The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for September 4, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           08/31/2001 - 09/04/2001

                              ** EVENT NUMBERS **

37902  38254  38255  38256  38257  38258  38259  38260  38261  38262  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37902       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER            REGION:  2  |NOTIFICATION DATE: 04/09/2001|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 11:08[EDT]|
|   RXTYPE: [3] B&W-L-LP                         |EVENT DATE:        04/09/2001|
+------------------------------------------------+EVENT TIME:        09:54[EDT]|
| NRC NOTIFIED BY:  RICHARD SWEENEY              |LAST UPDATE DATE:  09/03/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |CAUDLE JULIAN        R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION TO THE NATIONAL MARINE AND FISHERIES SERVICE AS A       |
| RESULT OF THE ENDANGERED SEA TURTLES NON-LETHAL TAKE LIMIT BEING EXCEEDED    |
|                                                                              |
| "On April 09, 2001 at 0940 the 40th non-lethal sea turtle take in the        |
| biennial period occurred.                                                    |
|                                                                              |
| "In accordance with Crystal River Unit #3 Operating License, Appendix B,     |
| Environmental Protection Plan (Non-Radiological),  'Endangered or threatened |
| sea turtles shall be protected in accordance with the Incidental Take        |
| Statement issued by the National Marine and Fisheries Service (NMFS).'  The  |
| NMFS has established numerical limits on live takes, lethal takes causally   |
| related to plant operation, and lethal takes not related to plant            |
| operations.                                                                  |
|                                                                              |
| "The NMFS must be notified within five days whenever:                        |
|                                                                              |
| a.  The 40th non-lethal take occurs in the biennial period, or               |
| b.  The third causally related mortality occurs in the biennial period, or   |
| c.   The sixth non-causally related mortality occurs in the biennial         |
| period.                                                                      |
|                                                                              |
| "The current biennial period for monitoring sea turtle takes began January   |
| 1, 2001.                                                                     |
|                                                                              |
| "Thus, in accordance with Crystal Unit #3 Administrative Instruction 571,    |
| Sea Turtle Rescue and Handling Guidance, the NMFS must be notified within    |
| five days.                                                                   |
|                                                                              |
| "In accordance with Crystal River Unit #3 Compliance Procedure 151, External |
| Reporting Requirements, this 40th non-lethal sea turtle take is Reportable   |
| as a 4-Hour Report under 10 CFR 50.72(b)(2)(xi) as this event is related to  |
| the protection of the environment for which a notification to other          |
| government agencies has been or will be made."                               |
|                                                                              |
| The licensee will inform the NRC resident inspector.                         |
|                                                                              |
| * * * UPDATE 0944EDT ON 4/10/01 FROM R. SWEENEY TO S. SANDIN * * *           |
|                                                                              |
| "On April 10, 2001 at 0859 the 41st non-lethal sea turtle take in the        |
| biennial period occurred."                                                   |
|                                                                              |
| The licensee informed the NRC resident inspector.  Notified R2DO(Julian).    |
|                                                                              |
| ***** UPDATE RECEIVED AT 0911 ON 04/17/01 FROM CHRISTOPHER PELLERIN TO LEIGH |
| TROCINE *****                                                                |
|                                                                              |
| The 42nd, non-lethal, sea turtle take in the biennial period occurred at     |
| 0810 on April 17, 2001.                                                      |
|                                                                              |
| The licensee notified the NRC resident inspector.  The NRC operations        |
| officer notified the R2DO (Ernstes).                                         |
|                                                                              |
| * * * UPDATE 1125 EDT ON 5/1/01 FROM DAVID SCHULKER TO FANGIE JONES * * *    |
|                                                                              |
| "On May 1, 2001 at 0805 a turtle was identified as the 43rd rescued, live    |
| sea turtle in this biennial period.  This sea turtle will be kept for a      |
| short observation period and then safely returned to the environment."       |
|                                                                              |
| The licensee will inform the NRC Resident Inspector and the National         |
| Wildlife and Fisheries Service.  Notified R2DO(Jay Henson).                  |
|                                                                              |
| * * * UPDATE ON 5/29/01 BY FERGUSON TO SANDIN * * *                          |
|                                                                              |
| On May 29, 2001 at 0943 two turtles were identified as the 44th and 45th     |
| rescued, Iive Sea turtles in this biennial period. These healthy sea turtles |
| will be kept for a short observation period and then safely returned to the  |
| environment.                                                                 |
|                                                                              |
