressure instrument and therefore were not valid. The purpose of the | | pressure check is to identify if wet air inleakage has begun on the surge | | drum bank. | | | | "It is important to note that an AQ-NCS pressure instrument was subsequently | | connected to the system and pressure readings have been taken. The pressure | | readings indicate there has been no wet air inleakage. Double contingency | | has been restored since the ability to read pressure in the surge drum bank | | using a properly operating AQ-NCS pressure instrument has been restored | | | | "NUCLEAR CRITICALITY SAFETY CONTROLS INVOLVED AND THEIR IMPACT ON DOUBLE | | CONTINGENCY: Double contingency is maintained by implementing two controls | | on moderation. | | | | "The first leg of double contingency is based on maintaining the integrity | | of the surge drum system against wet air inleakage. This integrity is | | assured by an SRI for the unlikely breach of the surge drum system. | | Structural integrity of the drum is intact, therefore this SRI is | | maintained. | | | | "The second leg of double contingency is based on the performance of shiftly | | pressure checks using an AQ-NCS instrument as an indication of wet air | | inleakage. The required checks were performed using a failed instrument. | | Since a failed instrument was used, the shiftly checks were invalid | | resulting in a loss of this control. Since there are two controls on one | | parameter, double contingency was not maintained. | | | | "Even though moderation control was maintained; double contingency is based | | on two controls on moderation. Therefore double contingency was not | | maintained. The drum contained non-fissile material. It should be noted that | | a second parameter (not controlled in the NCSA) was maintained since the | | drum contained non-fissile material. | | | | "Potential Critical Pathways: These drums are used to store gases. | | Therefore, in order for a criticality to be possible, the drum would have to | | contain fissile UF6. Wet air would have to react with any UF6 in the drum. | | The leak would have to occur over a long period of time in order to create a | | large mass of UO2F2 and then sufficiently moderate the material. | | | | "Safety Significance: Although pressure readings were taken using a failed | | AQ-NCS pressure instrument, there are several important mitigating factors. | | First the integrity of the drum bank has been maintained. Second, the drum | | contained non-fissile material. Third, the uranium has been maintained in | | the gas phase. Because the drum contained non-fissile material, the NCS | | controls were not necessary to prevent a criticality from occurring." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39378 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 11/16/2002| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 10:31[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 11/16/2002| +------------------------------------------------+EVENT TIME: 08:40[CST]| | NRC NOTIFIED BY: E. HINSON |LAST UPDATE DATE: 11/16/2002| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHUCK CAIN R4 | |10 CFR SECTION: | | |DDDD 73.71(b)(1) SAFEGUARDS REPORTS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT INVOLVING A LOST ACCESS BADGE | | | | Immediate compensatory measures taken upon discovery. Licensee notified the | | NRC resident inspector. Contact the Headquarters Operations Officer for | | details. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39379 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 11/16/2002| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 13:18[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/16/2002| +------------------------------------------------+EVENT TIME: 09:20[EST]| | NRC NOTIFIED BY: RICHARD HACKMAN |LAST UPDATE DATE: 11/16/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRUCE BURGESS R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO SODIUM HYPOCHLORITE DISCHARGE TO LAKE MICHIGAN | | | | "Notification was made on 11/16/02 at 1150 to the National Response Center | | and at 1205 to the Michigan Dept. of Environmental Quality of a Sodium | | Hypochlorite discharge to Lake Michigan that exceeded the permitted | | concentration. On 11/16/02 at 0920, a chemist discovered and isolated a | | leak from the Hypochlorite facility. Circulating Water discharge Total | | Residual Chlorine (TRC) was measured at that time to be 0.3ppm. The | | concentration dropped below the permit limit of 0.038ppm at 0930. A | | recorded rise in TRC indicated that the leakage started at 0015. The Unit 1 | | TRC High Alarm did not function. The recorded TRC concentration ranged | | between 0.26 and 0.4ppm during the 9 hour period. Hypochlorite tank level | | change indicates that approximately 1080 gallons of 12% sodium hypochlorite | | solution was discharged from the leak to the forebay and out of the | | Circulating Water discharge to Lake Michigan. No environmental impact is | | expected from the discharge based on the chlorine concentration and release | | duration." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39380 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 11/16/2002| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 22:49[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/16/2002| +------------------------------------------------+EVENT TIME: 20:42[CST]| | NRC NOTIFIED BY: JOHN PIERCE |LAST UPDATE DATE: 11/16/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHUCK CAIN R4 | |10 CFR SECTION: |ELLIS MERSCHOFF R4 | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|ELMO COLLINS R4 | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED A MANUAL REACTOR TRIP DUE TO A LOSS OF OPEN LOOP COOLING | | WATER | | | | "The South Texas Project makes the following 4 hour non-emergency report of | | a manual Reactor Protection System actuation per 10CFR50.72.b.2.ii. | | | | "At 20:42 on 11/16/02 Unit 1 reactor was manually tripped due to a loss of | | open loop cooling water. Reports indicated flooding in the circulating | | water intake structure due to a problem with circulating water pump #11, | | which caused the loss of open loop cooling." | | | | Operators received a loss of open loop cooling which supplies auxiliary | | cooling to the main generator. Per procedure, Unit 1 was manually tripped. | | Upon investigation, a 4-6 inch crack in circulating water pump #11 housing | | was discovered. A preliminary review indicates that water may have | | electrically shorted the three operating open loop cooling pumps which are | | also located in the intake structure. | | | | Unit 1 is currently stable in mode 3 with all auxiliary feedwater pumps in | | service. Vacuum in the main condenser is presently 27 inches with both | | circulating water pumps 13 and 14 operating. All rods fully inserted. | | Normal offsite power is available and no electrical buses were lost as a | | result of the flooding although electrical maintenance is investigating | | several electrical ground alarms. The licensee reviewed their Emergency | | Plan and determined that the criteria for declaration of an NOUE was not | | satisfied. The licensee notified the NRC resident inspector and does not | | plan on a press release at this time. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39381 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 11/17/2002| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 15:38[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/17/2002| +------------------------------------------------+EVENT TIME: 13:06[EST]| | NRC NOTIFIED BY: RICHARD STONE |LAST UPDATE DATE: 11/17/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LEONARD WERT R2 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI DECLARED INOPERABLE DURING QUARTERLY SURVEILLANCE TESTING | | | | "Unit 1 High Pressure Coolant Injection (HPCI) flow controller indicates 512 | | GPM with system in standby. Found when aligning system for surveillance. | | Cannot assure system will achieve rated flow automatically. HPCI is a | | single train system." | | | | HPCI was declared inoperable placing Unit 1 in a 14-day LCO A/S 3.5.1. The | | licensee intends to troubleshoot the problem including a fill/vent of the | | applicable flow transmitter. The licensee will inform the NRC resident | | inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021