Event Notification Report for December 7, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/06/2001 - 12/07/2001 ** EVENT NUMBERS ** 38542 38543 38544 38545 . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38542 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 12/06/2001| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 04:55[EST]| | RXTYPE: [2] GE-4 |EVENT DATE: 12/06/2001| +------------------------------------------------+EVENT TIME: 03:50[EST]| | NRC NOTIFIED BY: JEFF GROFF |LAST UPDATE DATE: 12/06/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |PATRICK HILAND R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM DUE TO A LOSS OF STATOR WATER COOLING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 0350 on 12/6/01 with the reactor at 100%, a manual reactor scram was | | inserted due to the loss of stator water cooling. All control rods fully | | inserted into the core. While taking a stator water sample, the heat | | exchanger vent line broke off the heat exchanger losing stator water from | | the system. A reactor scram was inserted prior to an [imminent] turbine | | generator trip." | | | | "Following the reactor scram, water level dropped to approximately 120". | | Reactor water level is being maintained in the normal level band (197") with | | feedwater/condensate. The following 'Level 3' isolations occurred as | | expected:" | | | | "Group 4 - RHR Shutdown Cooling and Head Spray" | | "Group 13 - Drywell Sumps" | | "Group 15 - Traversing Incore Probe Systems" | | | | "All valves in [Groups] 4 and 15 were closed prior to the event. Group 13 | | valves closed as designed. No ECCS systems initiated, and no SRVs lifted. | | All Emergency Diesel Generators are operable." | | | | The licensee stated that the main steam isolation valves remained open and | | that the main condenser is being used as the heat sink. Containment | | parameters are normal, and the grid is stable. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 38543 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CROW BUTTE RESOURCES |NOTIFICATION DATE: 12/06/2001| |LICENSEE: CROW BUTTE RESOURCES |NOTIFICATION TIME: 09:39[EST]| | CITY: CRAWFORD REGION: 4 |EVENT DATE: 12/05/2001| | COUNTY: DAWES STATE: NE |EVENT TIME: 14:30[CST]| |LICENSE#: SUA-1534 AGREEMENT: Y |LAST UPDATE DATE: 12/06/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANTHONY GODY R4 | | |FRED BROWN NMSS | +------------------------------------------------+MIKE LAYTON (MINING) NMSS | | NRC NOTIFIED BY: MIKE GRIFFIN | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A SHALLOW MONITOR WELL IN EXCURSION FOR SULFATE | | | | At approximately 1430 CST on 12/05/01, the licensee received second | | confirmation of well #SM723 being in excursion for sulfate. Sulfate was | | discovered to be at a concentration of 68 mg/l which exceeded the upper | | control limit of 65 mg/l. This excursion is believed to be naturally | | occurring, and the licensee has submitted a license amendment request to | | change the upper control limit. The licensee also plans to maintain an | | increased monitoring frequency. The licensee stated that well #SM723 is | | located within a controlled well field with a shallow aquifer and that there | | was no adverse impact expected on individuals or the environment. | | | | (Call the NRC operations officer for licensee contact information.) | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38544 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 12/06/2001| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 11:34[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 12/06/2001| +------------------------------------------------+EVENT TIME: 09:05[CST]| | NRC NOTIFIED BY: WEEKLEY |LAST UPDATE DATE: 12/06/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTHONY GODY R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 12 Power Operation |1 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE MADE AN OFFSITE NOTIFICATION TO THE MISSOURI PUBLIC SERVICE | | COMMISSION | | | | The following is a report to the Missouri Public Service Commission (MPSC) | | to notify the them of a forced outage at the Callaway Nuclear Plant. This | | notification is reportable under 4CSR240-20.080(3)(B) because the outage is | | expected to last longer than 72 hours. | | | | At 2248 CST, December 3, 2001, Callaway Plant shut down to effect repairs on | | the Main Generator. A leak had developed on a Main Generator cooling | | system requiring repairs which could only be made with the unit off-line. | | Initially, the Plant was expected to return to service within 72 hours, but | | due to the complexity of the repairs, the unit is now expected to return to | | service after the 72-hour deadline has expired. Expectations are to return | | to service by December 7, 2001. | | | | The Licensee has informed the NRC Resident Inspector of the MPSC | | notification. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38545 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 12/06/2001| | UNIT: [1] [2] [] STATE: AL |NOTIFICATION TIME: 13:52[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 12/06/2001| +------------------------------------------------+EVENT TIME: 10:20[CST]| | NRC NOTIFIED BY: CHERI COLLINS |LAST UPDATE DATE: 12/06/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MARK LESSER R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY | | | | A licensed operator (currently inactive) tested positive for illegal drug | | use under the licensee's fitness-for-duty (FFD) program. The individual was | | not on shift assignment, nor had the individual performed on-shift | | activities during the past year. The individual's site access has been | | terminated. The NRC resident inspector has been informed of this event by | | the licensee. | +------------------------------------------------------------------------------+ .
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