Event Notification Report for April 9, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/08/2002 - 04/09/2002 ** EVENT NUMBERS ** 38818 38839 38840 38841 38842 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38818 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 03/31/2002| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 05:32[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/31/2002| +------------------------------------------------+EVENT TIME: 04:10[EST]| | NRC NOTIFIED BY: GORDON ROBINSON |LAST UPDATE DATE: 04/08/2002| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM RULAND R1 | |10 CFR SECTION: | | |AINA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | |AINB 50.72(b)(3)(v)(B) POT RHR INOP | | |AINC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N Y 87 Power Operation |87 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DIESEL GENERATORS DECLARED INOPERABLE FOR SHORT TIME PERIOD | | | | "During performance of 24 month Division 1 Diesel Generator LOCA/LOOP | | surveillance testing, two pump start timers failed to meet the required | | acceptance criteria. The A RHR Pump timer actuated at 3.72 seconds | | (criteria: 2.7 sec. to 3.6 sec) and the C ESW Pump timer actuated at 39.24 | | seconds (criteria: 39.6 sec. to 48.4 sec). With failure of the timers proper | | loading on the Diesel Generators is not assured, and they ['A' and 'C'] were | | declared inoperable until the associated pump control breakers were opened. | | The Susquehanna safety analysis requires three operable Diesel Generators to | | safely shutdown the plant. Therefore with only two operable Diesel | | Generators, the condition requires an 8 hr ENS notification in accordance | | with 10CFR50.72(b)(3)(v) and (vi)." | | | | With Unit 1 shutdown the 'A' RHR pump is not needed, but the 'C' ESW pump | | does need to be operable resulting in part of the 8 hour report. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * RETRACTED ON 04/08/2002 AT 1433 EDT BY GRANT FERNSLER TO GERRY WAIG * | | * * | | | | "On 3/31/2002, Susquehanna LLC made an ENS notification per | | 10CFR50.72(b)(3)(v) and (vi). The event was the result of two load sequence | | timers for separate diesel generators found outside of the allowable values. | | The associated diesel generators were declared inoperable. | | | | "Upon subsequent engineering review, it was determined that although the | | timers were not within the design specifications all equipment would have | | been able to perform its safety function, as evidenced by the emergency | | generators maintaining voltage and frequency, and the loads energizing and | | running during the testing. Additionally, the requirements of the Technical | | Specification Actions were followed for all inoperable equipment. | | | | With all equipment remaining capable of performing its design function, this | | ENS Notification EN#38818 is retracted." | | | | "The NRC Resident Inspector was notified by the licensee. | | | | The R1DO (Bradley Fewell) was notified by the Headquarters Operations | | Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38839 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 04/08/2002| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 11:03[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 04/08/2002| +------------------------------------------------+EVENT TIME: 03:00[CDT]| | NRC NOTIFIED BY: WILLIAM GREEN |LAST UPDATE DATE: 04/08/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BILL JONES R4 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF EMERGENCY PREPAREDNESS CAPABILITIES | | | | "At 0300 one of the two belts on the Emergency Outside AIR Fan (OAF-2) for | | the Technical Support Center (TSC) / Operations Support Center (OSC) was | | found broken. The other fan belt appeared to be degrading rapidly. The fan | | was taken out of service. OAF-2 provides outside air to the TSC / OSC that | | is filtered. Unavailability of this fan could prevent the use of the TSC / | | OSC in the event of a radiological release. | | | | "Station Procedure 5.7.7, activation of the TSC section 4, Evacuation of the | | TSC, provides guidance for the evacuation of the TSC and the relocation of | | TSC personnel. Station Procedure 5.7.8.1, Activation of the Alternate OSC, | | provides guidance for the evacuation of the OSC and the relocation of OSC | | personnel. In the event of an emergency that requires activation of the TSC | | / OSC, the TSC / OSC will be activated and atmospheric monitoring will be | | performed in accordance with existing station procedures. If conditions | | require the evacuation of the TSC / OSC, TSC / OSC personnel will be | | relocated in accordance with existing station procedures. | | | | "Currently repairs to replace the belts on OAF-2 are underway. OAF-2 should | | be returned to service today." | | | | The NRC Resident Inspector has been notified. | | | | * * * UPDATED ON 03/08/02 AT 1542 EDT BY WILLIAM GREEN TO GERRY WAIG * * * | | | | "At 1340 CDT OAF-2 was returned to service after a replacement of the | | damaged belts. The fan has been inspected by Maintenance and determined to | | be operating properly. Damage to belts appears to be from normal wear." | | | | The NRC Resident Inspector was notified by the licensee. | | | | R4DO (Kriss Kennedy) was notified by the Headquarters Operations Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38840 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/08/2002| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:13[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/08/2002| +------------------------------------------------+EVENT TIME: 10:52[EDT]| | NRC NOTIFIED BY: MIKE MICKLOW |LAST UPDATE DATE: 04/08/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |J. BRADLEY FEWELL R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNSUCCESSFUL TEST OF THE SIREN SILENT TEST | | | | "During the siren silent test performed on 4-08-02 at the Cobbs Hill | | location, all sirens indicated failure to reply. A subsequent test was | | performed from the Monroe County 911 center. All sirens indicated failure to | | reply. A single activation test on siren #1 in Monroe County was performed. | | The siren did not receive a signal to activate. Continuous radio traffic was | | detected on the siren radio frequency. This prevented a signal from being | | received by the sirens. Wayne and Monroe County were notified to utilize | | route-alerting procedures in the event that notification to the public was | | necessary. A technician was dispatched with a radio signal detection | | instrument to determine the source of the radio traffic on thc siren | | frequency. Siren #22 in Monroe County was found to have a strong continuous | | active radio signal. Siren #22 was de-energized and the continuous radio | | signal stopped. Siren #22 is quarantined as part of a root cause | | investigation. Follow up testing is planned." | | | | The NRC Resident Inspector was notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38841 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MAINE YANKEE REGION: 1 |NOTIFICATION DATE: 04/08/2002| | UNIT: [1] [] [] STATE: ME |NOTIFICATION TIME: 18:15[EDT]| | RXTYPE: [1] CE |EVENT DATE: 04/08/2002| +------------------------------------------------+EVENT TIME: 15:15[EDT]| | NRC NOTIFIED BY: TERRY WHITE |LAST UPDATE DATE: 04/08/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |J. BRADLEY FEWELL R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION OF FATALITY | | | | At 1300 EDT on 4/8/2002 a contract worker was transported from the site by | | ambulance to Mid Coast Hospital in Brunswick, Maine. Prior to being | | transported, the worker was treated by onsite EMT and other medical | | personnel. The worker was not working in a radioactive contaminated area and | | was not contaminated at the time of the event. The licensee later learned | | that the worker died of an apparent heart attack. The licensee safety | | department reported the death to OSHA at 1515 EDT. | | | | The licensee reported that R1 (Randy Ragland) has been notified of the | | event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38842 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 04/08/2002| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 20:55[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 04/08/2002| +------------------------------------------------+EVENT TIME: 19:07[EDT]| | NRC NOTIFIED BY: ROBERT THOMAS |LAST UPDATE DATE: 04/08/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |J. BRADLEY FEWELL R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION OF MINOR OIL SPILL | | | | "IAW [In Accordance With] AP-09.03, Oil Spill Prevention Control and | | Countermeasures Plan, reported to NYSDEC and USCG National Response Ctr [an] | | oil spill in which oil and lubricant [less than 1 gallon] washed off a road | | sander during rain showers entered storm drain. Slight sheen observed at | | outfall for storm drains to Lake Ontario." | | | | The NRC Resident will be notified of the event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021