Event Notification Report for December 17, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/14/2001 - 12/17/2001 ** EVENT NUMBERS ** 38513 38562 38563 38564 38565 38566 38567 38568 38569 38570 38571 38572 38573 38574 38575 38576 . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38513 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/23/2001| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 12:30[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/23/2001| +------------------------------------------------+EVENT TIME: 12:10[EST]| | NRC NOTIFIED BY: CHARLIE PIKE |LAST UPDATE DATE: 12/15/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO FLORIDA STATE INVOLVING RECOVERED SEA TURTLE FROM | | UNIT 1 INTAKE STRUCTURE | | | | "A sea turtle with no external injuries but appearing to be distressed was | | recovered from the Unit 1 Intake Structure. The State Stranding Coordinator | | for sea turtles has been contacted." | | | | * * * UPDATE 11/23/01 AT 1255EST FROM CHARLIE PIKE TO S. SANDIN * * * | | | | "Turtle has died." | | | | The licensee informed both the State of Florida and the NRC Resident | | Inspector. | | | | * * * UPDATE 1413EST ON 12/3/01 FROM JACK BREEN TO FANGIE JONES * * * | | | | At approximately 1215 EST on 12/3/01, a report was made to the Florida | | Department of Fish and Wildlife concerning the recovery of an injured sea | | turtle from the plant's intake canal. The turtle was a green sea turtle in | | the intake canal that appeared distressed and looked to have a wound from a | | boat motor on its back. It will be transferred to the State for | | rehabilitation. | | | | The licensee plans to notify the NRC resident inspector. Notified | | R2DO(MacAlpine). | | | | * * * UPDATE 1333EST ON 12/15/01 FROM JACK BREEN TO JOHN MACKINNON * * * | | | | At approximately 1215 EST on 12/15/01, a report was made to the Florida | | Department of Fish and Wildlife Conservation Commission to pick up a Green | | Turtle for rehabilitation. The Green Turtle was taken from the plant's | | intake canal, and the turtle appears to have shark bites. | | | | The licensee plans to notify the NRC resident inspector. Notified R2DO | | (Chuck Ogle). | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38562 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 12/14/2001| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 08:57[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 12/14/2001| +------------------------------------------------+EVENT TIME: 06:45[CST]| | NRC NOTIFIED BY: KEVIN HUJET |LAST UPDATE DATE: 12/14/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 95 Power Operation |95 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT COMPUTER AND SAFETY PARAMETERS DISPLAY SYSTEM INOPERABLE | | | | The unit suffered a failure of the plant computer at 1452 CST on 12/13/01 | | and repairs are ongoing. The plant computer is expected to be down greater | | than 24 hours. The plant computer feeds the Safety Parameter Display System | | (SPDS), which is inoperable also. The licensee has made a decision to make | | this report under a major loss of emergency assessment capabilities per 10 | | CFR 50.72(b)(3)(xiii) as a conservative measure. The control board | | indicators are operable and are used by the operators normally in an | | emergency. The Shift Technical Advisor will perform a manual review of | | safety parameters in the case of an emergency, using the control board | | indications. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38563 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ELKHART HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: ELKHART HOSPITAL |NOTIFICATION TIME: 12:17[EST]| | CITY: ELKHART REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: 00:00[CST]| |LICENSE#: 13-18879-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: GARETH WILLIAMS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATIONS: UNDERDOSES OF SAMARIUM-153 | | | | Elkhart Hospital was notified today by the RSO for Spectrum Pharmaceuticals | | that Sa-153 quadramet doses total activity shipped to them was incorrectly | | calibrated. Spectrum Pharmaceuticals informed the Hospital that they had | | made an error in the attenuation calculation for the beta factor in the | | samarium-153 total activity and that this error may have been made more than | | 6 months ago. Spectrum Pharmaceuticals believes that the Sa-153 total | | activity is actually less by 20 to 30%. At this time, Elkhart Hospital does | | not know how many patients have received an underdose of Sa-153. