Event Notification Report for April 16, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/15/2002 - 04/16/2002 ** EVENT NUMBERS ** 38776 38813 38854 38855 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38776 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SOUTHEAST MO STATE UNIVERSITY |NOTIFICATION DATE: 03/18/2002| |LICENSEE: SOUTHEAST MO STATE UNIVERSITY |NOTIFICATION TIME: 11:53[EST]| | CITY: CAPE GIRARDEAU REGION: 3 |EVENT DATE: 03/15/2002| | COUNTY: CAPE GIRARDEAU STATE: MO |EVENT TIME: 16:30[CST]| |LICENSE#: 24-09296-02 AGREEMENT: N |LAST UPDATE DATE: 04/15/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN HICKEY NMSS | | |MONTE PHILLIPS R3 | +------------------------------------------------+ | | NRC NOTIFIED BY: WALTER LILLY | | | HQ OPS OFFICER: RICH LAURA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE/TEDE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PERSONNEL OVEREXPOSURE POSSIBLE IF UNCHARACTERIZED ALPHA EMITTER ABSORBED BY | | AIRBORNE INHALATION | | | | During a routine radiological survey, the school found a table in Johnson | | Hall that was contaminated with 150 DPM/100 centimeters squared [initially | | estimated to be approximately 30,000 dpm or 14E-3 microcuries] of | | Americium-241. Johnson Hall, room 222, is normally locked with restricted | | access and the cause of the contamination is historical in nature. The | | table was decontaminated and wrapped in plastic for proper disposal. There | | were no known personnel overexposures due to this event. However, "if 100% | | was absorbed by airborne contamination and deposited on bone surface, it | | would exceed the ALI by 2.3." | | | | The licensee discussed this report with R3(Null). | | | | | | * * * RETRACTION ON 4/15/02 @ 0845 BY LILLY TO GOULD * * * | | | | After reviewing this event with Region 3 personnel it was determined that | | it was not reportable based on a model which shows that the maximum dose | | would be about 2 millirem/yr. | | | | Notified REG 3 RDO (Riemer) and NMSS EO (Hickey) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38813 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ILLINOIS DEPT OF NUCLEAR SAFETY |NOTIFICATION DATE: 03/28/2002| |LICENSEE: SHOLLE CORPORATION |NOTIFICATION TIME: 13:39[EST]| | CITY: NORTHLAKE REGION: 3 |EVENT DATE: 03/27/2002| | COUNTY: STATE: IL |EVENT TIME: [CST]| |LICENSE#: 9201385 AGREEMENT: Y |LAST UPDATE DATE: 04/15/2002| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN MADERA R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE KLINGER | | | HQ OPS OFFICER: MIKE NORRIS | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT FOR A LOST GAUGE | | | | "A general licensee reported the loss of an NDC Infrared Engineering Model | | 103, serial no. 773, containing 100 mCi of Am-241. The gauging device was | | initially installed in 1982. The general licensee is a manufacturer of | | packaging products. The device was apparently installed at one time in a | | plastic extruder line. In November 2000 it was reported to the Department as | | being on the laminator in the plant. While performing the inventory for the | | most recent Departmental self-inspection, the licensee was unable to account | | for this device. Licensee states that it conducted an extensive | | investigation of the circumstances surrounding the disappearance of the | | device. Their investigation continues and they will file the required report | | as soon as possible. The department's investigation is ongoing." | | | | *****UPDATE State of Illinois to R. Laura on April 15, 2002 at 16:30**** | | | | The lost gage was found during renovations in the building. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38854 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 04/15/2002| | UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 02:59[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/15/2002| +------------------------------------------------+EVENT TIME: 00:16[EDT]| | NRC NOTIFIED BY: SIMMONS |LAST UPDATE DATE: 04/15/2002| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |KEN BARR R2 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Hot Standby |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD ESF ACTUATION RESULTING IN AUTOMATIC REPOSITIONING OF AUX | | FEEDWATER VALVES. | | | | | | Unit 2 was in mode 3 and stable following the completion of a preplanned | | shutdown for a refueling outage. The aux feedwater was in service at the | | time of this actuation. The AFW Level Control Valves had been throttled, | | the "B" Main Feedwater Pump reset and Feedwater Isolation (FWI) reset to | | accordance with procedures. The RCS Tavg drifted above 550�F. When the | | RCS Tavg dropped below 550�F, a FWI signal was generated causing the reset | | Main Feedwater Pump to trip and the Aux Feedwater valves to reposition open. | | The Aux Feedwater pumps were already running. An investigation is | | ongoing. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38855 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 04/15/2002| | UNIT: [] [2] [] STATE: AR |NOTIFICATION TIME: 12:04[EDT]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 04/15/2002| +------------------------------------------------+EVENT TIME: 07:33[CDT]| | NRC NOTIFIED BY: JAMES PORTER |LAST UPDATE DATE: 04/15/2002| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LINDA SMITH R4 | |10 CFR SECTION: |THOMAS KOSHY NRR | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION |NADER MAMISH IRO | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEGRADED PRESSURE BOUNDARY AT ARKANSAS NUCLEAR ONE UNIT 2 | | | | "Boron deposits were discovered on five pressurizer heater sleeve | | penetrations during visual inspection. Two additional heater penetrations | | are suspected of leaking, but further inspection activities are required to | | confirm these leaks. Pressurizer heater sleeve penetration leakage is | | considered RCS pressure boundary leakage. Small amounts of boron were | | discovered at each of the five nozzle penetration interfaces. Prior to | | shutdown for refueling, RCS unidentified leakage was about 0.22 gpm. | | Currently, Unit 2 is in reduced inventory with the pressurizer empty." | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021