Event Notification Report for June 3, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/31/2002 - 06/03/2002 ** EVENT NUMBERS ** 38513 38940 38954 38958 38959 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38513 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/23/2001| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 12:30[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/23/2001| +------------------------------------------------+EVENT TIME: 12:10[EST]| | NRC NOTIFIED BY: CHARLIE PIKE |LAST UPDATE DATE: 06/02/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO FLORIDA STATE INVOLVING RECOVERED SEA TURTLE FROM | | UNIT 1 INTAKE STRUCTURE | | | | "A sea turtle with no external injuries but appearing to be distressed was | | recovered from the Unit 1 Intake Structure. The State Stranding Coordinator | | for sea turtles has been contacted." | | | | * * * UPDATE 11/23/01 AT 1255EST FROM CHARLIE PIKE TO S. SANDIN * * * | | | | "Turtle has died." | | | | The licensee informed both the State of Florida and the NRC Resident | | Inspector. | | | | * * * UPDATE 1413EST ON 12/3/01 FROM JACK BREEN TO FANGIE JONES * * * | | | | At approximately 1215 EST on 12/3/01, a report was made to the Florida | | Department of Fish and Wildlife concerning the recovery of an injured sea | | turtle from the plant's intake canal. The turtle was a green sea turtle in | | the intake canal that appeared distressed and looked to have a wound from a | | boat motor on its back. It will be transferred to the State for | | rehabilitation. | | | | The licensee plans to notify the NRC resident inspector. Notified | | R2DO(MacAlpine). | | | | * * * UPDATE 1333EST ON 12/15/01 FROM JACK BREEN TO JOHN MACKINNON * * * | | | | At approximately 1215 EST on 12/15/01, a report was made to the Florida | | Department of Fish and Wildlife Conservation Commission to pick up a Green | | Turtle for rehabilitation. The Green Turtle was taken from the plant's | | intake canal, and the turtle appears to have shark bites. | | | | The licensee plans to notify the NRC resident inspector. Notified R2DO | | (Chuck Ogle). | | | | * * * UPDATE 1450EST ON 01/06/02 FROM TULLIDGE TO JOHN MACKINNON * * * | | | | At 1350EST, a notification to the State of Florida Department of Fish and | | Wildlife Conservation Commission was made due to finding an injured | | Loggerhead sea turtle in Unit 1 intake. The sea turtle was transported | | offsite for rehabilitation. R2DO (Tom Decker) notified. | | | | The licensee notified the NRC Resident Inspector. | | | | ***UPDATE 1330EST ON 4/23/02 FROM JACK BREEN TO RICH LAURA*** | | | | The licensee rescued a Loggerhead sea turtle from the intake canal. The | | Florida Fish and Wildlife Conservation Commission was notified, and the | | turtle was turned over for rehabilitation. | | | | The NRC Resident Inspector was informed. Notified R2DO (B. Bonser). | | | | ***UPDATE 1241EDT ON 5/29/02 FROM DAVE WILLIAMS TO RICHARD LAURA*** | | | | The licensee reported that an offsite notification was made to the Florida | | Fish and Wildlife Conservation Commission concerning the discovery of a live | | loggerhead sea turtle found in the plant's intake canal. The turtle was | | lethargic and was sent for rehabilitation. | | | | The NRC Resident Inspector was informed. Notified R2DO (K. Landis). | | | | ***** UPDATE AT 1125 EDT ON 06/01/02 FROM CHARLES MARPLE TO LEIGH TROCINE | | ***** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 1020 on 06/01/02, a notification was made to the Florida Fish and | | Wildlife Conservation Commission regarding a weak and emaciated Loggerhead | | turtle found in the plant intake barrier net. The turtle will be sent | | off-site to the Marine Life Center for Rehabilitation." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R2DO (Kerry Landis). | | | | *****UPDATE AT 11:53 EDT ON 6/2/02 FROM MARPLE TO LAURA****** | | | | "A notification was made to the Florida Fish and Wildlife Conservation | | Commission regarding a dead small green sea turtle found in the tangle net. | | The turtle will be maintained on ice for a postmortem examination." | | | | The NRC resident inspector was notified. Notified R2DO (K. Landis) | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38940 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 05/23/2002| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 21:36[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/23/2002| +------------------------------------------------+EVENT TIME: 14:02[EDT]| | NRC NOTIFIED BY: DAVID HALLONQUISTL |LAST UPDATE DATE: 05/31/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |FRANK COSTELLO R1 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 19 Power Operation |27 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH THRUST BEARING TEMPERATURE DURING HIGH PRESSURE COOLANT INJECTION | | (HPCI) OPERABILITY SURVEILLANCE TESTING | | | | HPCI was declared inoperable due to high thrust bearing temperature during | | performance of pump operability surveillance. There was nothing unusual or | | misunderstood other than the cause of the high thrust bearing temperature. | | As a result, the unit entered a 14-day limiting condition for operation. | | | | The licensee plans to notify the NRC resident inspector. | | | | * * * 1522 EDT 5/31/02 THIS EVENT WAS RETRACTED JOHN TWAROG TO MIKE NORRIS* | | * * | | | | "On 05/23/02 during a plant start-up with the reactor at approximately 19.5% | | power, a High Pressure Coolant Injection (HPCI) turbine thrust bearing | | temperature high alarm (SO 12) occurred while performing operational | | surveillance testing of the