Event Notification Report for November 14, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/13/2002 - 11/14/2002 ** EVENT NUMBERS ** 39300 39352 39356 39367 39368 39369 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39300 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 10/17/2002| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 18:55[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 10/17/2002| +------------------------------------------------+EVENT TIME: 14:30[CDT]| | NRC NOTIFIED BY: BRIAN HUPKE |LAST UPDATE DATE: 11/13/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |THOMAS KOZAK R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 94 Power Operation |94 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI INOPERABLE DUE TO LOW INTERNAL BATTERY RESISTANCE | | | | The licensee reported that during a 250 Vdc battery surveillance the | | internal resistance of cell #18 was greater than the technical specification | | (TS) limit. As a result, the licensee declared battery bank 1D4 inoperable | | which also rendered inoperable the HPCI system and any containment isolation | | valves powered from the battery bank. This included 5 total CIVs | | [Containment isolation valves] from the following systems: HPCI, RWCU and | | MSL drain and Torus drain valves. Corrective maintenance was performed on | | the battery cell and the internal resistance passed the TS limit. HPCI and | | CIVs were returned to an operable status approximately 3 hours after being | | declared inoperable. At the time of this event, the RCIC system was | | inoperable for planned maintenance so the LCO entered for HPCI was more | | restrictive allowing 12 hours rather than the normal 14 day LCO for HPCI. | | | | *** THIS EVENT WAS RETRACTED AT 1357 ON 11/13/2002 BY CLARE BLEAU TO ERIC | | THOMAS *** | | | | The licensee is retracting this report based on the following: | | | | "On 10/17/02 Event Notification #39300 was completed pursuant to 10 CFR | | 50.72 (b)(3)(v)(D) due to the 250 Volt Station Battery 1D4 being declared | | inoperable which caused the High Pressure Coolant Injection (HPCI) system to | | also be inoperable. At the time that this occurred, the Reactor Core | | Isolation Cooling (RCIC) system was also inoperable due to preplanned | | maintenance. This required that a 12 hour to hot shutdown and 36 hour to | | cold shutdown LCO be entered per Technical Specification 3.5.1.J. | | Maintenance was performed on battery 1D4 and it was returned to operability. | | The other related LCOs were also exited prior to plant shutdown. | | | | "An operability evaluation was subsequently completed which determined that | | 1D4 could have performed its design function with the data taken from STP | | 3.8.4-05. C&D Technologies has confirmed this. Only one of the two | | connections needs to be below 50 micro ohms to meet TS 3.8.4.5. | | | | "If all of the discharge current were to pass through the 129 micro ohm | | connection, the voltage drop would be 0.06 volts. This has no bearing on the | | design function of the 250 VDC system. 1D4 currently has a design margin of | | 1.65 (65% excess battery capacity). Therefore, battery 1D4 actually was | | operable and capable of performing its required safety function. The PCIV | | [Primary Containment Isolation Valve] LCO 3.6.1.3 was also entered for | | 250VDC MOVs that are PCIVs. This included the HPCI outboard steam supply | | valve MO-2239 and the HPCI feedwater injection isolation valve MO-2312. | | Review of the shift logs and discussion with the shift manager confirmed | | that these valves were not closed so that HPCI remained available during | | this event. No LER is required under 10 CFR 50.73 (a)(2)(v)(D) and the | | 8-hour Non-emergency notification under 10 CFR 50.72 (b)(3)(v)(D) (EN#39300) | | can be retracted." | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | | | | Notified Bruce Burgess, R3DO. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39352 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 11/07/2002| |LICENSEE: HARRINGTON GEOTECHNICAL ENGINEERING |NOTIFICATION TIME: 12:50[EST]| | CITY: ORANGE REGION: 4 |EVENT DATE: 10/06/2002| | COUNTY: ORANGE STATE: CA |EVENT TIME: 04:30[PST]| |LICENSE#: CA 5657 AGREEMENT: Y |LAST UPDATE DATE: 11/13/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT GREGER | | | HQ OPS OFFICER: MIKE RIPLEY | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING STOLEN MOISTURE DENSITY GAUGE | | | | The licensee reported at 1115 PST on 7/6/02 that a CPN Model MC3 moisture | | density gauge was stolen from the back of the licensee's pickup truck on | | 7/06/02 sometime between 0430 and 0530 PST in the city of Orange, CA . The | | gauge serial number is not currently available. Gauge contains nominally 10 | | millicuries Cs-137 and 30 millicuries Am-241/Be. The gauge was chained and | | locked in the back of the pickup and the chain was found cut. Local law | | enforcement responded. The licensee plans on issuing a press release and a | | reward for the return of the gauge. | | | | ****UPDATE ON 11/13/02 AT 14:100 FROM LAURA**** | | | | The above text listed the incorrect date for the event. The event occurred | | on 11/6/02 and NOT 7/6/02. | | | | Notified DIRO (McGinty) and R4DO (Cain). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39356 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 11/08/2002| |LICENSEE: LITTON SYSTEMS, INC. |NOTIFICATION TIME: 09:41[EST]| | CITY: Apopka REGION: 2 |EVENT DATE: 11/07/2002| | COUNTY: STATE: FL |EVENT TIME: [EST]| |LICENSE#: 2159-1 AGREEMENT: Y |LAST UPDATE DATE: 11/08/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES R. OGLE R2 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JERRY EAKINS | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LOST OR STOLEN AM-241 SOURCE | | | | "Licensee reported at 1530 [EST] that source could not be found during | | current inventory. Last inventory was performed on 14 February. Licensee is | | conducting an investigation." | | | | The lost or stolen material is a sealed 4 microcurie Am - 241 source used | | for military sighting application. | | | | The State of Florida Bureau of Radiation Control radiological incident | | number is FL02-172. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39367 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 11/13/2002| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 04:53[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/13/2002| +------------------------------------------------+EVENT TIME: 04:07[EST]| | NRC NOTIFIED BY: J.C. WILLIAMS |LAST UPDATE DATE: 11/13/2002| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LEONARD WERT R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 21 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP FROM 21% POWER | | | | "Unit Two Reactor was at 21% power and Main Turbine roll up was in progress | | to synch to [the] grid after 2R9 refueling outage. Main feedwater was in | | service to all 4 steam generators. Steam generator #3 water level increased | | to the Hi-Hi P-14 setpoint which tripped the main turbine and main | | feedwater. AFW [auxiliary feedwater] actuated as required. The reactor was | | manually tripped. All rods fully inserted. The cause of the transient is | | being evaluated at this time. The reactor is stable in Mode 3 [Hot | | Standby]." | | | | Highest steam generator level attained was 88%. | | | | Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39368 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 11/13/2002| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 10:13[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 11/13/2002| +------------------------------------------------+EVENT TIME: 04:58[CST]| | NRC NOTIFIED BY: D. CLARK |LAST UPDATE DATE: 11/13/2002| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRUCE BURGESS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EMERGENCY DIESEL GENERATOR AUTOSTARTED AND LOADED TO DIVISION 2 BUS. | | | | "At 0458 CST on 11/13/02, an undervoltage was detected on 4 KV ESS Div 2 | | Bus 14-1. The normal feed breaker to the bus auto tripped, the U-1 | | Emergency Diesel Generator auto started, and loaded to the bus. The | | preliminary investigation determined that work was being performed in a | | breaker cubicle adjacent to the bus auxiliary cubicle. Vibration from the | | work may have caused the bus potential fuse drawer to fall open, actuating | | the bus undervoltage relay. Normal power to the bus was restored at 0538 | | hours. A prompt investigation is in progress." | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39369 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 11/14/2002| | UNIT: [] [] [3] STATE: SC |NOTIFICATION TIME: 05:24[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 11/14/2002| +------------------------------------------------+EVENT TIME: 04:19[EST]| | NRC NOTIFIED BY: NEIL CONSTANCE |LAST UPDATE DATE: 11/14/2002| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LEONARD WERT R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 A/R Y 100 Power Operation |0 Hot Standby | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP | | | | "The Moisture Separator drain tanks each provide a trip signal to the main | | turbine on a high level on 2 [of] 3 level switches. At 0419 [EST], 2 [of] 3 | | level switches indicated a high level in the 3A Moisture Separator Drain | | Tank Level, resulting in a MT [Main Turbine] trip and anticipatory RPS trip. | | Post-trip response was normal." | | | | All rods inserted into the core. No PORV's lifted. No ECCS actuation. The | | cause of the heater drain system upset is under investigation. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021