Event Notification Report for May 14, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/13/2002 - 05/14/2002 ** EVENT NUMBERS ** 38915 38916 38917 38918 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38915 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 05/13/2002| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 02:39[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/12/2002| +------------------------------------------------+EVENT TIME: 23:01[EDT]| | NRC NOTIFIED BY: BRADDOCK D. LEWIS |LAST UPDATE DATE: 05/13/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTON VEGEL R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO AN INSTRUMENTATION RACK POWER SUPPLY FAILURE | | WHICH CAUSED A STEAM GENERATOR FEEDWATER REGULATING VALVE TO FAIL CLOSED | | | | The following text is a portion of a facsimile received from the licensee: | | | | "DC Cook Unit 2 tripped from full power due to an instrumentation rack power | | supply failure on 05/12/02 [at] 2301. All control rods fully inserted. No | | Safety Injection was required. The Unit 2 Reactor is stable and | | subcritical. The Steam Generator Stop Valves were manually closed by the | | Operating Crew to stabilize RCS Temperature in accordance with Plant | | operating procedures. Reactor Coolant Temperature is being maintained | | manually on the Steam Generator Atmospheric relief valves at No-Load T(ave) | | in accordance with plant procedures." | | | | "This instrumentation rack power supply failure caused the #21 Steam | | Generator Feed Regulating Valve to fail CLOSED. The Unit 2 Reactor | | subsequently TRIPPED on Low Level in [the] #21 Steam Generator coincident | | with Low Feedwater Flow. Several control systems were affected by the | | control rack instrumentation failure: Pressurizer Pressure Control - | | transferred control to manual and restored Pressurizer pressure, Pressurizer | | Level Control - transferred control to manual and restored Pressurizer water | | level, Refueling Water Sequence - Manually transferred Charging Pump Suction | | to the RWST. Manual Operator response maintained and restored critical | | plant parameters in MANUAL to normal parameter values." | | | | "Unit 2 entered Technical Specification 3.0.3 for 34 minutes because the | | control system failures and plant system response temporarily caused the | | Boration Flow paths from both the Refueling Water Storage Tank and Boric | | Acid Storage Tanks to become INOPERABLE. Both Boration flow paths were | | subsequently returned to OPERABLE status by manual Operator action." | | | | "The Reactor trip is reportable in accordance with 10 CFR 50.72(b)(2)(iv)(B) | | as an actuation of the Reactor Protection System (RPS) when the Reactor was | | critical. The Reactor TRIP was the result of an instrumentation rack power | | supply failure and was not part of any preplanned test or evolution." | | | | The licensee stated that the unit is currently stable in Mode 3 (Hot | | Standby). The reactor coolant pumps are available for primary system | | transport control. Pressurizer level and pressure control are in manual. | | Normal charging and makeup are available, but the automatic function of the | | refueling water sequence is not available. The auxiliary feedwater pumps | | automatically started as expected and are currently being utilized to supply | | water to the steam generators. Secondary steam is being dumped to | | atmosphere. There is no evidence of steam generator tube leakage, and | | containment parameters are as expected. There were no safety injections and | | none were required, and none of the primary power-operated relief valves | | lifted. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38916 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 05/13/2002| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 03:21[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/13/2002| +------------------------------------------------+EVENT TIME: 00:16[CDT]| | NRC NOTIFIED BY: TOM CLAY |LAST UPDATE DATE: 05/13/2002| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTON VEGEL R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 86 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM ON HIGH WATER LEVEL DUE TO THE FAILURE OF THE | | STARTUP LEVEL CONTROLLER DURING EXTENDED POWER UPRATE TESTING ON FEEDWATER | | LEVEL CONTROL | | | | The following text is a portion of a facsimile received from the licensee: | | | | "With the reactor at 86% power, extended power uprate testing on feedwater | | level control was in progress. A six-inch level step change from 32" to 38" | | was inputted for testing. Feedwater was being controlled by the startup | | level controller. The startup level controller failed to respond, allowing | | reactor water level to go high and cause a reactor scram on level 8, 52". | | All other systems responded normally." | | | | The licensee stated that all control rods fully inserted due to the | | automatic reactor scram and that the highest reactor water level was 53". | | There were no safety injections or emergency core cooling system actuations, | | and none were required. | | | | The licensee stated that the unit is currently in Hot Shutdown. Normal | | feedwater is being supplied to the reactor vessel for level control, and | | pressure is being controlled via the main steam line drains which go to the | | condenser (the heat sink). The outboard main steam isolation valves were | | manually closed. Containment parameters are normal. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38917 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 05/13/2002| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 15:04[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/13/2002| +------------------------------------------------+EVENT TIME: 11:18[EDT]| | NRC NOTIFIED BY: TOD KASPAR |LAST UPDATE DATE: 05/13/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RONALD GARDNER R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Hot Standby |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS-FOR-DUTY REPORT | | | | A contract supervisor tested positive for drug use during a follow-up test. | | The individual's site access has been terminated. Contact the NRC Operations | | Center for additional information. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38918 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/13/2002| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 15:49[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/13/2002| +------------------------------------------------+EVENT TIME: 00:25[EDT]| | NRC NOTIFIED BY: DANIEL J. BOYLE |LAST UPDATE DATE: 05/13/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 | |10 CFR SECTION: |JOSEPH HOLONICH IRO | |NONR OTHER UNSPEC REQMNT |MICHAEL JOHNSON NRR | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |72 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OPERATING LICENSE REPORT OF SIGNIFICANT ELECTRICAL TRANSIENT DUE TO | | LIGHTNING STRIKE | | | | "On May 13, 2002, at 0025, Hope Creek Generating Station experienced a | | significant electrical transient as a result of lightning strike that caused | | the trip and re-closure of the New Freedom Line. | | | | "The most significant impact was the loss of Feedwater Heating Transient due | | to the trip of the 6A, 6B, and 6C Feedwater Heaters. This Feedwater trip | | resulted in a peak transient power level of 105% power. | | | | "Hope Creek Generating Facility Operating License (NPI-57) item 2.C(1) | | specifically authorizes operation of the facility not in excess of 3339 | | megawatts thermal (100%). | | | | "Additionally, Operating [License] Item 2.C(11) prohibits operating the | | facility with Feedwater Heater capacity that would result in a rated power | | Feedwater Heater temperature less than 400 degrees. | | | | "Both of these Operating License conditions were challenged during this | | transient and are reportable IAW section 2F of the Operating License. | | | | "Station power was manually reduced and subsequently stabilized at | | approximately 75% to deal with the transient, and the Feedwater Heaters were | | restored to service. | | | | "Additional equipment affected as a result of the electrical transient is as | | follows: 'C' ECCS keep fill Jockey pump tripped; Hydrogen Water Chemistry | | Injection system tripped; the North and South plant Ventilation Radiation | | Monitoring system tripped; the Drywell Leak Detection system tripped; | | Cooling Tower Blowdown Radiation Monitor tripped; the 'B' 1E Panel room | | Ventilation Train tripped and the standby 'A' train started; the 'A' Control | | Room Ventilation train tripped and the 'B' train auto started. The unit | | sustained a loss of Drywell cooling, and the 'B' Fuel Pool Cooling Pump | | tripped. The RWCU system pumps tripped. | | | | "The plant is stable, and the event is under investigation." | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021