Event Notification Report for December 19, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/18/2001 - 12/19/2001 ** EVENT NUMBERS ** 38424 38580 38581 . !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38424 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 10/24/2001| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 19:09[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 10/24/2001| +------------------------------------------------+EVENT TIME: 16:25[CDT]| | NRC NOTIFIED BY: RODE |LAST UPDATE DATE: 12/18/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRENT CLAYTON R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 63 Power Operation |63 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PROCEDURE USED FOR INSTALLATION OF TEMPORARY FIRE SEALS WAS NOT IN | | COMPLIANCE WITH THE CALCULATION QUALIFYING THE TEMPORARY FIRE SEALS | | | | During an internal review of the fire protection program at Point Beach | | Nuclear Power Plant, it was determined that the procedure used for the | | installation of temporary fire seals was not in compliance with the | | calculation qualifying the temporary fire seals. The procedure called for 4 | | inches of Kaowool while the calculation demonstrated the 5 inches would | | ensure adequate fire protection. | | | | Out of the 9 barriers that were identified, 4 of them are required to | | provide train separation for safe shut down equipment. Due to the identified | | condition, these penetrations may not have adequately provided such | | separation as required by our safe shutdown analysis. | | | | Immediate actions taken included: 1) Affected penetrations were identified | | and declared out of service. 2) Appropriate fire rounds were commenced. 3) | | Installed the required 5 inches of Kaowool in the identified barriers and | | returned the barriers back to service. | | | | Pending corrective actions: Although the calculation determined 5 inches of | | Kaowool provides an adequate fire barrier, engineering will perform an | | additional evaluation to determine if 4 inches of Kaowool would suffice. | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATE 1409EST ON 12/18/2001 FROM RYAN RODE TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | "Subsequent to this notification our Engineering Staff has prepared and | | approved, a Fire Protection Engineering Evaluation (FPEE 2001-003) of the | | as-found condition for these temporary fire seals following the guidelines | | of Generic Letter 86-10. This analysis demonstrates that a 4 inch temporary | | penetration seal constructed of 8 pounds per cubic feet ceramic fiber | | material satisfies the time function of a 3 hour rated seal by preventing | | fire propagation across the barrier. Accordingly, we have concluded that | | the presence of temporary fire seals with 4 inches of seal material did not | | significantly compromise plant safety with respect to separation of the safe | | shutdown equipment and this event notification should be retracted. | | | | The licensee informed the NRC Resident Inspector. Notified R3DO(Phillips). | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38580 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HONEYWELL INTERNATIONAL, INC. |NOTIFICATION DATE: 12/18/2001| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 09:13[EST]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 12/17/2001| | |EVENT TIME: 12:05[CST]| | |LAST UPDATE DATE: 12/18/2001| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |MONTE PHILLIPS R3 | | DOCKET: 04003392 |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HUGH ROBERTS | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |JBBE 40.60(b)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF THE STANDBY GENERATOR TO START ON AUTOMATIC DUE TO A PARTIAL | | POWER OUTAGE AND RELAY FAILURE | | | | Moisture in a substation resulted in a partial power outage, and a faulty | | relay resulted in a failure to switch over to an automatic start on the | | standby generator. The failure of the standby generator to start on | | automatic occurred at 1205 CST on 12/17/01. The facility was shut down | | until the generator was restored and the relay was fixed. The system was | | restored to service at approximately 1930 CST on 12/17/01. | | | | The licensee reported that there was no loss of source material related to | | this event. In addition, there were no personnel radiation exposures or | | contaminations. | | | | The licensee reported this event in accordance with 10CFR40.60(b)(2)(iii) | | because there was no redundant equipment available to operate and perform | | the required safety function. | | | | The licensee notified the NRC resident inspector (Bruce Bartlett) for | | Paducah and plans to submit a written report. | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38581 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 12/19/2001| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 04:47[EST]| | RXTYPE: [1] CE |EVENT DATE: 12/19/2001| +------------------------------------------------+EVENT TIME: 02:50[CST]| | NRC NOTIFIED BY: CHRISTENSEN |LAST UPDATE DATE: 12/19/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GARY SANBORN R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOCAL FIRE DEPARTMENT NOTIFIED OF A FIRE ONSITE | | | | A fire alarm was received @ 0248 CST on 12/19/01 for room-22 safety | | injection pump room. An inspection showed heavy smoke at entrance to | | room. The plant fire brigade was manned and personnel entered the room. | | The fire source was an extension cord, connected to some heaters, which | | started some anti-contamination clothing on fire. The fire was identified @ | | 0306 CST and declared out @ 0308 CST. The Blair Fire Department was | | notified @ 0250 CST and responded to the site. No entry was made to the | | Protected Area, as the fire was out upon their arrival. The licensee is | | still investigating the cause. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021