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38564 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GOSHEN GENERAL HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: GOSHEN GENERAL HOSPITAL |NOTIFICATION TIME: 12:18[EST]| | CITY: GOSHEN REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: 00:00[CST]| |LICENSE#: 13-18845-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: Dr. SHEPERD | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATIONS: UNDERDOSES OF SAMARIUM-153 | | | | Goshen General Hospital was notified today by the RSO for Spectrum | | Pharmaceuticals that Sa-153 quadramet, used for pain relief in bone cancer | | patients, beta attenuation were incorrectly calculated. This attenuation | | calculation error made by Spectrum Pharmaceuticals has resulted in patient's | | given Sa-153 at Goshen General Hospital being underdosed between 20 to 30%. | | The attenuation error may have existed for greater than 6 months. Three | | patients have been given a possible underdose of Sa-153. | | | | NRC Region 3 personnel have been notified of this event by the licensee. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38565 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: HOME HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: HOME HOSPITAL |NOTIFICATION TIME: 13:17[EST]| | CITY: LAFAYETTE REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: [CST]| |LICENSE#: 13-09788-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DUNSEATH | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL MEDICAL MISADMINISTRATION: UNDERDOSE OF SAMARIUM-153 | | | | The licensee was notified today by the RSO for Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet doses may be approximately 20-30% | | less than labeled due to an error in the attenuation calculation for the | | beta factor in the Sa-153 total activity calculation. This calculation | | error may have existed for greater than 6 months. The licensee is aware of | | one patient who was treated during this period and is reviewing treatment | | records to determine whether any others may be affected. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38566 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST. JOSEPH'S REGIONAL MEDICAL CENTR |NOTIFICATION DATE: 12/14/2001| |LICENSEE: ST. JOSEPH'S REGIONAL MEDICAL CENTR. |NOTIFICATION TIME: 14:13[EST]| | CITY: SOUTH BEND REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: [CST]| |LICENSE#: 13-02650-02 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: Dr. JOHN SCHEU | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL MEDICAL MISADMINISTRATIONS: UNDERDOSES OF SAMARIUM-153 | | | | The licensee was notified today by the RSO for Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet doses may be approximately 20-30% | | less than labeled due to an error in the attenuation calculation for the | | beta factor in the Sa-153 total activity calculation. This calculation | | error may have existed greater than 6 months. The licensee is aware of two | | patients who were treated during this period. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38567 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 12/14/2001| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 14:30[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 12/14/2001| +------------------------------------------------+EVENT TIME: 11:27[EST]| | NRC NOTIFIED BY: STEVE COSAR |LAST UPDATE DATE: 12/14/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS-FOR-DUTY REPORT | | | | A contract supervisor tested positive for illegal drug use during a random | | test. The individual did not have access to vital areas, and his site access | | has been terminated. The NRC resident inspector has been informed of this | | event by the licensee. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38568 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: BORGESS MEDICAL CENTER |NOTIFICATION DATE: 12/14/2001| |LICENSEE: BORGESS MEDICAL CENTER |NOTIFICATION TIME: 14:44[EST]| | CITY: KALAMAZOO REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: MI |EVENT TIME: [EST]| |LICENSE#: 21-12275-02 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC RAMSAY | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION: UNDERDOSE OF SAMARIUM-153 | | | | The licensee was notified today by the RSO for Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet doses may be approximately 20-30% | | less than labeled due to an error in the attenuation calculation for the | | beta factor in the Sa-153 total activity calculation. This calculation | | error may have existed for greater than 6 months. The licensee does not | | know how many patients have been treated and is looking through records to | | determine number of patients treated with Sa-153. