Event Notification Report for November 8, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/07/2002 - 11/08/2002 ** EVENT NUMBERS ** 39346 39350 39351 39353 39354 39355 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39346 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 11/06/2002| |LICENSEE: SCIENCE APPLICATIONS INTERNATIONAL CO|NOTIFICATION TIME: 00:25[EST]| | CITY: San Diego REGION: 4 |EVENT DATE: 09/30/2002| | COUNTY: STATE: CA |EVENT TIME: [PST]| |LICENSE#: CA 2290-37 AGREEMENT: Y |LAST UPDATE DATE: 11/06/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT GREGER | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TWO SEALED CESIUM SOURCES INADVERTENTLY SHIPPED WITH VEHICLES | | | | " SAIC [Science Applications International Corp.] sold two Mobile VACIS | | trucks to the Department of the Army-SECOM. The Mobile Vehicle and Cargo | | Inspection System (VACIS) is a truck-mounted gamma-ray imaging system | | designed to non-intrusively inspect the contents of trucks, containers, | | cargo and passenger vehicles for explosive devices and/or contraband. | | | | "Each Mobile VACIS truck contains one 1.6 Ci Cs-137 sealed source. The | | trucks were to be shipped first, then the Cs-137 sealed sources were to be | | shipped later. However on September 30, 2002, the trucks were shipped with | | the sealed sources inside by mistake without the proper DOT paperwork and | | marking/labeling. This mistake was not discovered until November 5, 2002, | | when SAIC prepared to ship the sources. They then discovered that the | | sources were inside the trucks that had been shipped previously. The trucks | | were shipped first to Houston by ground and then overseas by ocean carrier. | | The two shipping companies involved are US Freight and Saudi Arabia | | Shipping. SAIC has faxed all DOT shipping information to the carrier. The | | shipment is not due to arrive in port until November 15, 2002. The company | | plans to have a representative meet the shipment when it arrives at port. | | | | "According to SAIC, the sources are in type A containers that are locked. | | SAIC has the key in their possession- without this key the sources cannot be | | removed. The highest reading on the truck found during the package survey | | prior to shipment was 50 microR/hour." | | | | The State of California has notified NRC Region 4 (Linda McLean) of this | | event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39350 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WAYNE STATE UNIVERSITY |NOTIFICATION DATE: 11/07/2002| |LICENSEE: WAYNE STATE UNIVERSITY |NOTIFICATION TIME: 08:17[EST]| | CITY: DETROIT REGION: 3 |EVENT DATE: 11/06/2002| | COUNTY: STATE: MI |EVENT TIME: 09:00[EST]| |LICENSE#: 210074108 AGREEMENT: N |LAST UPDATE DATE: 11/07/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MONTE PHILLIPS R3 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MARY SVOBODA | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BLO2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PHOSPHORUS 32 SOURCES INADVERTENTLY SENT TO LANDFILL WITH TRASH | | | | On 11/06/02 at approximately 0600 EDT a Wayne State University custodian | | mistakenly picked up two shielded 250 microcurie P 32 sources and disposed | | of them as trash. The trash and sources were subsequently disposed of at a | | landfill site. The university Office of Environmental Health and Safety | | contacted the landfill operator to try to locate the sources but was told | | that the pit in which it would have been placed had been covered over. The | | sources were used by the university for bio-med research. The licensee plans | | to notify the State of Michigan of this event. | | | | * * * * UPDATE FROM MARY SVOBODA TO MIKE RIPLEY 1533 EST 11/7/02 * * * | | | | On 11/07/02 at 1533 EST, the licensee updated the initial information | | stating that the radioactive material was in the form of two vials of P 32 | | rather than sealed sources. In addition, the material was placed in the | | dumpster between 0200 and 0700 EST on 11/06/02, and the landfill site is | | located in Riverview, MI. The licensee is forwarding a written report to | | Region 3. Notified NMSS (D. Broaddus) and R3DO (M. Phillips). