Event Notification Report for November 9, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/08/2001 - 11/09/2001 ** EVENT NUMBERS ** 38479 38480 38482 38483 38484 38485 38486 . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38479 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/08/2001| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 10:39[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/08/2001| +------------------------------------------------+EVENT TIME: 10:39[EST]| | NRC NOTIFIED BY: KORTH |LAST UPDATE DATE: 11/08/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |R2 IRC TEAM MANAGER R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE STATE THAT TWO DEAD SEA TURTLES WERE DISCOVERED IN | | THE INTAKE CANAL | | | | At approximately 0800 on 11/8/01 two dead sea turtles(one green and one | | loggerhead) were recovered from the licensee's intake canal. Pursuant to | | the sea turtle permit, the Florida Department of Environmental | | Protection(FDEP) was notified at approximately 0845. Both turtles | | apparently drowned below the surface of the 5" mesh barrier net. The | | carcasses will be turned over to the FWCC. | | | | The NRC Resident Inspector and the FDEP were notified. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38480 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/08/2001| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 14:00[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/08/2001| +------------------------------------------------+EVENT TIME: 13:05[EST]| | NRC NOTIFIED BY: JACK BREEN |LAST UPDATE DATE: 11/08/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |R2 IRC TEAM MANAGER R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE STATE OF A DEAD SEA TURTLE DISCOVERED IN THE | | INTAKE CANAL | | | | "At approximately 1230, one dead sea turtle was recovered from the St. Lucie | | Intake Canal. Pursuant to the sea turtle permit the Florida Department of | | Environmental Protection (FDEP) was notified at 1305. The notification of | | FDEP necessitates a four (4) hour non-emergency notification of [the] NRC | | per 10CFR50.72(b)(2)(xi)." | | | | The licensee informed the State of Florida and will inform the NRC Resident | | Inspector. | | | | HOO Note: See previous event #38479. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Hospital |Event Number: 38482 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF PENNSYLVANIA |NOTIFICATION DATE: 11/08/2001| |LICENSEE: UNIVERSITY OF PENNSYLVANIA |NOTIFICATION TIME: 16:05[EST]| | CITY: PHILADELPHA REGION: 1 |EVENT DATE: 11/08/2001| | COUNTY: STATE: PA |EVENT TIME: 15:15[EST]| |LICENSE#: 37-00118-07 AGREEMENT: N |LAST UPDATE DATE: 11/08/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |R1 IRC TEAM MANAGER R1 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: FORREST | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE REPORTED A MEDICAL MISADMINISTRATION OCCURRED DURING | | THERAPEUTIC TREATMENT | | | | At approximately 2:45 pm on November 7, 2001, a physician, an authorized | | user in Nuclear Medicine, began administration of a Y-90 therapeutic | | radiopharmaceutical dose in accordance with the written directive for the | | treatment. | | | | The administration system used a saline flush followed by an air flush to | | administer the radiopharmaceutical. During the air flush at approximately | | 3:15 pm, fluid was observed on the top of the second dose vial. To avoid | | infusing a potentially non-sterile dose, the doctor stopped the dose | | administration before the entire dose was infused. Based on post infusion | | measurements of the dose vials, the patient received approximately 80 mCi | | instead of the prescribed 120 mCi. | | | | The administrating physician informed the patient on November 7, 2001 that | | because of the administration problem, the total prescribed dose was not | | administered. The referring physician will be notified. | | | | There are no expected harmful effects as a result of this treatment. The | | treatment protocol requires the subject to receive three separate 120 mCi | | doses of the Y-90 radiopharmaceutical. This was the patient's second | | treatment. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38483 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/08/2001| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 16:30[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/08/2001| +------------------------------------------------+EVENT TIME: 12:40[EST]| | NRC NOTIFIED BY: JIM TOTTON |LAST UPDATE DATE: 11/08/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |R2 IRC TEAM MANAGER R2 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INFORMATION REPORT INVOLVING A CONTROLLED PLANT SHUTDOWN FOR REPAIRS | | | | "A controlled plant shutdown was performed due to a small (1 inch or less) | | steam leak on 'B' main steam header. The leak originated from a 1 inch | | drain line located upstream of the 'B' MSIV. The Unit was shutdown in | | accordance with plant procedures. A plant cooldown to mode 5 is in progress | | to affect repairs." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38484 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CONAM |NOTIFICATION DATE: 11/08/2001| |LICENSEE: CONAM |NOTIFICATION TIME: 16:52[EST]| | CITY: GLEN DALE HTS. REGION: 3 |EVENT DATE: 11/08/2001| | COUNTY: STATE: IL |EVENT TIME: 09:35[CST]| |LICENSE#: 12-16559-02 AGREEMENT: Y |LAST UPDATE DATE: 11/08/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |R3 IRC TEAM MANAGER R3 | | |R1 IRC TEAM MANAGER R1 | +------------------------------------------------+PATRICIA HOLAHAN NMSS | | NRC NOTIFIED BY: SLACK | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | | | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE CONAM COMPANY REPORTED THAT ONE OF THEIR RADIOGRAPH CAMERAS HAD A SOURCE | | THAT BECAME STUCK | | | | An Iridium - 192 AEA model 660B radiography camera in use at the Sunoco | | refinery at Gerard Pt. Philadelphia, Pa. had the source get stuck while the | | licensee was retracting it into the camera. The source was moved in and out | | of the camera a few times before it finally was fully retracted into the | | camera. No one was overexposed and the camera will be returned to the | | manufacturer for inspection and repair. They believe the cause was due to a | | locking problem in the camera. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38485 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/08/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:35[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/08/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:45[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/08/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |R3 IRC TEAM MANAGER R3 | | DOCKET: 0707002 | | +------------------------------------------------+ | | NRC NOTIFIED BY: KEITH VANDERPOOL | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY SYSTEM DISCOVERED INOPERABLE DURING SURVEILLANCE TEST | | | | "At 1045 hours maintenance personnel identified the failure of the safety | | system component in the X-760 building. During the scheduled TSR | | surveillance, maintenance on the X-760 Criticality Accident Alarm System | | (CAAS), maintenance personnel identified that the associated nitrogen horns | | would not have functioned as designed. Post maintenance testing of the | | associated nitrogen horn identified that the horns would not sound as | | required due to a gross leak at the block manifold. Repairs and a | | successful post maintenance test were completed under the direction of the | | System Engineer. The Plant Shift Superintendent (PSS) has directed a random | | check of the site CAAS facilities be conducted to ensure this condition does | | not exist elsewhere. The X-760 CAAS remains inoperable pending the | | completion of the requested engineering evaluation to address the gross leak | | condition causing the safety system failure." | | | | Operations informed both the NRC Resident Inspector and the DOE Site | | Representative. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38486 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 11/09/2001| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 01:08[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 11/08/2001| +------------------------------------------------+EVENT TIME: 20:57[EST]| | NRC NOTIFIED BY: RONALD GREEN |LAST UPDATE DATE: 11/09/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |R1 IRC TEAM MANAGER R1 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R N 0 Startup |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING UNIT STARTUP | | | | "During a reactor start up, BVPS Unit One Reactor tripped prior to reaching | | criticality. The apparent cause of the trip is a blown control power fuse | | on Intermediate Range Nuclear Instrument channel N36. The blown fuse caused | | actuation of the Intermediate Range high level trip. All control rods fully | | inserted. All equipment properly functioned. Unit One is presently in mode | | three at normal temperature and pressure. Decay heat removal is through the | | steam bypass valves to the main condenser as it was throughout the event. A | | main feed pump is supplying feedwater through the bypass feedwater | | regulating valves." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021