Event Notification Report for September 7, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/06/2001 - 09/07/2001 ** EVENT NUMBERS ** 38132 38266 38267 38268 38269 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38132 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 07/12/2001| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 05:21[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 07/11/2001| +------------------------------------------------+EVENT TIME: 23:30[EDT]| | NRC NOTIFIED BY: GENE MICHELSON |LAST UPDATE DATE: 09/06/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANTHONY DIMITRIADIS R1 | |10 CFR SECTION: | | |AINA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF AN EXCESSIVE ACCUMULATION OF WATER IN TWO UNDERGROUND FUEL OIL | | STORAGE TANKS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[An] excessive accumulation of water [was] discovered in both [the] D11 and | | D12 underground fuel oil storage tanks. [There was 33 inches of water in | | D11 and 22.5 inches of water in D12.] This event would prevent both diesel | | generators from fulfilling their required safety function. [Technical | | Specification 3.8.1.1, Actions 'b' and 'e,' were] entered, and reportability | | manual event SAF 1.8 [was also] entered." | | | | "Actions Taken: Water has been removed from both [the] D11 and D12 | | underground fuel oil storage tanks. [The licensee is] currently performing | | [an] operability determination." | | | | The licensee stated that the unit is remains in the 72-hour limiting | | condition for operation due to the ongoing operability determination. | | | | The licensee notified the NRC resident inspector. | | | | * * * RETRACTION ON 09/06/01 AT 1407 ET BY STAN GAMBLE TAKEN BY MACKINNON * | | * * | | | | Subsequent testing verified that the water level in both tanks was below the | | fuel oil transfer pump suction and that no water was found in the associated | | Day Tanks. | | | | Since no water had been nor would it have been transferred from the Fuel Oil | | Storage Tanks to the Day Tanks during operation of the Diesel Generators, a | | condition did not exist at the time of discovery that could have prevented | | the fulfillment of the safety function. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38266 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/06/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:52[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/06/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 06:00[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/06/2001| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MARK RING R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+RICHARD WESSMAN IRO | | NRC NOTIFIED BY: M. PITTMAN | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4 HOUR REPORT - NRC BULLETIN 91-01 | | | | The following is taken from a facsimile report: | | | | At 0600, on 9-06-01, the Plant Shift Superintendent (PSS) was notified that | | moisture sampling results on Unit 1 Cell 2 even R-114 system in building | | C-337 were above allowable limits of NCSA CAS-011. NCSA CAS-011 sets the | | limit for moisture content in R-114 at 1760 ppm. The sample results showed | | that the actual moisture content in C-337 Unit 1 Cell 2 even R-114 system | | was 2100 ppm. | | | | Set point calculations for the R-114 moisture meters used by Cascade | | personnel to determine the moisture content of R-114 for Cascade coolant | | systems was found biased low with respect to moisture content. The meters | | are used to detect high moisture levels in the R-114. An R-114 system | | containing a high moisture content is required to be independently verified | | drained prior to removing the fluorinating process environment. Since the | | setpoint calculation was potentially in error, R-114 with a potentially high | | moisture content was not immediately drained according to NCSA CAS-002. | | This control prevents a moderating environment within the process gas system | | from exceeding 50% relative humidity at 70 degrees F. | | | | The NRC Acting Senior Resident has been notified of this event. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | The final determination of whether the moisture content limit has been | | exceeded cannot be made until the moisture meter "as-found" calibration data | | can be reviewed. This data a not currently available. However, the plant | | is pro-actively taking the compensatory actions as though the moisture meter | | were in error until such time as the calibration data can be reviewed as a | | final determination made. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR: | | In order for a criticality to be possible a fissile deposit containing | | greater than a critical mass would have to absorb greater than 10 kg of | | water. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC: | | Two controls on moderation. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS): | | No known deposits of concern at this time. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | Double contingency for this scenario is established by implementing two | | controls on moderation. | | | | The first leg of double contingency is based on immediately draining the | | R-114 upon determination that it contains a high moisture content. The set | | point calculation derived for the R-114 moisture meter was biased low with | | respect to moisture content. Due to the set point calculation error the | | R-114 system was not immediately drained as required by the NCSA which may | | have allowed an unknown quantity of water to enter the process system. | | Since the quantity of water in-leakage to the process system cannot be | | quantified the process condition was exceeded and double contingency was not | | maintained. | | | | The second leg of double contingency is based on independently verifying the | | immediate draining of the R-114 upon determining that it contains a high | | moisture content. The set point calculation derived for the independent | | R-114 moisture meter was biased low with respect to moisture content. Due | | to the set point calculation error the R-114 system was not independently | | verified as being immediately drained as required by the NCSA which may have | | allowed an unknown quantity of water to enter the process system. Since the | | quantity of water in-leakage to the process system cannot be quantified the | | process condition was exceeded and double contingency was not maintained. | | | | Since double contingency is based on two controls on moderation, double | | contingency was not maintained. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | The R-114 system is in the process of being drained. The process system | | will then be sampled for R-114 per CP3-CO-C02029 and appropriate actions | | contained therein will be performed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38267 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 09/06/2001| |LICENSEE: SMURFIT-STONE CONTAINER CORP. |NOTIFICATION TIME: 15:15[EDT]| | CITY: PORT ST. JOE- REGION: 2 |EVENT DATE: 08/29/2001| | COUNTY: STATE: FL |EVENT TIME: 12:00[EDT]| |LICENSE#: 0194-1 AGREEMENT: Y |LAST UPDATE DATE: 09/06/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN MONNINGER R2 | | |M. WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLEY ADAMS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT: MISSING NDC DENSITY GAUGE | | | | | | Today Smurfit-Stone Container Corporation faxed a copy of a letter to the | | State of Florida Bureau of Radiation Control stating that a device was | | missing; NDC, Mass Monitor, Model # 104. The former Florida Coast Paper | | facility had several fixed radioactive sources when it went bankrupt in | | 1998. It was purchased by Smurfit-Stone and the radioactive sources have | | all been removed with the exception of this source. It was a portable | | device that had been kept in a locked steel toolbox within a locked | | laboratory. It was last seen in late June. Numerous contractors have been | | on site engaged in the removal of equipment prior to mill demolition. Mill | | personnel have searched the mill repeatedly and now suspect that the device | | was removed by one of the contractors. All facilities that have received | | equipment from the mill have been asked to search for the device. Florida | | is investigating this incident. Florida incident number for this event is | | FL01-095. The NDC Mass Monitor contained 30 millicuries of americium-241. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38268 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COLUMBIA GENERATING STATIREGION: 4 |NOTIFICATION DATE: 09/07/2001| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 00:47[EDT]| | RXTYPE: [2] GE-5 |EVENT DATE: 09/06/2001| +------------------------------------------------+EVENT TIME: 17:38[PDT]| | NRC NOTIFIED BY: WILLIAM BAKER |LAST UPDATE DATE: 09/07/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LINDA SMITH R4 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM MADE INOPERABLE | | | | "Columbia Generating Station Reactor Core Isolation Cooing (RCIC) system has | | been isolated and made inoperable per Technical Specification 3.5.3 and | | unavailable due to manual closure of the RCIC turbine trip valve. The | | manual closure of the RCIC turbine trip valve was required due to the loss | | of automatic trip capability of the turbine trip valve [due to a solenoid | | failure]. This loss of automatic trip capability under postulated | | conditions could cause a water hammer event significant enough to threaten | | primary containment. | | | | "The RCIC system is a single train system and is listed in plant procedures | | as an Engineered Safety Feature (ESF). | | | | "The RCIC system will function automatically or manually to inject water | | into the RPV if manually returned to service." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38269 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/07/2001| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 03:30[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/07/2001| +------------------------------------------------+EVENT TIME: 00:24[CDT]| | NRC NOTIFIED BY: MICHAEL FITZPATRICK |LAST UPDATE DATE: 09/07/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MARK RING R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 72 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM DUE TO 2 LOW PRESSURE HEATER STRINGS ISOLATING | | | | The following is taken from a facsimile report: | | | | This report is being made per 10CFR50.72(b)(2)(iv)(B) RPS actuation (scram) | | (4 hour notification for U-2). | | | | At 12:24 AM CDT, Friday 9/7/01, U-2 was manually scrammed. The initiating | | event was a loss of 2 of 3 Low Pressure Feedwater Heater Strings. A high | | level condition was initially received in the 21A Low Pressure Heater, which | | caused the Condensate System inlet and outlet isolation valves to the 2A Low | | Pressure Heater String to close. Subsequently, a high level condition was | | also received in the 21C Low Pressure Heater, which caused the Condensate | | System inlet and outlet isolation valves to the 2C Low Pressure Heater | | String to close. With a second Low Pressure Heater String isolated, Unit 2 | | was manually scrammed in accordance with LaSalle Procedure LOA-HD-201, | | "Heater Drain System Trouble". | | | | All systems operated as designed, There were no ECCS actuations or Primary | | Containment isolations. The lowest Reactor level reached was minus 20 inches | | (141 inches above the top of active fuel) and was recovered to normal level | | using feedwater. Reactor pressure responded normally. No Safety Relief | | Valves actuated. All Control Rods fully inserted. | | | | The NRC Resident Inspector has been notified. | | | | The cause of the Low Pressure Heater String loss is being investigated at | | this time. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021