Event Notification Report for October 17, 2001
*** NOT FOR PUBLIC DISTRIBUTION*** U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/16/2001 - 10/17/2001 ** EVENT NUMBERS ** 38220 38376 38395 . !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38220 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 08/17/2001| | UNIT: [] [] [3] STATE: AZ |NOTIFICATION TIME: 21:19[EDT]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 08/17/2001| +------------------------------------------------+EVENT TIME: 16:45[MST]| | NRC NOTIFIED BY: RUSSELL STROUD |LAST UPDATE DATE: 10/16/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTHONY GODY R4 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 97 Power Operation |55 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN DUE A LEAK FROM THE FUEL POOL INTO CONTAINMENT | | | | "On August 17, 2001 at approximately 1245 MST, Palo Verde Unit 3 was at | | approximately 97 percent power and at normal RCS temperature and pressure, | | when operations personnel detected an increase in containment sump level. | | Subsequent investigation revealed the quick operating closure device (QOCD) | | (EQID #PCE-M01) that isolates the containment from the fuel transfer tube | | was leaking by borated water from the fuel transfer canal at approximately 1 | | gallon per minute. Operations personnel entered TS LCO 3.6.1 Containment, | | Required Action A. This action requires the containment be restored to an | | operable status within one hour. | | | | "Since containment integrity was uncertain, and compliance with LCO 3.6 1 | | Required Action A could not be met within one hour, operations personnel | | entered LCO 3.6.1, Required Action 8.1 at 1345 MST. Required Action B.1 | | requires the unit be placed in Mode 3 in 6 hours, and Required Action 8.2 | | requires the unit be placed in Mode 5 within 36 hours, Following operations | | briefings, shutdown was commenced at approximately 1645 MST. At this time, | | Palo Verde Unit 3 is continuing to reduce power in an orderly manner and | | anticipates being in Mode 3 (Hot Standby) by approximately 1845 MST. | | | | "There were no other component failures, testing or work in progress that | | contributed to this event. The QOCD leak is allowing 4400 part per million | | borated water into the containment. There has been no release of | | radioactivity to the environment and no impact to the health and safety of | | the public has occurred or is anticipated. There is no elevated RCS activity | | and heat removal is via normal steaming to the main turbine condenser. The | | electric grid is stable." | | | | The licensee informed the NRC Resident Inspector. | | | | * * * RETRACTED AT 1257 EDT ON 10/16/01 BY DANIEL HAUTALA TO FANGIE JONES * | | * * | | | | "This notification is a retraction to the August 17, 2001, ENS #38220 which | | reported a Palo Verde Nuclear Generating Station Unit 3 shutdown required by | | Technical Specification 3.6.1. In the condition described by this ENS, the | | failure, a loss of containment integrity, never existed. Although personnel | | conservatively declared containment inoperable, plant engineers have since | | determined that containment integrity per Technical Specification 3.6.1 was | | maintained. The water leakage into containment via the Quick Operating | | Closure Device (QOCD) 0-rings did not constitute or create a potential | | accident leakage path out of containment. Therefore, the subsequent plant | | shutdown was not required by a Technical Specification action. | | | | "The NRC Resident Inspector has been notified." | | | | The Region 4 Duty Officer (Bill Jones) has been notified. | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38376 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 10/10/2001| |LICENSEE: LAW ENGINEERING AND ENVIRONMENTAL SER|NOTIFICATION TIME: 17:29[EDT]| | CITY: DALLAS REGION: 4 |EVENT DATE: 10/10/2001| | COUNTY: STATE: TX |EVENT TIME: [CDT]| |LICENSE#: L02453 AGREEMENT: Y |LAST UPDATE DATE: 10/10/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA HOWELL R4 | | |C.W. (BILL) REAMER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN, JR. (fax) | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT REGARDING DISCOVERY OF A LAW ENGINEERING AND | | ENVIRONMENTAL SERVICES GAUGE ON A RESIDENTIAL STREET BY AN EMPLOYEE OF | | ANOTHER COMPANY | | | | The following text is a portion of a facsimile received from the Texas | | Department of Health, Bureau of Radiation Control: | | | | "Texas Incident No.: I-7810" | | | | "License No.: L02453" | | | | "Licensee: Law Engineering and Environmental Services, Houston, Texas (Fort | | Worth Subsite)" | | | | "Event date and time: 10/10/01 a.m." | | | | "Event location: Dallas, Texas (exact location unknown at this time - gauge | | was transported to 10722 