Event Notification Report for November 13, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/12/2002 - 11/13/2002 ** EVENT NUMBERS ** 39352 39356 39359 39364 39365 39367 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39352 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 11/07/2002| |LICENSEE: HARRINGTON GEOTECHNICAL ENGINEERING |NOTIFICATION TIME: 12:50[EST]| | CITY: ORANGE REGION: 4 |EVENT DATE: 10/06/2002| | COUNTY: ORANGE STATE: CA |EVENT TIME: 04:30[PST]| |LICENSE#: CA 5657 AGREEMENT: Y |LAST UPDATE DATE: 11/07/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT GREGER | | | HQ OPS OFFICER: MIKE RIPLEY | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING STOLEN MOISTURE DENSITY GAUGE | | | | The licensee reported at 1115 PST on 7/6/02 that a CPN Model MC3 moisture | | density gauge was stolen from the back of the licensee's pickup truck on | | 7/06/02 sometime between 0430 and 0530 PST in the city of Orange, CA . The | | gauge serial number is not currently available. Gauge contains nominally 10 | | millicuries Cs-137 and 30 millicuries Am-241/Be. The gauge was chained and | | locked in the back of the pickup and the chain was found cut. Local law | | enforcement responded. The licensee plans on issuing a press release and a | | reward for the return of the gauge. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39356 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 11/08/2002| |LICENSEE: LITTON SYSTEMS, INC. |NOTIFICATION TIME: 09:41[EST]| | CITY: Apopka REGION: 2 |EVENT DATE: 11/07/2002| | COUNTY: STATE: FL |EVENT TIME: [EST]| |LICENSE#: 2159-1 AGREEMENT: Y |LAST UPDATE DATE: 11/08/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES R. OGLE R2 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JERRY EAKINS | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LOST OR STOLEN AM-241 SOURCE | | | | "Licensee reported at 1530 [EST] that source could not be found during | | current inventory. Last inventory was performed on 14 February. Licensee is | | conducting an investigation." | | | | The lost or stolen material is a sealed 4 microcurie Am - 241 source used | | for military sighting application. | | | | The State of Florida Bureau of Radiation Control radiological incident | | number is FL02-172. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39359 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 11/08/2002| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 14:50[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/08/2002| +------------------------------------------------+EVENT TIME: 13:10[EST]| | NRC NOTIFIED BY: V. BELLAMY |LAST UPDATE DATE: 11/08/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHARLES R. OGLE R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY | | | | A contract supervisor tested positive for drugs during a random test. The | | employee's access to the plant has been terminated. Refer to HOO log for | | additional details. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39364 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 11/12/2002| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 13:01[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/12/2002| +------------------------------------------------+EVENT TIME: 09:48[EST]| | NRC NOTIFIED BY: Joe Sullivan |LAST UPDATE DATE: 11/12/2002| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |HAROLD GRAY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP OF SALEM UNIT 1 DUE TO LOW S/G WATER LEVEL CAUSED BY | | FEED PUMP RUNBACK | | | | "This 4-hour notification is being made to report that Salem Unit 1 reactor | | was manually tripped at 0948 [EST] (RPS actuation). The trip was initiated | | due to low steam generator level (~16% narrow range). The low SG level | | appears to have been caused due to a runback of the 11 steam generator feed | | pump (SGFP) to idle. The cause of the runback has not been determined at | | this time. As a result of the runback, the level in steam generators | | dropped and the operators initiated a main turbine runback and tripped 11 | | SGFP manually. When operators observed the steam generators approaching the | | automatic reactor trip setpoint (14%), a manual reactor trip was initiated. | | | | "11, 12 & 13 auxiliary feed water pumps auto started after the trip due to | | valid steam generator low level, as expected on a unit trip. Main feedwater | | to the steam generators was isolated due to the "feed water interlock" which | | is expected on a normal trip. Additionally the ATWS mitigation system | | (AMSAC) did actuate post trip due to low steam generator levels but all | | auxiliary feed water pumps were already running prior to the actuation. | | | | "Salem Unit-1 is currently in MODE 3 [Hot Standby]. Reactor coolant system | | temperature is 547 [degrees] F with pressure at 2235 PSIG. Unit 1 has no | | shutdown tech. spec. action statements in effect. Major equipment out of | | service for planned maintenance includes the 16 service water pump which is | | expected back later today and Salem Unit-3 which is scheduled to be | | available on 11/15/02. | | | | "There were no personnel injuries or radiological occurrences associated | | with this event." | | | | Additionally, the licensee indicated that while the exact cause of the | | runback is not known, there was ongoing work on the limit switches for the | | 11 SGFP at the time of the runback, and there was some arcing in the | | switches. | | | | The licensee notified the resident inspector of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39365 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 11/12/2002| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 16:12[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 11/12/2002| +------------------------------------------------+EVENT TIME: 12:30[MST]| | NRC NOTIFIED BY: DON STRAKA |LAST UPDATE DATE: 11/12/2002| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHUCK CAIN R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Startup |0 Startup | |2 N Y 99 Power Operation |99 Power Operation | |3 N Y 99 Power Operation |99 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNINTENTIONAL RELEASE OF REVERSE OSMOSIS PRODUCT WATER | | | | "The following event description is based on information currently | | available. If through subsequent reviews of this event, additional | | information is identified that is pertinent to this event or alters the | | information being provided at this time, a follow-up notification will be | | made via the ENS or under the reporting requirements of 10CFR50.73. | | | | "On November 12, 2002, APS reported to the Arizona Department of | | Environmental Quality (ADEQ) the unintentional release of less than 500 | | gallons of reverse osmosis (RO) product water to sedimentation basin #2 that | | occurred on October 19, 2002 during a storm. RO product water is make-up | | water to the site drinking water system and meets all aquifer water quality | | standards. The Ground Water Quality Protection Permit does not authorize | | such a release. | | | | "This report to the ADEQ is in the form of a letter sent via certified | | mail. | | | | "No news release is anticipated." | | | | The licensee notified the resident inspector of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39367 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 11/13/2002| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 04:53[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/13/2002| +------------------------------------------------+EVENT TIME: 04:07[EST]| | NRC NOTIFIED BY: J.C. WILLIAMS |LAST UPDATE DATE: 11/13/2002| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LEONARD WERT R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 21 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP FROM 21% POWER | | | | "Unit Two Reactor was at 21% power and Main Turbine roll up was in progress | | to synch to [the] grid after 2R9 refueling outage. Main feedwater was in | | service to all 4 steam generators. Steam generator #3 water level increased | | to the Hi-Hi P-14 setpoint which tripped the main turbine and main | | feedwater. AFW [auxiliary feedwater] actuated as required. The reactor was | | manually tripped. All rods fully inserted. The cause of the transient is | | being evaluated at this time. The reactor is stable in Mode 3 [Hot | | Standby]." | | | | Highest steam generator level attained was 88%. | | | | Licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021