Event Notification Report for September 25, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/24/2001 - 09/25/2001 ** EVENT NUMBERS ** 38308 38309 38310 38311 38312 38313 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38308 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 09/24/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 05:55[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 09/24/2001| +------------------------------------------------+EVENT TIME: 04:55[EDT]| | NRC NOTIFIED BY: LAURIE RAYLE |LAST UPDATE DATE: 09/24/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAMES LINVILLE R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF PROMPT NOTIFICATION TONE ALERT RADIO FOR GREATER THAN 1 HOUR | | | | The licensee received a call at 0504 EDT from the Oswego County Warning | | Point that the Oswego County Prompt Notification Tone Alert Radio had been | | out-of-service for greater than 1 hour as of 0455 EDT. The cause of the | | outage is unknown and is being investigated. | | | | The licensee notified the NRC Resident Inspector. | | | | See event #38309 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38309 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 09/24/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 10:03[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 09/24/2001| +------------------------------------------------+EVENT TIME: 03:55[EDT]| | NRC NOTIFIED BY: HALLIDAY |LAST UPDATE DATE: 09/24/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |FRANK COSTELLO R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF PROMPT NOTIFICATION TONE ALERT RADIO FOR GREATER THAN 1 HOUR | | | | At 0504 the licensee received notification that Oswego County Prompt | | Notification System Tone Alert Radio was out of service at 0355 and remained | | out of service for>1 hour from 0455 onward. The Sheriff department was | | contacted by Oswego County Emergency Operations Center for alternate | | alerting methods. The National Weather Service is addressing the reason for | | the Tone Alert Radios being out of service and will provide a return to | | service time to the Oswego County EOC. | | | | The NRC Resident Inspector was notified. | | | | See event #38309 | | | | * * * UPDATE 1235EDT ON 9/24/01 FROM DAVE POULAN TO S. SANDIN * * * | | | | The Tone Alert Radio was restored to service at 1200EDT. The licensee will | | inform the NRC resident inspector. | | | | Notified R1DO(Costello). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Research Reactor |Event Number: 38310 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: REED COLLEGE |NOTIFICATION DATE: 09/24/2001| | RXTYPE: 250 KW TRIGA MARK I |NOTIFICATION TIME: 15:16[EDT]| | COMMENTS: |EVENT DATE: 09/24/2001| | |EVENT TIME: 11:35[PDT]| | |LAST UPDATE DATE: 09/24/2001| | CITY: PORTLAND REGION: 4 +-----------------------------+ | COUNTY: MULTNOMAH STATE: OR |PERSON ORGANIZATION | |LICENSE#: R-112 AGREEMENT: Y |GREG PICK R4 | | DOCKET: 05000288 |MARVIN MENDONCA NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: STEPHEN FRANTZ | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | COURTESY CALL INVOLVING INDICATION OF A LEAKING FUEL ELEMENT | | | | A particulate airborne monitor measured Cs-137 and Rb-88 which is indication | | of a leaking fuel element. The reactor is currently shutdown. The licensee | | will identify which fuel element is leaking and remove it from service | | before restarting. The offsite dose consequence is minimal since the | | airborne activity is less than 10(E-12) microcuries/ml. The licensee will | | inform the NRR project manager. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38311 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 09/24/2001| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 15:33[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 09/24/2001| +------------------------------------------------+EVENT TIME: 12:30[CDT]| | NRC NOTIFIED BY: JOHN DAMPF |LAST UPDATE DATE: 09/24/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GREG PICK R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATIONS TO VARIOUS AGENCIES DUE TO A SPILL OF SULFURIC ACID | | ONSITE | | | | "This 4-hour call is being made to the NRC based on the requirements of | | 10CFR50.72(b)(2)(xi). This is due to a chemical spill at the Callaway Plant | | requiring notification of the Environmental Protection Agency (EPA), the | | United States Coast Guard National Response Center (USCGNRC) and Department | | of Natural Resources (DNR). | | | | "On 9/24/01, a sulfuric acid spill was discovered on the plant site. Initial | | estimates place the spill volume at two hundred gallons and requires | | notification of the EPA, USCGNRC, and DNR. It was concluded this event is | | reportable per 10CFR50.72(b)(2)(xi) due to notifications made to various | | governmental agencies. | | | | "The NRC Resident Inspector was notified of this event by the licensee." | | | | The sulfuric acid is 93% concentration and is used for treating cooling | | tower basin water. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38312 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: RUTGERS UNIVERSITY |NOTIFICATION DATE: 09/24/2001| |LICENSEE: RUTGERS UNIVERSITY |NOTIFICATION TIME: 16:40[EDT]| | CITY: NEW BRUNSWICK REGION: 1 |EVENT DATE: 09/24/2001| | COUNTY: STATE: NJ |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 09/24/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |ERIC LEEDS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PATRICK McDERMOTT | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIALLY MISSING/UNACCOUNTED FOR TRITIUM EXIT SIGN | | | | Rutgers University located in New Brunswick, NJ is conducting an | | investigation to determine whether a general license exit sign containing | | between 20-30 curies tritium was installed in the Chapel and, if so, is | | missing. Interviews of several individuals has provided conflicting | | information. A records search is in progress. The licensee informed NRC | | Region I (Ruland). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38313 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 09/25/2001| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 03:39[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/24/2001| +------------------------------------------------+EVENT TIME: 23:51[EDT]| | NRC NOTIFIED BY: JOSEPH PIERCE |LAST UPDATE DATE: 09/25/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO LOSS OF CIRCULATING WATER PUMPS | | | | The licensee reported that Salem Unit 1 manually tripped the reactor due to | | a loss of circulating water pumps, caused by a fault on the #2 station power | | transformer. The fault isolation caused loss of one of the required two | | off-site power sources to both Salem units. Auxiliary feedwater started on | | low steam generator level after isolation of main feedwater due to the | | reactor trip. All system functioned as required. The unit is stable in Hot | | Standby and an investigation into the cause of the electrical disturbance is | | underway. | | | | Two of four reactor coolant pumps tripped when the unit was tripped, which | | is expected with the partial loss of off-site power. Presently, the only | | major secondary equipment that is unavailable is associated with the loss of | | power to two of four non-vital 4 Kv buses. There is one shutdown Technical | | Specification in effect and that is associated with having only one off-site | | power source. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021