North Stemmons Freeway, Dallas, Texas 75220[)]" | | | | "Event type: Found Nuclear Density Gauge, Troxler 3411 B, Serial #11251" | | | | "Notifications: Notified Troxler Electronic Labs, TDH Public Health Region | | 3 to pickup gauge and have leak tested." | | | | "Event description: Gauge found in the middle of a residential street by an | | employee of Giles Engineering, Texas License L04919-001. Gauge was found to | | be un-locked - both case and control rod. The gauge was reported to be in | | the 'On' position. No shipping papers were found in the case. No warning | | stickers were reported to be on the exterior of the case. Troxler Labs | | reports that the gauge was last seen by them over 2-years ago and was then | | owned by Austin Testing Engineers - no evidence of Licensure through this | | Agency. Gauge was tracked to Law Engineering in Fort Worth. TDH is holding | | the gauge. Will have leak test performed. Licensee was unaware that the | | gauge was missing and could not immediately find if the gauge was assigned | | on a job for 10/10/01." | | | | "Transport vehicle description: None available at this time." | | | | "Media attention: None" | | | | (Contact the NRC operations officer for an agreement state point of | | contact.) | +------------------------------------------------------------------------------+ . +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38395 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GLOBAL NUCLEAR FUEL - AMERICAS |NOTIFICATION DATE: 10/16/2001| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 16:18[EDT]| | COMMENTS: LEU CONVERSION (UF6 TO UO2) |EVENT DATE: 10/16/2001| | LEU FABRICATION |EVENT TIME: [EDT]| | LWR COMMERICAL FUEL |LAST UPDATE DATE: 10/16/2001| | CITY: WILMINGTON REGION: 2 +-----------------------------+ | COUNTY: NEW HANOVER STATE: NC |PERSON ORGANIZATION | |LICENSE#: SNM-1097 AGREEMENT: Y |DOUGLAS COLLINS R2 | | DOCKET: 07001113 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: LON PAULSON | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 REPORT - 24 HOUR | | | | The following is from a faxed report: | | | | At approximately 1630 on October 15, 2001 following an automatic shutdown of | | Dry Conversion Process Line 2, a higher than normal moisture analytical | | result was identified on Line 2A powder outlet cooling hopper. Manual | | moisture sample results indicated free moisture content in the U02 powder | | averaged 1.2% which is above the operational limit of 0.4% but well below | | the safety limit of 11 .2%. | | | | The associated outlet hatch valve control valve seats were subsequently | | determined to be leaking, leading to material with a higher than normal | | moisture content in the cooling hopper. The associated active engineered | | control (AEC) interlocks functioned as designed, the cooling hoppers were | | isolated, and the conversion process was automatically shutdown, thus no | | unsafe condition existed. | | | | The affected material has been transferred to favorable geometry containers | | per procedure. | | | | Controls were reestablished within 4 hours by proper function of the | | redundant dewpoint probe interlocks and automatic system shutdown. This | | event is reported pursuant to NRC Bulletin 91-01 (within 24 hours) due to | | loss of one of two independent moderation controls. Line 2 conversion | | remains shutdown pending investigation and implementation of corrective | | actions. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | Low safety significance - actual moisture content averaged 1.2% (12,200 ppm | | H20) within the established uniform moderation limit of 11.2% for (112,000 | | ppm H20) for the cooling hopper. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR): | | | | Multiple failure modes required before a criticality accident could occur. | | | | CONTROLLED PARAMETER(S) (MASS. MODERATION. GEOMETRY. CONCENTRATION. ETC): | | | | Moderation | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS): | | | | Net U02 inside cooling hopper A was ~50 kgs (4.95 % enriched) with 1.22% H20 | | (12,200 ppm H20). | | Uniform moderation limit for cooling hopper is 11.2% (112,000 ppm H20) | | assuming 5% enriched U02. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | Upstream moderation control on outlet hatch control system partially failed | | due to valve seat. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | | | 1. Conversion Line 2 shutdown. | | 2. Outlet hatch valve being replaced. | | 3. Investigation and implementation of additional corrective actions | | pending. | | | | The licensee intends to notify the local and state authorities and NRC | | Region 2 (David Ayres) | +------------------------------------------------------------------------------+ .
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021