|                                                                              |
| This is Reportable as a 4-Hour Report under 10 CFR 50.72 (b) (2) (xi) as     |
| this event is related to the protection of the environment for which a       |
| notification to other government agencies has been or will be made. This is  |
| an update to event 37902.                                                    |
|                                                                              |
| The NRC Resident Inspector was notified.  The REG2 RDO(Barr) was informed.   |
|                                                                              |
| * * * UPDATE 2014 EDT 6/4/2001 FROM RAWLS TAKEN BY STRANSKY * * *            |
|                                                                              |
| On June 4, 2001 at 1815, the 46th non-lethal sea turtle (Kemp's Ridley) take |
| in the biennial period occurred. The license has informed the NRC resident   |
| inspector.  Notified R2DO (Barr).                                            |
|                                                                              |
| * * * UPDATE 1315EDT ON 6/10/01 FROM CHARLES J. MORRIS TO S. SANDIN * * *    |
|                                                                              |
| On June 10, 2001 at 1100, the 47th non-lethal sea turtle take in the         |
| biennial period occurred. The license has informed the NRC resident          |
| inspector.  Notified R2DO (Bonser).                                          |
|                                                                              |
| * * * UPDATE 0952 ON 8/20/2001 FROM FERGUSON TAKEN BY STRANSKY * * *         |
|                                                                              |
| On August 20, 2001 at 0815, the 48th non-lethal sea turtle take in the       |
| biennial period occurred. The licensee as informed the NRC resident          |
| inspector. Notified R2DO (Payne).                                            |
|                                                                              |
| * * *  UPDATE 1216 ON 9/3/01 BY SCHULKER TO GOULD * * *                      |
|                                                                              |
| On September 3, 2001 at 0845 a turtle was identified as the 49th rescued,    |
| live sea turtle in this biennial period.  This turtle has an injury to the   |
| lower jaw and is being transported to the Clearwater Marine Science Station  |
| for treatment. It has not been determined at this time if the injury is      |
| casually related to Crystal River Operations.                                |
|                                                                              |
| This is Reportable as a 4-Hour Report under 10 CFR 50.72 (b) (2) (xi) as     |
| this event is related to the protection of the environment for which a       |
| notification to other government agencies has been or will be made. This is  |
| an update to event 37902.                                                    |
|                                                                              |
| The NTC Resident Inspector and  other government agencies will be notified.  |
|                                                                              |
| Notified Reg 2 RDO(Lesser)                                                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38254       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SALEM                    REGION:  1  |NOTIFICATION DATE: 08/31/2001|
|    UNIT:  [1] [] []                 STATE:  NJ |NOTIFICATION TIME: 08:35[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        08/31/2001|
+------------------------------------------------+EVENT TIME:        04:55[EDT]|
| NRC NOTIFIED BY:  FORD                         |LAST UPDATE DATE:  08/31/2001|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |DAVID LEW            R1      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NATIONAL MARINE FISHERIES SERVICE NOTIFIED OF THE RECOVERY OF A DEAD         |
| LOGGERHEAD TURTLE                                                            |
|                                                                              |
| A deceased endangered loggerhead turtle was recovered from the circulating   |
| water intake trash bars.  Based on the condition of the turtle, it was       |
| determined to have been deceased for some time and the cause was not         |
| directly related to being impinged on the circulating water (cw) trash       |
| bars.                                                                        |
|                                                                              |
| The NRC Resident Inspector will be notified along with the National Marine   |
| Fisheries Service                                                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   38255       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  MAYO CLINIC                          |NOTIFICATION DATE: 08/31/2001|
|LICENSEE:  SAINT MARYS HOSPITAL                 |NOTIFICATION TIME: 09:19[EDT]|
|    CITY:  ROCHESTER                REGION:  3  |EVENT DATE:        08/30/2001|
|  COUNTY:                            STATE:  MN |EVENT TIME:        08:55[CDT]|
|LICENSE#:  22-26031-01           AGREEMENT:  N  |LAST UPDATE DATE:  08/31/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JOHN MADERA          R3      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  CLASSIC                      |                             |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33(a)            MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MEDICAL MISADMINISTRATION DURING THE USE OF A GAMMA STEREO TACTIC UNIT       |
|                                                                              |
| A CANCER PATIENT WAS UNDERGOING THERAPEUTIC TREATMENTS AND RECEIVED A        |
| COBALT-60 DOSE GREATER THAN 39% OF THE PRESCRIBED DOSE.  THE PRESCRIBED DOSE |
| WAS 20 GRAYS AND THE ACTUAL DOSE WAS 27.8 GRAYS.   CAUSE OF THE              |
| MISADMINISTRATION WAS DUE TO THE TIME OF TREATMENT BEING INCORRECTLY ENTERED |
| IN THE TREATMENT UNIT.  THE PATIENT AND PHYSICIAN WERE NOTIFIED.             |