HPCI system. The turbine thrust bearing | | displayed a constant temperature rise until the alarm set point of 200 F was | | reached. The turbine was secured a few minutes later and the temperature | | indication on the thrust bearing peaked at approximately 200 F before | | indication of cool down appeared. | | | | "The Manager of Maintenance Mechanical/Electrical consulted a Kingsberry | | Thrust bearing Company Engineer who stated that temperature-induced bearing | | damage will not occur until the bearing temperature exceeds 250 F. The | | maximum indicated bearing temperature received was less than 210 F. | | Additionally, an oil sample was taken and visually examined with no | | indication of gross suspended particulate. | | | | "System Engineering completed an assessment of this condition on 05/24/02 | | which revealed evidence that provided credible justification using sound | | engineering judgment that the thrust bearing temperature indication was | | false and an actual high temperature condition did not exist at any time | | during the surveillance testing. Insulation had been removed from the | | turbine casing around the turbine gland seal during the mid-cycle outage. | | This resulted in an elevated temperature indication of the thrust bearing | | due to radiant and convective heat transfer to the temperature indicator's | | thermocouple external to the thrust bearing. Steam leaking past the gland | | seal may have also contributed to the temperature increase. When the exposed | | area of the HPCI turbine was reinsulated, indicated temperature began to | | rapidly decrease. Subsequent HPCI system operation supported these | | conclusions. The maximum thrust bearing temperature indication received | | during this surveillance was 158 F. Trend analysis demonstrated that the | | maximum temperature would have peaked at approximately 175 F." | | | | The NRC Resident Inspector has been notified. R1DO (Rogge) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38954 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 05/31/2002| | UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 02:02[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/31/2002| +------------------------------------------------+EVENT TIME: 01:16[EDT]| | NRC NOTIFIED BY: PAUL SIMMON |LAST UPDATE DATE: 05/31/2002| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KERRY LANDIS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 71 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED AN AUTOMATIC REACTOR TRIP DUE TO GENERATOR PROTECTION | | ACTUATION | | | | "On May 31, 2002 at 0116EDT, Unit 2 was at 71% reactor power and increasing | | to 100% when the reactor tripped due to a failure with the generator stator | | cooling water system. All systems responded as designed. The plant is | | currently in mode 3, full temperature and pressure." | | | | Both motor-driven and the steam-driven auxiliary feedwater pumps actuated | | and are currently supplying the Steam Generators with the Main Condenser | | removing decay heat. The steam-driven auxiliary feedwater pump was | | subsequently secured and returned to standby. All rods fully inserted with | | all EDGs available, if necessary. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38958 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 06/01/2002| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 20:27[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 06/01/2002| +------------------------------------------------+EVENT TIME: 18:40[EDT]| | NRC NOTIFIED BY: PHILLIP ROSE |LAST UPDATE DATE: 06/01/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KERRY LANDIS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 2 Startup |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING STARTUP | | | | "During plant startup, a spike occurred on the N32/N36 channel of | | source/intermediate range excore neutron flux detectors. The reactor | | tripped automatically. All system[s] operated normally. Emergency | | feedwater was already in service for the startup, no actuation occurred." | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38959 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 06/02/2002| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 01:37[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 06/02/2002| +------------------------------------------------+EVENT TIME: 01:02[EDT]| | NRC NOTIFIED BY: HOMMEL |LAST UPDATE DATE: 06/02/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: ALERT |PETE ESELGROTH R1 | |10 CFR SECTION: |WILLIAM BECKNER NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |TONY MCMURTRAY SRI | | |RANDY BLOUGH R1 | | |DONALD FLOREK R1 | | |MIKE BUCKLEY RI | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD CARBON DIOXIDE INJECTION INTO THE E3 DIESEL ROOM | | | | This "Cardox system" injection occurred at 0033 during diesel testing. An | | alert was declared at 0102 due to the detection of toxic gases(CO2) within a | | vital area. The room was evacuated(only two people were in the room at that | | time) safely and there were no injuries. There was no fire damage and the | | CO2 tank was isolated. | | | | The NRC Resident Inspector, State and local agencies were notified by the | | licensee. | | | | Notified FEMA (Sweetser), DOE(Morroney), EPA/DOT/NRC(Thomas), CDC(Rhyne), | | FDA(Shandruk) and OHS(Edwards) | | | | * * * UPDATE ON 6/2/02 @ 0420 BY CAMPBELL TO GOULD * * * | | | | The Alert was terminated at 0301. | | | | Notified DOE(Yates), CDC(Rhyne), EPA/NRC/DOT(Thomas), FEMA(Sulivan), | | OHS(Edwards) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021