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38569 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: BRONSON METHODIST HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: BRONSON METHODIST HOSPITAL |NOTIFICATION TIME: 14:48[EST]| | CITY: KALAMAZOO REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: MI |EVENT TIME: [EST]| |LICENSE#: 21-13125-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MARK WATTS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION: UNDERDOSE OF SAMARIUM-153 | | | | The licensee was notified today by the RSO for Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet doses may be approximately 20-30% | | less than labeled due to an error in the attenuation calculation for the | | beta factor in the Sa-153 total activity calculation. This calculation | | error may have existed for greater than 6 months. The licensee is aware of | | one patient treated in the last year. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38570 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST. LUKES HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: ST. LUKES HOSPITAL |NOTIFICATION TIME: 15:07[EST]| | CITY: BETHLAHAM REGION: 1 |EVENT DATE: 12/12/2001| | COUNTY: STATE: PA |EVENT TIME: 07:00[EST]| |LICENSE#: 37-07939-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CLIFFORD ANDERSON R1 | | |PAUL BONNETT R1 | +------------------------------------------------+ | | NRC NOTIFIED BY: KATHY SANDERS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAA1 20.1906(d)(1) SURFACE CONTAM LEVELS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SURFACE CONTAMINATION | | | | IBA out of New Jersey delivered a metal case, ammo case, which contained | | less than 21 millicuries of fluorine-18, to St. Lukes North outpatient | | facility on 12/12/01 before 0700 hours. Swipes taken of the outside and | | inside of the ammo case found technetium-99m contamination. Outside and | | inside swipes both indicated contamination level around 6800 cpm. The ammo | | case was decontaminated and placed in St. Lukes Hot Lab. St. Lukes | | contacted IBA and informed them of the contamination. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38571 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: LOUISIANA RADIATION PROTECTION DIV |NOTIFICATION DATE: 12/14/2001| |LICENSEE: BAYOU TESTERS |NOTIFICATION TIME: 15:20[EST]| | CITY: REGION: 4 |EVENT DATE: 12/12/2001| | COUNTY: STATE: LA |EVENT TIME: 00:00[CST]| |LICENSE#: LA-7112-L01 AGREEMENT: Y |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BILL JONES R4 | | |FED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SCOTT BLACKWELL | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EXCESSIVE EXPOSURE | | | | "The monthly personnel badges showed an excessive exposure for three | | employees. [One individual] had 5136 mRem, [another individual] had 5095 | | mRem, and [a third individual] had 5200 mRem for the year as of November 10, | | 2001. Once the facility received the badge report, the facility notified | | [the] DEQ. The facility is also sending a written report to [the] DEQ. | | These three individuals have been removed from radiation work." | | | | Event Report No.: LA010017 | | | | (Call the NRC operation officer for contact information and for the names of | | the individuals involved.) | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38572 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST. JOSEPH'S HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: ST. JOSEPH'S HOSPITAL |NOTIFICATION TIME: 15:27[EST]| | CITY: KOKOMO REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: 00:00[CST]| |LICENSE#: 13-11385-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TODD REYBURN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL MEDICAL MISADMINISTRATION: UNDERDOSE OF SAMARIUM-153 | | | | The licensee was notified today by the RSO for Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet doses may be approximately 20-30% | | less than labeled due to an error in the attenuation calculation for the | | beta factor in the Sa-153 total activity calculation. This condition may | | have existed for greater than 1 year. The licensee found one patient who | | was treated with Sa-153 and that was on 10/05/00. