Event Notification Report for February 11, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/08/2002 - 02/11/2002 ** EVENT NUMBERS ** 38676 38679 38683 38684 38685 38686 38687 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! Power Reactor Event Number: 38676 - FACILITY: LIMERICK REGION: 1 NOTIFICATION DATE: 02/06/2002 UNIT: [1] [] [] STATE: PA NOTIFICATION TIME: 22:37[EST] RXTYPE: [1] GE-4,[2] GE-4 EVENT DATE: 02/06/2002 NRC NOTIFIED BY: PETE ORPHANOS LAST UPDATE DATE: 02/08/2002 EMERGENCY CLASS: NON EMERGENCY LAWRENCE DOERFLEIN R1 10 CFR SECTION: AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION UNIT SCRAM CODERX CRITINIT PWR INIT RX MODE CURR PWR CURR RX MODE 1 N Y 94 Power Operation 94 Power Operation EVENT TEXT HPCI DECLARED INOPERABLE "During the completion of scheduled testing on the Unit 1 High Pressure Coolant injection (HPCI) system, a valve designed to provide minimum flow protection for the associated pump did not automatically open in the time frame expected during pump shutdown. The valve did respond correctly to Operator action. "HPCI was declared inoperable as of 1722 hours on February 6th, 2002. Troubleshooting on the minimum flow protection circuitry is currently in progress. "This report is being made in pursuant to 10CFR50.72(b)(3)(V)(D) for failure of a single train accident mitigation system." The NRC resident inspector has been informed of this event by the licensee. * * * UPDATE 1508EST ON 2/8/02 FROM STAN GAMBLE TO S. SANDIN * * * The licensee is retracting this report based on the following: "This is a retraction of the event notification made on 2/6/02 at 22:37 hours. This event (#38676) was initially reported as a safety system functional failure under the requirement of 10CFR50.72(b)(3)(v)(D), after the Unit 1 High Pressure Coolant Injection (HPCI) minimum flow valve did not automatically open during system testing. "Subsequent testing verified that the valve would have opened automatically without operator action following the low flow alarm actuation. A delay in response is expected when system flow is reduced to a value within the range of the flow transmitter. This delay in response, and the short duration of pump operation at a no flow condition is not detrimental to the HPCI pump. "The system response was verified to be as designed considering the test conditions. A condition did not exist at the time of discovery that could have prevented the fulfillment of the safety function." The licensee informed the NRC Resident Inspector. Notified R1DO(Doerflein). !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! Power Reactor Event Number: 38679 - FACILITY: FITZPATRICK REGION: 1 NOTIFICATION DATE: 02/07/2002 UNIT: [1] [] [] STATE: NY NOTIFICATION TIME: 14:26[EST] RXTYPE: [1] GE-4 EVENT DATE: 02/07/2002 NRC NOTIFIED BY: SHAWN ALLEN LAST UPDATE DATE: 02/08/2002 EMERGENCY CLASS: NON EMERGENCY LAWRENCE DOERFLEIN R1 10 CFR SECTION: AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION UNIT SCRAM CODERX CRITINIT PWR INIT RX MODE CURR PWR CURR RX MODE 1 N Y 100 Power Operation 100 Power Operation EVENT TEXT HPCI DECLARED INOPERABLE FOLLOWING DISCOVERY OF UNKNOWN CONTAMINANT IN OIL "Declared High Pressure Coolant Injection System (HPCI) INOP due to unknown contaminants in the oil system. Plant formulated an action plan to resample the sump, identify the particles, and identify the source of the contaminants. Entered 7 day LCO per Tech Spec 3.5.C.1.a." The licensee informed the NRC Resident Inspector. * * * UPDATE 1620EST ON 2/8/02 FROM ANDY HALLIDAY TO S. SANDIN * * * The licensee is retracting this report based on the following: "Further analysis has shown that the foreign material found in the HPCI lube oil sample taken 2/7/2002 did not cause HPCI to become inoperable, it could have performed its design function before, during and after the time it was declared inoperable. "This is based on determination through engineering review that the type and size of material found in the sample would not have prevented