The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for January 10, 2002

                         
                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           01/09/2002 - 01/10/2002

                              ** EVENT NUMBERS **

38602  38620  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38602       |
+------------------------------------------------------------------------------+
                         
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER            REGION:  2  |NOTIFICATION DATE: 01/01/2002|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 10:08[EST]|
|   RXTYPE: [3] B&W-L-LP                         |EVENT DATE:        01/01/2002|
+------------------------------------------------+EVENT TIME:        09:19[EST]|
| NRC NOTIFIED BY:  BILL BANDHAUER               |LAST UPDATE DATE:  01/09/2002|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |ANNE BOLAND          R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE  
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE RESCUED SEA TURTLE                                  |
|                                                                              |
| EN #37902 started the biennial report period.                                |
|                                                                              |
| On January 1, 2002 at 0919, a rescued sea turtle was identified as a green   |
| sea turtle.  This is the 62nd rescue of a live sea turtle at Crystal River   |
| Unit 3 (CR-3) in this biennial period. Notification to the National Marine   |
| Fisheries Service and the Florida Fish and Wildlife Conservation Commission. |
|                                                                              |
|                                                                              |
| The licensee intends to notify the NRC Resident Inspector.                   |
|                                                                              |
| * * *  UPDATE ON 1/05/02 @ 1002 BY RAWLS TO GOULD  * * *                     |
|                                                                              |
| On January 5, 2002, at 0720, a rescued sea turtle was identified as a        |
| Loggerhead Sea Turtle. This is the 63rd rescue of a live sea turtle at       |
| Crystal River Unit 3 (CR3) in this biennial period.  This is reportable as a |
| 4-hour report under 10 CFR 50.72(b)(2)(xi) as this event is related to the   |
| protection of the environment for which a notification to other government   |
| agencies (National Marine Fisheries Service and Florida Fish and Wildlife    |
| Conservation Commission) has been or will be made.                           |
|                                                                              |
| The NRC Resident Inspector was notified.                                     |
|                                                                              |
| Reg 2 RDO (Decker) was notified.                                             |
|                                                                              |
| * * * UPDATE ON 01/09/02 @ 1107 EST BY ANDY BARNES TAKEN BY MACKINNON * * *  |
|                                                                              |
| On January 9, 2002, at 0838, a rescued sea turtle was identified as a Kemp's |
| Ridley Sea Turtle. This is the 64th rescue of a live turtle at Crystal River |
| Unit 3 (CR-3) in this biennial period. This is reportable as a 4-hour 10     |
| CFR50.72 (b)(2)(xi) as this event is related to the protection of the        |
| environment for which a notification to other government agencies (National  |
| Marine Fisheries Service and Florida Fish and Wildlife Conservation          |
| Commission) has been or will be made.                                        |
|                                                                              |
| The NRC Resident Inspector was notified.                                     |
|                                                                              |
| Reg 2 (Brian Bonser) was notified.                                           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38620       |
+------------------------------------------------------------------------------+
                         
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: QUAD CITIES              REGION:  3  |NOTIFICATION DATE: 01/09/2002|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 18:08[EST]|
|   RXTYPE: [1] GE-3,[2] GE-3                    |EVENT DATE:        01/09/2002|
+------------------------------------------------+EVENT TIME:        14:12[CST]|
| NRC NOTIFIED BY:  KEN HILL                     |LAST UPDATE DATE:  01/09/2002|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |CHRISTOPHER GRIMES   NRR     |
|ASHU 50.72(b)(2)(i)      PLANT S/D REQD BY TS   |RICHARD WESSMAN      IRO     |
|AIND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE  
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |15       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TECHNICAL SPECIFICATION REQUIRED SHUTDOWN DUE TO POTENTIAL JET PUMP
FAILURE  |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "At 1412 [CST], Unit 1 experienced indication of Jet Pump #19/20 failure     |
| based on the following plant indications:                                    |
| a)  Gross Megawatt Electric decrease[,]                                      |
| b)  Reactor Pressure decrease[,]                                             |
| c)  Total Core Flow Indication increase[, and]                               |
| d)  Core Plate dP decrease[.]"                                               |
|                                                                              |
| "At 1442 [CST], the 1B Recirculation Pump tripped - the cause of this trip   |
| is unknown at this time.  Based on indication of Jet Pump [#]19/20 failure,  |
| the plant entered Tech Spec 3.4.2, Condition A, at 1521 [CST], requiring the |
| unit to be placed in Mode 3 within 12 hours.  A plant shutdown is in         |
| progress.  No other related surveillances were in progress at the time.  All |
| other equipment is operating as expected with all ECCS equipment available   |
| on Unit 1."                                                                  |
|                                                                              |
| "Unit 1 has been operating with a minor fuel leak, which has been            |
| suppressed, since December 22, 2001.  Steam line radiation levels increased  |
| and subsequently decreased, and the SJAE Radiation Monitors show a minor     |
| spike and return to near pre-event values.  Main Chimney Radiation Monitors  |
| show no change in station effluent release rate to the environment.  No      |
| estimate of return to service for the unit is available at this time."       |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Wednesday, March 24, 2021