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38573 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MEMORIAL HOSPITAL |NOTIFICATION DATE: 12/14/2001| |LICENSEE: MEMORIAL HOSPITAL |NOTIFICATION TIME: 15:43[EST]| | CITY: SOUTH BEND REGION: 3 |EVENT DATE: 12/14/2001| | COUNTY: STATE: IN |EVENT TIME: 00:00[CST]| |LICENSE#: 13-18881-01 AGREEMENT: N |LAST UPDATE DATE: 12/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANNE MARIE STONE R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RICHARD SELLE | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL MEDICAL MISADMINISTRATIONS: UNDERDOSES OF SAMARIUM-153 | | | | The licensee was notified today by the RSO of Spectrum Pharmaceuticals that | | the total activity of Sa-153 quadramet does may be approximately 20-30% less | | than labeled due to an error in the attenuation calculation for beta factor | | in the Sa-153 total activity. The licensee believes that he has treated two | | patients since 1998 with Sa-153. | | | | NRC Region 3 has been notified of this event. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38574 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 12/15/2001| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 23:00[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 12/15/2001| +------------------------------------------------+EVENT TIME: 19:00[EST]| | NRC NOTIFIED BY: TOM RESTUCCIO |LAST UPDATE DATE: 12/15/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 60 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FROM 60% POWER DUE TO UNIDENTIFIED LEAK RATE EXCEEDING | | 5 GPM | | | | At 0431 on December 15, 2001, Unit 2 noted a step increase in unidentified | | drywell leakage from 0.2 gpm (normal) to 0.4 gpm. Coincident with this step | | increase, containment atmosphere radiation levels rose and alarmed on the | | particulate channels. Throughout the day, investigation continued into | | possible causes, and the trend in leakage showed no appreciable increase. | | At 1658, containment atmosphere radiation levels rose again, and a large | | step increase in leakage was noted from approximately 0.5 gpm to 1.7 gpm. | | The technical specification limit is less than 5 gpm unidentified leakage | | and less than a 2-gpm rise in unidentified leakage during the previous the | | 24 hours. At 1745, plant management ordered an orderly plant shutdown to | | identify the source of leakage in the drywell. At 1900, a normal reactor | | shutdown was commenced, original reactor power was 100%, in preparation for | | repairing the leak in the drywell. At 1919, drywell unidentified leakage | | rose to 2.27 gpm, and the technical specification action statement was | | entered for greater than a 2-gpm rise in unidentified leakage during the | | previous 24 hours. | | | | At 2040, the drywell unidentified leak rate exceeded 5 gpm (5.87 gpm), and | | the decision was made to scram the plant. At 2046, the reactor mode switch | | was placed in shutdown, all systems functioned as required, all rods fully | | inserted into the core. The scram signal received was Average Power Range | | Monitor (APRM) neutron upscale due to setpoint setdown with the mode switch | | out of run. A secondary scram signal was received when reactor water level | | dropped to less than 159.3" (Level 3) (expected due to level shrink on the | | scram). Level 3 also provided a Primary Containment Isolation System (PCIS) | | signal to group 4 (Residual Heat Removal System, [RHS] sampling valves) and | | group 5 (RHS shutdown cooling valves). At the time of the signal, all group | | 4 and 5 valves were closed. At 2043, technical specification action | | statement associated with exceeding 5 gpm was exited. At 2149, technical | | specification action statement associated with greater than 2 gpm rise over | | the previous 24 hours was exited. | | | | At this time, drywell unidentified leakage 1.5 gpm and lowering, plant | | pressure is being reduced. Reactor water level is being maintained with | | condensate/feedwater. Reactor pressure control is being maintained via | | turbine bypass valves with cooldown in progress. All Emergency Core Cooling | | Systems and the Emergency Diesel Generator are fully operable, and the | | electrical grid is stable. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38575 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/16/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 00:30[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 12/15/2001| +------------------------------------------------+EVENT TIME: 22:28[EST]| | NRC NOTIFIED BY: ALAN RABENOLD |LAST UPDATE DATE: 12/16/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |ACCS 50.72(b)(2)(iv)(A) ECCS INJECTION | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE REACTOR RECIRCULATION PUMPS DOWN SHIFTED TO SLOW SPEED FOR UNKNOWN | | REASONS RESULTING IN AN AUTOMATIC REACTOR SCRAM, BALANCE-OF-PLANT | | ISOLATIONS, AND EMERGENCY CORE COOLING SYSTEM ACTUATIONS. | | | | At 2228 EST on 12/15/01, the reactor recirculation pumps down shifted to | | slow speed for unknown reasons. This caused reactor