any part of HPCI from failing to operate as required. "Preliminary cause determination is that 4 liters of unfiltered oil were added to the 150 gallon lube oil system during the previous monthly sample evolution. "For these reasons. JAF is concluding that HPCI remained operable from the original LCO entry of 12:15; 2/7/02. and is retracting notification #38679." The licensee informed the NRC Resident Inspector. Notified R1DO(Doerflein). General Information or Other Event Number: 38683 - REP ORG: OHIO BUREAU OF RADIATION PROTECTION NOTIFICATION DATE: 02/08/2002 LICENSEE: BATTELLE MEMORIAL INSTITUTE NOTIFICATION TIME: 13:43[EST] CITY: COLUMBUS REGION: 3 EVENT DATE: 01/29/2002 COUNTY: STATE: OH EVENT TIME: [EST] LICENSE#: OH03610250000 AGREEMENT: Y LAST UPDATE DATE: 02/08/2002 DOCKET: PERSON ORGANIZATION THOMAS KOZAK R3 FRED BROWN NMSS NRC NOTIFIED BY: MICHAEL SNEE HQ OPS OFFICER: JOHN MacKINNON EMERGENCY CLASS: NON EMERGENCY 10 CFR SECTION: NAGR AGREEMENT STATE EVENT TEXT AGREEMENT STATE EVENT The licensee reported the loss of a internally contaminated duct. The duct is 13-feet long and 4-inches in diameter and contaminated with U-234, U-235, and U-238, with the highest concentration being U-234. The licensee estimates that 1.5 microcuries of U-234 is in the duct. The duct was sent to a construction debris landfill in Franklin County, Ohio along with other construction debris. Source/Material: Unsealed Material, Other Radionuclide: U-234 Activity (Curies): 0.0000015 Agreement State Item number: OH-02-021 General Information or Other Event Number: 38684 - REP ORG: MARYLAND DEPT OF THE ENVIRONMENT NOTIFICATION DATE: 02/08/2002 LICENSEE: HOLY CROSS HOSPITAL NOTIFICATION TIME: 15:36[EST] CITY: SILVER SPRINGS REGION: 1 EVENT DATE: 02/04/2002 COUNTY: MONTGOMERY STATE: MD EVENT TIME: 15:00[EST] LICENSE#: MD-31-001-01 AGREEMENT: Y LAST UPDATE DATE: 02/08/2002 DOCKET: PERSON ORGANIZATION LAWRENCE DOERFLEIN R1 PAUL FREDRICKSON R2 NRC NOTIFIED BY: RAY MANLEY HQ OPS OFFICER: STEVE SANDIN EMERGENCY CLASS: NON EMERGENCY 10 CFR SECTION: NAGR AGREEMENT STATE EVENT TEXT AGREEMENT STATE REPORT INVOLVING POTENTIAL PERSONNEL EXPOSURES On 2/4/02 at 1500EST a female patient undergoing treatment for thyroid cancer received 250 millicuries I-131 at the Holy Cross Hospital located at 1500 Forest Glen Road in Silver Springs, MD 20910. The patient subsequently expired on 2/5/02 at 0630EST. The body was released by the hospital to the Metropolitan Funeral Home located at 5517 Vine Street in Alexandria, VA for cremation. Due to the relatively short period of time between administration of the I-131 dose and the patient's demise radiation levels were measured 67 mR/hr @ 1 meter. The decedent was transferred back to Holy Cross Hospital and is in an area away from the general public awaiting final disposition. Both NRC Region I (Duncan White) and NRC Region II are aware of this event. Contamination surveys were performed at the Funeral Home with negative results. An investigation is ongoing to determine any personnel exposures associated with this incident. Other Nuclear Material Event Number: 38685 - REP ORG: BRIGHAM YOUNG UNIVERSITY NOTIFICATION DATE: 02/08/2002 LICENSEE: BRIGHAM YOUNG UNIVERSITY NOTIFICATION TIME: 16:15[EST] CITY: LAIE REGION: 4 EVENT DATE: 01/01/2002 COUNTY: HONOLUL STATE: HI EVENT TIME: [HST] LICENSE#: AGREEMENT: N LAST UPDATE DATE: 02/08/2002 DOCKET: PERSON ORGANIZATION JOHN PELLET R4 M. WAYNE HODGES NMSS NRC NOTIFIED BY: JIM FREEMAN HQ OPS OFFICER: STEVE SANDIN EMERGENCY CLASS: NON EMERGENCY 10 CFR SECTION: BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X EVENT TEXT SELF-POWERED TRITIUM EXIT SIGNS DISCOVERED MISSING FOLLOWING FACILITY RENOVATION The auditorium at the Brigham Young University Campus in Laie, HI underwent renovation between 6/2000 and 1/2002. The contractor removed nine (9) self-powered tritium exit signs for storage and reinstallation following completion of the work. After work was completed the signs could not be located. The Safety