Event Notification Report for March 5, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/04/2002 - 03/05/2002 ** EVENT NUMBERS ** 38477 38704 38748 38749 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38477 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 11/07/2001| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 19:47[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/07/2001| +------------------------------------------------+EVENT TIME: 14:14[EST]| | NRC NOTIFIED BY: DANIEL G. MALONE |LAST UPDATE DATE: 03/04/2002| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |R3 IRC TEAM MANAGER R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HEAD LOSS CHARACTERISTICS OF CHECK VALVES GREATER THAN PREVIOUSLY ASSUMED. | | | | On November 7, 2001, at approximately 1414 hours, with the plant in mode 5 | | (cold shutdown), evaluation of preliminary results from mock-up testing of | | containment sump check valves determined that the head loss characteristics | | of the check valves are greater than previously assumed by calculations that | | support the safety analyses. The result of increased head loss through the | | containment sump check valves is reduced available net positive suction head | | (NPSH) for the safety injection and containment spray pumps during | | recirculation mode following a loss of coolant accident (LOCA). The reduced | | available NPSH may have effected the ability of the pumps to satisfy their | | required design safety function during previous periods of plant operation. | | Recirculation mode operation of these pumps is required by Technical | | Specifications in Mode 3 (hot standby) and above. Therefore, this condition | | has no adverse implications for the present plant condition at Mode 5. | | Evaluation of test results is continuing. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * RETRACTED AT 1450 EST ON 03/04/02 BY DAN MALONE TO GERRY WAIG* * * | | | | "Subsequent evaluation of the past operability of the pumps with the reduced | | NPSH condition was concluded that the pumps were nonconforming but operable. | | This conclusion was reached by crediting containment overpressure and actual | | plant parameters, which increase available NPSH above that required for all | | pumps considering the most limiting postulated conditions. | | | | "Since a determination of nonconforming but operable was reached for past | | operating conditions, there was no loss of a required safety function and no | | significant impact on plant safety this condition was originally discovered | | and reported with the plant in Mode 5; and was corrected prior to plant | | restart by modifying plant equipment and procedures without further reliance | | on crediting containment overpressure." | | | | Licensee notified the NRC Resident Inspector. Notified R3DO (John Madera). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38704 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/16/2002| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 11:11[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/15/2002| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 22:00[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/04/2002| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |ANTON VEGEL R3 | | DOCKET: 0707001 |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEVIN BEASLEY | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY EQUIPMENT FAILURE - PROCESS GAS LEAK DETECTION FAILURE | | | | "At 2200 CST, on 02-15-02 the Plant Shift Superintendent (PSS) was notified | | of a failure of the Process Gas Leak Detector (PGLD) system in the C-333 | | building. During above atmospheric operation a PGLD alarm was received in | | the Area Control Room [ACR] on C-333 Unit 4 Cell 4. An operator responded | | to the local cell panel to investigate according to the alarm response | | procedure. Upon arriving at the cell panel the operator discovered that the | | Ready light was not Illuminated on the PGLD panel. At this time the | | operator attempted to test fire the PGLD system, however the system would | | not respond. The Front Line Mgr. and the PSS were immediately notified of | | the system failure. At this time, required TSR 2.4.4.1 LCO continuous smoke | | watches were put in place in the affected areas until repair of the system | | was completed. Following replacement of the power supply by Instrument | | Maintenance and testing by Operations, ten Unit 4 Cell 4 PGLD system was | | declared operable by the PSS at 2340 CST. At this time the TSR required | | smoke watches were discontinued. | | | | "The PGLD system