pressure vessel (RPV) | | water level to swell, and an automatic reactor scram from 100% power | | occurred when Level 8 was reached. All control rods fully inserted. | | Following the scram, RPV water level started to decrease because the | | feedwater pumps also tripped (as designed) when Level 8 was reached. When | | RPV water level dropped to Level 2 (130 inches), balance-of-plant isolations | | occurred, and all of the applicable valves properly isolated. In addition, | | the high pressure core spray (HPCS) and reactor core isolation cooling | | (RCIC) systems automatically actuated when Level 2 was reached. The HPCS | | and RCIC systems were utilized to restore RPV water level to the normal | | range. | | | | The unit is currently stable in Mode 3 with RPV pressure at 900 psi and RPV | | water level at 210 inches. Normal feedwater is being utilized to maintain | | RPV water level within the proper band, and the HPCS and RCIC systems have | | been secured. The main steam isolation valves remained open, and the | | condenser is being utilized as the heat sink. Containment parameters are | | currently normal, the electrical grid is stable, and the emergency diesel | | generators are available. | | | | The licensee stated that all systems functioned as required and that there | | was nothing unusual or misunderstood other than the cause of the initiating | | event (the recirculation pumps down shifting to slow speed). The licensee's | | investigation is underway. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38576 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 12/16/2001| | UNIT: [] [3] [] STATE: PA |NOTIFICATION TIME: 21:39[EST]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 12/16/2001| +------------------------------------------------+EVENT TIME: 16:45[EST]| | NRC NOTIFIED BY: JOHN McCLINTOCK |LAST UPDATE DATE: 12/16/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | | |AINC 50.72(b)(3)(v)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH HIGH FLOW INSTRUMENTATION FOR REACTOR WATER CLEANUP (RWCU) FOUND | | INOPERABLE. | | | | During performance of routine surveillance testing on the PBAPS Unit 3 RWCU | | system high flow isolation instrumentation, it was discovered that both | | channels of isolation instrumentation were simultaneously inoperable. Both | | affected instruments were returned to operable status by 1828 hours on | | 12/16/01. | | | | The RWCU system is designed to automatically isolate upon detection of a | | high flow condition. This isolation detection system utilizes two channels | | of differential pressure instrumentation for high flow detection. An | | isolation of the RWCU system can be accomplished by actuation of either | | channel of the logic. A single channel trip would result in either an | | inboard or outboard isolation. A failure of both channels would result in a | | failure of the system to isolate as required. | | | | On 12/16/01 at 1111 hours, surveillance testing of the "A" channel high flow | | instrument (DPIS 3-12-124A) determined that this instrument failed to trip | | due to entrapped air in the sensing line. DPIS 3-12-124A was vented, | | retested, and returned to operable status at 1536 on 12/16/01. | | | | At 1645 hours, surveillance testing of the "B" channel RWCU high flow | | instrument (DPIS 3-12-124B) determined that this instrument failed to trip | | due to entrapped air in the sensing line. DPIS 3-12-124B was vented, | | retested, and returned to operable status at 1828 on 12/16/01. | | | | At 1645 on 12/16/01, it was determined that both channels of Unit 3 RWCU | | system high flow isolation instrumentation were simultaneously inoperable | | since the system had been placed in service during refueling outage 3R13. | | Unit 3 entered Mode 2 on 10/08/01 at 2221 hours, requiring the Primary | | Containment Isolation (PCIS) function to be operable. | | | | Based on the above, this event is reportable under 10 CFR | | 50.72(b)(3)(v)(C). | | | | The systems affected were the RWCU system isolation logic instruments, DPIS | | 3-12-124A and DPIS 3-12-124B. These instruments actuate on high system flow | | of 125%. No plant effects or transient occurred as a result of this event. | | The RWCU system isolation capability, on high system flow, was inoperable. | | This isolation capability is required whenever the RWCU system is in service | | with the reactor in Modes 1, 2, or 3. | | | | DPISs 3-12-124A and 3-12-124B were filled, vented, tested satisfactorily, | | and returned to operable status. | | | | A station investigation to determine the cause of the air entrapment is in | | progress. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021