Event Notification Report for December 27, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/26/2001 - 12/27/2001 ** EVENT NUMBERS ** 38593 38594 38595 38596 . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38593 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 12/26/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 08:52[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 12/26/2001| +------------------------------------------------+EVENT TIME: 07:20[EST]| | NRC NOTIFIED BY: RUH |LAST UPDATE DATE: 12/26/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MICHELE EVANS R1 | |10 CFR SECTION: |VICTOR DRICKS PAO | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|JOSEPH HOLONICH IRO | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP FROM 100% POWER DUE TO TURBINE TRIP | | | | The plant had an auto stop oil pressure trip on the main turbine followed by | | a reactor trip from 100% power. The plant went into natural circulation for | | 1 hour at which time the #24 reactor coolant pump was put in service. | | Auxiliary feedwater was placed in service. Partial offsite power was lost | | and the three EDG's auto started and powered buses "2A" and "3A". The cause | | of the trip is being investigated. All rods fully inserted, no ECCS was | | initiated and no safety relief valves lifted, however, the atmospheric dump | | valves were opened to vent steam from the system. The plant is stable and | | in hot shutdown. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38594 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CBC ENGINEERS AND ASSOCIATES |NOTIFICATION DATE: 12/26/2001| |LICENSEE: CBC ENGINEERS AND ASSOCIATES |NOTIFICATION TIME: 11:52[EST]| | CITY: WHITESVILLE REGION: 2 |EVENT DATE: 12/26/2001| | COUNTY: STATE: WV |EVENT TIME: [EST]| |LICENSE#: 34-26768-02 AGREEMENT: N |LAST UPDATE DATE: 12/26/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE BOLAND R2 | | |BRENT CLAYTON R3 | +------------------------------------------------+FRED BROWN NMSS | | NRC NOTIFIED BY: BANNER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TROXLER GAUGE STOLEN FROM CBC ENGINEERS AND ASSOCIATES OF DAYTON, OHIO | | | | A Troxler gauge model #3430 serial # 29017 which was locked in a truck was | | stolen along with the truck from the driver's residence in Whitesville, West | | Virginia. The gauge contained 8 mCi of Cs-137 and 40 mCi of Am-241/Be. The | | W Va State Police were notified and the licensee will contact the local fire | | department along with the media to offer a reward. | | | | * * * UPDATE ON 12/26/01 @ 1237 BY BANNER TO GOULD * * * | | | | The vehicle was found in West Virginia with Troxler gauge intact. | | | | Notified Reg 2 (Boland), Reg 3 (Clayton) and NMSS (Brown) | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38595 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 12/26/2001| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 14:10[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/26/2001| +------------------------------------------------+EVENT TIME: 10:16[EST]| | NRC NOTIFIED BY: JIM SETLIFFE |LAST UPDATE DATE: 12/26/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE BOLAND R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT EMPLOYEE TESTED POSITIVE FOR ILLEGAL DRUGS | | | | An electrical licensee tested positive for marijuana during a random drug | | test. The employee's access to the plant has been pulled and his past work | | is being reviewed. | | | | Call the Headquarters Operation Officer for further details. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38596 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/26/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 15:39[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/21/2001| +------------------------------------------------+EVENT TIME: 20:25[EST]| | NRC NOTIFIED BY: VEITCH |LAST UPDATE DATE: 12/26/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRENT CLAYTON R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 85 Power Operation |85 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INDETERMINATE IF HIGH PRESSURE CORE SPRAY (HPCS) EMERGENCY DIESEL GENERATOR | | (DG) COULD FULFILL ITS REQUIRED SAFETY FUNCTION. | | | | "On 12/21/01, Condition Report 01-4350 was initiated to document the failure | | of Div . 3 DG to pass SVI-E22-T1319. Specifically, the DG did not come up to | | frequency/voltage within the required 13 seconds (TS 3.8.1.7.b.2). The DG | | was declared inoperable and an immediate investigation was requested. The | | immediate investigation indicated that the cause of the SVI failure was due | | to the DG governor control switch not being properly set during shutdown on | | the DG on 12/16/01. In analyzing the shutdown data from the 12/21/01 DG | | surveillance testing, it was determined that the situation had been | | corrected, and that the next DG start, the DG would satisfy the TS SR. The | | DG was started on 12/22/01 and satisfied the SR. The DG was then declared | | operable. | | | | "During this time, it is indeterminate if the HPCS DG could fulfill its | | required safety function. The immediate investigation infers that an | | operator error occurred when shutting down the DG on 12/16/01. This error, | | the mis-operation of the DG governor control switch, prevented the DG from | | properly coming up to the required frequency/voltage within 13 seconds as | | identified on 12/21/01. Hence, it is conservative to assume that the | | capability to perform the safety function was not maintained. This | | condition is an 8-hour report pursuant to 50.72(b)(3)(v) and (vi). It | | should be noted that HPCS is a single train system and there are no | | redundant features within the same system to perform the safety function." | | | | The NRC resident inspector will be notified of this event by the licensee. | +------------------------------------------------------------------------------+ .
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