Event Notification Report for October 10, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/09/2002 - 10/10/2002 ** EVENT NUMBERS ** 39260 39262 39263 39264 39265 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39260 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 10/09/2002| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 03:31[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 10/09/2002| +------------------------------------------------+EVENT TIME: 03:07[EDT]| | NRC NOTIFIED BY: LOU GAREAU |LAST UPDATE DATE: 10/09/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |JOHN WHITE R1 | |10 CFR SECTION: |WILLIAM BECKNER NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |NADER MAMISH IRO | | |JIM DUNKER FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO FIRE IN PROTECTED AREA LASTING GREATER THAN 10 | | MINUTES | | | | "Unusual event was classified based on a fire in the protected area lasting | | > 10 minutes. The fire started in the motor of the 'B' circulating water | | pump. It was 'contained' to that location (the CW pump motor). Motor | | [is]still smoldering, [but] it is controlled and contained. Steam Generator | | Blowdown system isolated due to high flash tank level. Multiple rad | | monitors went into alarm due to voltage surge." | | | | The NRC Resident Inspector will be notified. | | | | The Licensee reported that no offsite assistance was requested and that the | | State (NH) was notified. | | | | ***UPDATE JIM HILL TO JOHN MacKINNON 0614 EDT 10/9/02*** | | | | The Unusual Event was Terminated at 0547 EDT. | | | | The Licensee has notified the NRC Resident Inspector and the State(NH). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39262 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COLUMBIA GENERATING STATIREGION: 4 |NOTIFICATION DATE: 10/09/2002| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 15:30[EDT]| | RXTYPE: [2] GE-5 |EVENT DATE: 08/16/2002| +------------------------------------------------+EVENT TIME: 02:54[PDT]| | NRC NOTIFIED BY: CRAIG SLY |LAST UPDATE DATE: 10/09/2002| | HQ OPS OFFICER: MIKE RIPLEY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JONES R4 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID SYSTEM ACTUATION DUE TO LOSS OF RPS BUS "A" | | | | "On August 16, 2002 at approximately 0254 hours, a loss of Reactor | | Protection System (RPS) Bus A occurred while operators were attempting to | | reset a half-scram on the A2 logic channel of the RPS. The A2 logic reset | | attempt was required in accordance with a surveillance test procedure that | | was in progress, PPM OSP-RPS-Q402, MSIV Closure Scram Functional. Upon loss | | of RPS Bus A, control room operators entered Abnormal Procedure ABN-RPS, | | Loss of RPS, and an operator was dispatched to investigate the problem. | | | | "The operator investigating the problem discovered that the Motor Generator | | Set (RPS-MG-A) that supplies RPS Bus A was running with both of its | | electrical protection assemblies (EPAs) in the tripped position. In | | accordance with procedure ABN-RPS, operators transferred RPS Bus A to its | | alternate power supply and then reset the half-scram and associated | | containment outboard isolations. The operators then exited PPM OSP-RPS-Q402. | | The follow-up investigation found that the loss of the RPS Bus A was due to | | a trip of the RPS-MG-A output breaker (RPS-MG-CB1) on over-voltage. The | | output breaker trip caused both downstream Electrical Protection Assemblies | | (RPS-EPA-3A and RPS-EPA-3C) to trip. This is the expected and required | | response for RPS-EPA-3A and RPS-EPA-3C." | | | | The loss of power to RPS Bus A had the following effects on the plant: An | | actuation of RPS trip system A (Half-Scram), Main Steam Line Radiation | | Monitors A and C lost power; a trip of the Balance of Plant isolation logic | | in control room relay Cabinet RC-1; an outboard primary containment | | isolation signal was received by the following (valves closed or were | | already closed): Main Steam Line Drain Valves, Reactor Water Sample Valve, | | Drywell Floor and Equipment Drain Isolation Valves, Residual Heat Removal | | (RHR) Discharge to Radwaste and Heat Exchanger Sample Isolation Valves, RHR | | Shutdown Cooling (SDC) Reactor Head Spray Isolation Valve, SDC Return | | Valves, Reactor Water Cleanup (RWCU) Suction Valve. All of these plant | | equipment responses were as expected and per plant design. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 39263 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST PATRICK HOSPITAL |NOTIFICATION DATE: 10/09/2002| |LICENSEE: ST PATRICK HOSPITAL |NOTIFICATION TIME: 16:38[EDT]| | CITY: MISSOULA REGION: 4 |EVENT DATE: 08/30/2002| | COUNTY: STATE: MT |EVENT TIME: [MDT]| |LICENSE#: 121677302 AGREEMENT: N |LAST UPDATE DATE: 10/09/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JONES R4 | | |ERIC LEEDS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BREWER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33 MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | A patient was receiving a gynecological implant of Cs-137 which had the | | incorrect activity entered into the computer. The calibrated activity was | | inadvertently entered instead of the current activity. The patient was | | also receiving external beam therapy from a linear accelerator along with | | the Cs-137 implant. With the incorrect data being entered into the | | computer, the patient received a total dose(external and implant) which | | deviated below the prescribed dose by approximately 16%. The implant | | dosage, however had greater than a 20% deviation less than the prescribed | | dose. This medical misadministration was discovered on 10/09/02 @ 1620 MT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39264 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 10/09/2002| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 17:12[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 10/09/2002| +------------------------------------------------+EVENT TIME: 13:59[EDT]| | NRC NOTIFIED BY: LEONE |LAST UPDATE DATE: 10/09/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN WHITE R1 | |10 CFR SECTION: |WILLIAM BECKNER NRR | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY DIESEL GENERATORS DECLARED INOPERABLE | | | | "At 1518 hours on October 9, 2002 Indian Point Unit 2 commenced a controlled | | shutdown per T/S 3.0.1. T/S 3.0.1 was entered because Emergency Diesel | | Generators (EDG) 21 and 23 were declared inoperable. EDG 23 was declared | | inoperable at 2152 hours on October 8, 2002 due to failure of monthly test. | | EDG 21 was declared inoperable at 1359 hours on October 9, 2002 due to | | indications of jacket water in the lube oil system. EDG 23 was declared | | operable at 1635 hours on October 9, 2002 following corrective actions and | | testing at which time T/S 3.0.1 was exited. They think EDG 21 may have a | | cracked engine head. The reactor power reduction was stopped at 97 percent, | | but the are planning to return to 100%. The to the Public Service | | Commission was informed of the reason for the downpower at 1610 hours on | | October 9, 2002." | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39265 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 10/10/2002| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 00:20[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 10/10/2002| +------------------------------------------------+EVENT TIME: 00:08[EDT]| | NRC NOTIFIED BY: ROBERT BOESCH |LAST UPDATE DATE: 10/10/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN WHITE R1 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN DUE TO FAILURE TO MEET 2 OFFSITE POWER SUPPLIES | | | | "Susquehanna Unit 1 initiated a Technical Specification required shutdown | | due to failure to meet LCO 3.8.1 Action A.3 and the Notice of Enforcement | | Discretion (Docket No. 50-387), for operating with one inoperable offsite | | power supply. The offsite power supply was originally lost due to a | | Transformer failure on 10/3/02 at 0230 est. The NOED allowed Unit One to | | continue operation until 10/1 0/02 at 0230. The shutdown requirements of LCO | | 3.8.1 Action F (Mode 3 within 12 hours and Mode 4 within 36 hours) are being | | implemented. It has been determined that replacement activities of the | | transformer will not be completed in time to meet the NOED, and therefore | | shutdown of unit 1 has been initiated as of 0008. | | | | "This event is a Technical Specification required shutdown, and is | | reportable as a four hour ENS Notification under 10 CFR 50.72(b)(2)(I)." | | | | The Licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021