| THERE IS NO ANTICIPATION OF ANY ADVERSE AFFECT.                              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   38256       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  KANSAS DEPT OF HEALTH & ENVIRONMENT  |NOTIFICATION DATE: 08/31/2001|
|LICENSEE:  UNIVERSITY OF KANSAS HOSPITAL AUTHORI|NOTIFICATION TIME: 13:30[EDT]|
|    CITY:  KANSAS CITY              REGION:  4  |EVENT DATE:        08/31/2001|
|  COUNTY:                            STATE:  KS |EVENT TIME:             [CDT]|
|LICENSE#:  18-C801               AGREEMENT:  Y  |LAST UPDATE DATE:  08/31/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |GAIL GOOD            R4      |
|                                                |SUSAN FRANT          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TOM CONLEY                   |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - MEDICAL MISADMINISTRATION                           |
|                                                                              |
| The wrong radiopharmaceutical was administered to a patient, resulting in a  |
| dose of 9 rem (90 mSv) to the lower large intestine. A technician had picked |
| up two doses:  one Tc-99m dose (prescribed for the patient) and one Ga-67    |
| dose. The technician then engaged in a conversation with another individual, |
| became distracted and inadvertently administered the Ga-67 dose to the       |
| patient.                                                                     |
|                                                                              |
| The hospital will be submitting a written report to the state within 15      |
| days.                                                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   38257       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TENNESSEE DIV OF RAD HEALTH          |NOTIFICATION DATE: 08/31/2001|
|LICENSEE:  HENRY COUNTY MEDICAL CENTER          |NOTIFICATION TIME: 16:10[EDT]|
|    CITY:  PARIS                    REGION:  2  |EVENT DATE:        08/31/2001|
|  COUNTY:                            STATE:  TN |EVENT TIME:             [EDT]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  08/31/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |MARK LESSER          R2      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DEBRA SHULTS (FACSIMILE)     |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT                                                       |
|                                                                              |
| "The licensee called to report that 105 iodine-125 seeds totaling 336        |
| millicuries were missing. The seeds were delivered to the hospital by        |
| Airborne Express on 8/29/01 and records indicate they were received by a     |
| purchasing clerk at approximately 2:00 p.m.. A prostate implant was          |
| scheduled for the morning of 8/31/01. When the radiation therapy             |
| technologist went to retrieve the seeds from the nuclear medicine            |
| department. the nuclear medicine technologist was unaware that any seeds had |
| been delivered to the hospital. The clerk who signed for the seeds is not at |
| the hospital today and on vacation until Tuesday. The housekeeping staff     |
| member who cleaned the area on 8/29/01 does not recall seeing any container  |
| fitting the description of the one in which the seeds were packaged and      |
| delivered. The Nuclear Medicine Department and the Radiology Department have |
| been searched and the package not located. The dumpsters were emptied and    |
| sent to the landfill prior to discovery of the missing sources. An           |
| investigation is underway at the hospital. State radiation control personnel |
| will conduct an onsite investigation."                                       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   38258       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TEXAS DEPARTMENT OF HEALTH           |NOTIFICATION DATE: 08/31/2001|
|LICENSEE:  ATSER CORPORATION                    |NOTIFICATION TIME: 17:15[EDT]|
|    CITY:  HOUSTON                  REGION:  4  |EVENT DATE:        08/30/2001|
|  COUNTY:                            STATE:  TX |EVENT TIME:        12:15[CDT]|
|LICENSE#:  L04741                AGREEMENT:  Y  |LAST UPDATE DATE:  08/31/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |GAIL GOOD            R4      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  HELEN WATKINS (FACSIMILE)    |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - STOLEN NUCLEAR GAUGE FOUND                          |
|                                                                              |
| "A yellow box with a Yellow II label was found and Hazmat responded to the   |
| scene. The box was found abandoned in a dumpster at an apartment building.   |
| Hazmat's radiation survey meters indicated the presence of radioactive       |
| material. However, the radiation levels indicated were inconsistent with     |
| readings expected from a gauge. It was later determined the Hazmat team had  |
| confused �R with mR and the readings were much lower than earlier believed.  |
|                                                                              |
| "The city requested assistance to identify the owner of the gauge and        |
| possibly to take possession of the gauge. Because Houston was recently       |
| flooded, the city's basement area (with a lead lined vault was severely      |
| damaged and could not be used to temporarily secure the gauge.               |
|                                                                              |
| "It was determined that the gauge belonged to ATSER Corporation (L04741). A  |
| former employee reported carrying it in his vehicle and it was stolen along  |
| with the vehicle. The company is still investigating. The gauge is a         |
| Humboldt, s/n 3612. The source serial number of the Cs-137 source is 9842GQ  |
| and the Am-241/Be source is NJ03905."                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38259       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 09/01/2001|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 00:05[EDT]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        08/31/2001|
+------------------------------------------------+EVENT TIME:        23:08[EDT]|