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39351 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 11/07/2002| | UNIT: [1] [2] [] STATE: MD |NOTIFICATION TIME: 10:22[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/07/2002| +------------------------------------------------+EVENT TIME: 09:30[EST]| | NRC NOTIFIED BY: BRUCE SHICK |LAST UPDATE DATE: 11/07/2002| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LAWRENCE DOERFLEIN R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSITIVE INDICATION OF COLIFORM IN WATER SAMPLING | | | | Water sampling taken from the office cleaning facility indicated positive on | | total coliform bacteria. Fecal coliform results were negative. Chlorine | | residuals established at the time of the sample have been reverified and the | | licensee believes it was in the sample analysis. Back-up sampling will be | | taken tomorrow, 11/8/02, and send for sampling verification. | | | | The Licensee notified the Maryland Department of the Environment and the NRC | | Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39353 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BYRON REGION: 3 |NOTIFICATION DATE: 11/07/2002| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 14:42[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/07/2002| +------------------------------------------------+EVENT TIME: 12:47[CST]| | NRC NOTIFIED BY: MIKE WINTER |LAST UPDATE DATE: 11/07/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON OVER TEMPERATURE DELTA-TEMPERATURE | | | | "Unit 1 automatically tripped on over-temperature delta-temperature reactor | | trip signal at 1247. All control rods fully inserted. The 1A auxiliary | | feedwater pump was manually started to supply the steam generator, and the | | 1B auxiliary feedwater pump started automatically on Low-2 Steam generator | | level [18%]. The cause of the transient was apparently a turbine | | malfunction. Pressurizer power operated relief valves opened automatically | | to lower reactor coolant pressure, and were successfully reclosed. Steam | | generator relief valves also opened to lower steam pressure, and reclosed. | | The plant has been stabilized at normal zero power temperature and pressure | | per emergency procedures." | | | | The Licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39354 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 11/07/2002| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 16:58[EST]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 11/07/2002| +------------------------------------------------+EVENT TIME: 14:39[EST]| | NRC NOTIFIED BY: BERRY FOSTER |LAST UPDATE DATE: 11/07/2002| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHARLES R. OGLE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP | | | | "Reactor trip believed to be the result of 500KV switchyard maintenance. | | One Main generator output breaker was open for maintenance prior to the | | trip, and when the second output breaker opened, the main turbine tripped | | causing the plant to trip. Emergency Operating Procedure 2, Vital Systems | | Status Verification has been completed satisfactorily. Emergency Operating | | Procedure 10, Post Trip Stabilization, has also been completed | | satisfactorily. The root cause of the trip is unknown at this time." | | | | All control rods fully inserted. Steam generator reliefs lifted to relieve | | steam pressure, and reclosed. No pressure operated relief valve lifted. | | | | Licensee notified NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39355 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 11/07/2002| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 17:16[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/01/2002| +------------------------------------------------+EVENT TIME: 17:27[CST]| | NRC NOTIFIED BY: BOB BRINKLEY |LAST UPDATE DATE: 11/07/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling Shutdow|0 Refueling Shutdow| | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID SPECIFIED SYSTEM ACTUATION DUE TO POST MAINTENANCE TESTING | | | | "Per 10CFR50.73(a)(1), we make the following report under | | 10CFR50.73(a)(2)(iv)(A) | | | | "At 1727 on 11/01/02, while performing Solid State Protection System | | Post-Modification Testing (PMT), a fault in Logic Train R resulted in an | | invalid Train A Safety Injection (SI) actuation signal, Containment | | Ventilation Isolation (CVI), and Containment Phase A isolation. | | | | "We provide the following information: | | (a) The specific train and systems that were actuated: Train 'A' Safety | | Injection signal resulted in actuation of ESF Diesel Generator 21, | | Containment Isolation Phase 'A', Containment Ventilation Isolation and other | | designated equipment designed to start on a safety injection signal. | | (b) Whether each train actuation was complete or partial: This actuation | | signal only affected Train 'A' and was complete. | | (c) Whether or not the system started and functioned successfully: All | | affected systems functioned properly." | | | | The Licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021