Officer (SO) at the University believes that the signs may have been installed at another business location. Based on other self-powered exit signs currently in possession, the SO feels the missing signs contained 10 Curie tritium sources each and were manufactured by SRB Technologies, Inc. located in Winston-Salem, NC between 1992 and 1993. A written report will be submitted for the loss of this general licensed material in accordance with NUREG-1556. Power Reactor Event Number: 38686 - FACILITY: HATCH REGION: 2 NOTIFICATION DATE: 02/09/2002 UNIT: [1] [] [] STATE: GA NOTIFICATION TIME: 00:30[EST] RXTYPE: [1] GE-4,[2] GE-4 EVENT DATE: 02/08/2002 NRC NOTIFIED BY: ED BURKETT LAST UPDATE DATE: 02/09/2002 EMERGENCY CLASS: NON EMERGENCY PAUL FREDRICKSON R2 10 CFR SECTION: ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA UNIT SCRAM CODERX CRITINIT PWR INIT RX MODE CURR PWR CURR RX MODE 1 M/R Y 27 Power Operation 0 Hot Shutdown EVENT TEXT MANUAL REACTOR SCRAM - DEGRADED VACUUM DUE TO ACTIONS FOR HIGH OFFGAS HYDROGEN "Plant Hatch Unit 1 was SCRAMMED at 2252 EST on 02-08-2002. The Reactor was SCRAMMED from approximately 27% RTP and the Main Turbine subsequently tripped. Degraded function of the Main Condenser Offgas Recombiner system had resulted in high Hydrogen in the Offgas. The 'Failure of Recombiner' Abnormal Operating procedure (AOP) had been entered at approximately 2100 and a power reduction begun from 100% RTP at about 2105. Per the AOP, the inservice Steam jet Air Ejector was removed from service at 2220 (due to the Offgas Hydrogen concentration reaching approximately 4%). Hatch Unit 1 was subsequently scrammed due to degrading Condenser Vacuum. The mechanical vacuum pump was placed in service after the SCRAM to maintain Condenser Vacuum as the heat sink. The lowest Reactor Water Level noted during the SCRAM (approximately 7" above Instrument zero) was above any ESF actuation settings, so no ESFs were required or received. No Reactor Pressure increase was noted during the SCRAM. At this time plans are to proceed to Cold Shutdown for repairs to the Offgas Recombiner system and other maintenance. Air purge had been placed inservice to purge the Hydrogen from the Offgas system at around 2230, and remains inservice to reduce Hydrogen concentrations." The licensee notified the NRC Resident Inspector. Power Reactor Event Number: 38687 FACILITY: DIABLO CANYON REGION: 4 NOTIFICATION DATE: 02/09/2002 UNIT: [] [2] [] STATE: CA NOTIFICATION TIME: 10:09[EST] RXTYPE: [1] W-4-LP,[2] W-4-LP EVENT DATE: 02/09/2002 NRC NOTIFIED BY: DOUGLAS DYE LAST UPDATE DATE: 02/09/2002 EMERGENCY CLASS: NON EMERGENCY JOHN PELLET R4 10 CFR SECTION: ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT UNIT SCRAM CODERX CRITINIT PWR INIT RX MODE CURR PWR CURR RX MODE 2 M/R Y 100 Power Operation 0 Hot Standby EVENT TEXT MANUAL REACTOR TRIP DUE TO LOSS OF FEEDWATER TO A STEAM GENERATOR "At 0337, on 2/9/2002, Unit 2 reactor was manually tripped due to a failure of feedwater regulating valve FW-2-FCV-540. The valve failed closed isolating feedwater to steam generator 2-4. The reason for the failure is currently unknown, investigation continues. All safety systems responded as required. [All control rods fully inserted]. Auxiliary feedwater pumps 2-1, 2-2, 2-3 started as required in response to low steam generator water levels. "DCPP unit 2 is stable in Mode 3, heat removal is via steam dumping to the normal condenser, auxiliary feedwater continues to supply the steam generators." The unit will remain in Mode 3 until repairs are made. The unit 2 steam generator 4 has had a long term tube leak (about 2 years) on the order of about 3.82 gpd (TS limit 150 gpd) by most recent calculation. Secondary activity is less than detectable and only a count rate on steam jet air ejector is positive indication. Primary activity pretrip was 3.47E-3 �Ci/ml. The licensee notified the NRC Resident Inspector and will make a normal press release.
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021