Event Notification Report for July 5, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/04/2002 - 07/05/2002 ** EVENT NUMBERS ** 39033 39041 . +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39033 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MARYLAND DEPT OF THE ENVIRONMENT |NOTIFICATION DATE: 07/01/2002| |LICENSEE: NEUTRON PRODUCTS |NOTIFICATION TIME: 08:16[EDT]| | CITY: ROCKVILLE REGION: 1 |EVENT DATE: 06/27/2002| | COUNTY: MONTGOMERY STATE: MD |EVENT TIME: 08:00[EDT]| |LICENSE#: MD 3102501 AGREEMENT: Y |LAST UPDATE DATE: 07/01/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MICHAEL MODES R1 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ALAN JACOBSON | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RADIATION ALARM AT A WASTE TRANSFER STATION WAS ACTIVATED BY A TUCK | | CONTAINING REFUSE. | | | | | | A truck containing a roll off refuse container set off the radiation monitor | | at the Montgomery County Waste Transfer Station located in Rockville, MD at | | 0800 hours on 06/27/02. The refuse container was searched and a bag | | containing paper towels and rags found to be contaminated with cobalt-60 | | with a radiation reading of 0.5 mr/hr. The load was rejected and sent back | | to Neutron Products Incorporated, Dickerson, MD. The load was evaluated and | | the radioactive material was removed and placed into storage with | | radioactive waste. Neutron Products was cited by the State of Maryland for | | improper disposal of radioactive waste and inadequate surveying and | | monitoring. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39041 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 07/04/2002| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 05:57[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 07/04/2002| +------------------------------------------------+EVENT TIME: 01:33[CDT]| | NRC NOTIFIED BY: MERRIKEN |LAST UPDATE DATE: 07/04/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |PATRICK HILAND R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 95 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM FROM 94.6% POWER DUE TO TURBINE TRIP CAUSED BY GENERATOR TRIP | | AND LOCKOUT | | | | On July 4, 2002, at 0133, Clinton Power Station scrammed from 94.6% due to a | | Turbine Trip from a Generator Trip and Lockout. The initiating event for | | the scram is not presently known at this time but it is believed to be a | | problem with the Main Power Transformer (MPT) B. The Sudden Pressure MPT B | | alarm came simultaneously with the reactor scram. The Sudden Pressure MPT B | | alarm is brought in by the Sudden Pressure Fault Relay, which initiates a | | Main Generator trip and lockout, which trips the Main Turbine and initiates | | a reactor scram. | | | | The MPT B deluge system initiated, however, there was no physical evidence | | of any damage to MPT B. After conducting a visual inspection of MPT B, the | | deluge system was secured. A clearance is being applied to MPT B for | | investigation. | | | | The plant is presently in Mode 3, maintaining reactor pressure within a | | pressure band of 550 to 650 psig and level between Level 3 and Level 8, | | which is the normal level band. | | | | The plant responded normally on the scram. All rods fully inserted, no ECCS | | injection occurred and no relief valves lifted. | | | | The NRC Resident Inspector and the State were notified. | | | | | | - | +------------------------------------------------------------------------------+ .
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