is designed to detect the leakage of process gas from the | | process system and is required to be operable while operating in Cascade | | Mode 2 (Above Atmospheric Pressure). Due to the failure of this TSR | | required system; the PSS has determined that this is reportable as a 24 hour | | Event Report. | | | | "The NRC Resident inspector has been notified of this event." | | | | * * * RETRACTED AT 0346 EST ON 02/22/02 BY ERIC WALKER TO FANGIE JONES * * * | | | | | | "This event has been retracted. Even though the power loss causes the system | | to be incapable of annunciating additional alarms from this system in the | | ACR, the same is true when a PGLD head actuates in response to smoke. The | | system Is designed to alert operators of a release or loss of system power. | | Operator response and the initiation of a smoke watch provide the safety | | function after the initial alarm is annunciated. The NRC resident inspector | | has been notified of this update." | | | | The R3DO (Bruce Jorgensen) and NMSS EO (E. William Brach) have been | | notified. | | | | * * * UPDATED AT 1750 EST ON 3/4/02 BY TOM WHITE TO FANGIE JONES * * * | | | | "Following discussions with NRC Region III and the PGDP NRC Senior Resident | | Inspector. USEC has determined that a rescission of the retraction made on | | 2/21/02 will be necessary in response to NRC concerns related to this | | matter. Therefore, USEC hereby rescinds the subject retraction and will be | | submitting the written report required by 10CFR76.120(d)(2). The NRC Senior | | Resident Inspector has been notified of the rescission." | | | | Notified the R3DO (John Madera) and NMSS EO (C. W. Reamer). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38748 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 03/04/2002| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 10:13[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/04/2002| +------------------------------------------------+EVENT TIME: 08:41[EST]| | NRC NOTIFIED BY: PHILLIP THOMPSON |LAST UPDATE DATE: 03/04/2002| | HQ OPS OFFICER: MIKE NORRIS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO LOSS OF FEEDWATER | | | | "Manual reactor trip due to falling level in 1A Steam Generator (S/G), (RPS | | Activation). Level decrease occurred after the Feedwater Regulating Valve | | (FRV) for the 1A S/G failed closed upon loss of the normal and backup | | electrical power to the valve solenoid. After the reactor trip, the 1A S/G | | experienced a LO-LO Level Alarm which auto started both motor driven | | Auxiliary Feedwater pumps, (ESF Actuation). All S/G levels are now at | | normal levels and Unit 1 is stable. An investigation is in progress to | | determine the loss of electrical power to the FRV solenoid for the 1A S/G." | | | | The plant is dumping steam to the Main Condenser with no known | | Primary/Secondary leakage. There was no actuation of primary safety valves. | | All safety systems are operable and normal electrical distribution is | | available. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38749 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 03/04/2002| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 11:37[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 03/04/2002| +------------------------------------------------+EVENT TIME: [CST]| | NRC NOTIFIED BY: RICK ROBBINS |LAST UPDATE DATE: 03/04/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |JOHN MADERA R3 | |10 CFR SECTION: |CHRIS GRIMES EO | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |RICHARD WESSMAN IRO | | |JEFF GRANT R3 | | |REGION V OSC EPA | | |BELCHER FEMA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DUE TO UNCONTROLLED FLAMMABLE GAS LEAK ONSITE | | | | At 0946 CST, 3/4/02, an Unusual Event was declared due to a non isolable | | leak on a propane tank. The tank is approximately 500 to 750 gals, and is | | 55 % full. The tank is leaking at the rate of 5% decrease every 20 minutes. | | The tank is 25 to 30 yards out in the Owner Controlled Area and a local | | area evacuation has been performed. The Two Creek Fire Department is on the | | scene. | | | | NRC Resident Inspector has been notified. | | | | At 1147 EST, NRC entered Monitoring for Normal Phase Mode. | | | | ***EVENT UPDATED AT 1309 EST ON 3/4/02 BY MARK HANSON TO FANGIE JONES*** | | | | At 1154 CST, Licensee terminated Unusual Event due to leak isolated. | | | | At 1310 EST, NRC exited monitoring for the Unusual Event. | | | | Notified IRO (Holonich), R3DO (Madera), NRR (Grimes), PAO (Dricks), FEMA | | (Snyder). | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021