| NRC NOTIFIED BY:  JAMES ABRAHAM                |LAST UPDATE DATE:  09/01/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 1-HOUR SECURITY REPORT INVOLVED SAFEGUARDS SYSTEM DEGRADATION                |
|                                                                              |
| Safeguards system degradation related to detection of area boundary.         |
| Immediate compensatory measures taken upon discovery.  The licensee will     |
| inform the NRC resident inspector.  Contact the Headquarters Operations      |
| Center for additional details.                                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38260       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 09/01/2001|
|    UNIT:  [1] [2] []                STATE:  FL |NOTIFICATION TIME: 08:45[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        09/01/2001|
+------------------------------------------------+EVENT TIME:        08:15[EDT]|
| NRC NOTIFIED BY:  JOE HESSLING                 |LAST UPDATE DATE:  09/01/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION TO FLORIDA STATE AND WILDLIFE INVOLVING INJURED TURTLE  |
|                                                                              |
| "Notification being made due to a State Notification (Florida State and      |
| Wildlife) at 0815.                                                           |
|                                                                              |
| "Notification made due to injured immature Loggerhead sea turtle being       |
| transported offsite for rehabilitation.                                      |
|                                                                              |
| "Notification to offsite agency requires NRC notification pursuant to        |
| 10CFR50.72(b)(2)(xi)."                                                       |
|                                                                              |
| The licensee will inform the NRC resident inspector.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38261       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DUANE ARNOLD             REGION:  3  |NOTIFICATION DATE: 09/02/2001|
|    UNIT:  [1] [] []                 STATE:  IA |NOTIFICATION TIME: 17:52[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        09/02/2001|
+------------------------------------------------+EVENT TIME:        13:08[CDT]|
| NRC NOTIFIED BY:  MIKE HAUNER                  |LAST UPDATE DATE:  09/02/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |PATRICK HILAND       R3      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HPCI SYSTEM DECLARED INOPERABLE                                              |
|                                                                              |
| "The High Pressure Coolant Injection (HPCI) steam supply line drain trap     |
| developed a steam leak that required the drain trap to be manually           |
| isolated.                                                                    |
|                                                                              |
| "At 1308, shortly after isolating the steam trap, the HPCI steam supply      |
| drain pot high level alarm was received; the HPCI system was declared        |
| inoperable and a 14-day LCO was entered per Technical Specification 3.5.1    |
| Condition F.                                                                 |
|                                                                              |
| "At 1326, the HPCI turbine auto start feature was defeated to mitigate the   |
| potential damage to the turbine and other components from water in the steam |
| supply line.                                                                 |
|                                                                              |
| "Unplanned HPCI system inoperability is reportable under 50.72(b)(3)(v)(D)   |
| as a single train failure that could have prevented the fulfillment of a     |
| safety function of structures or systems to mitigate the consequences of an  |
| accident."                                                                   |
|                                                                              |
| The NRC resident inspector has been informed of this notification by the     |
| licensee.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38262       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 09/03/2001|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 22:02[EDT]|
|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        09/03/2001|
+------------------------------------------------+EVENT TIME:        17:28[CDT]|
| NRC NOTIFIED BY:  COVEYOU                      |LAST UPDATE DATE:  09/03/2001|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |PATRICK HILAND       R3      |
|10 CFR SECTION:                                 |JACK STROSNIDER      NRR     |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|ACCS 50.72(b)(2)(iv)(A)  ECCS INJECTION         |                             |
|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     M/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR MANUALLY SCRAMMED FROM 100% DUE TO LOW  VESSEL LEVEL                 |
|                                                                              |
| This report is being made per 10CFR50.72(b)(2)(iv)(B) RPS actuation (4 hour  |
| notification for U-2), 10CFR50.72(b)(2)(iv)(A) ECCS Injection/Actuation (4   |
| hour notification for Unit 2), and 10CFR50.72(b)(3)(iv)(A) System Actuation  |
| not including RPS (8 hour notification for Unit 1 and 2).                    |
|                                                                              |
| At 1728 CST. Monday, 9-3-01,U-2 was manually scrammed.  Initiating event     |
| appears to be a loss of Bus 241Y, which resulted in a loss of feedwater.     |
| The reactor was manually scrammed at approximately 20 inches before the      |
| automatic scram setpoint for low vessel water level.  All rods fully         |
| inserted.                                                                    |
|                                                                              |
| The Reactor Core Isolation Cooling (RCIC) and High-Pressure Core Spray       |
| (HPCS) systems automatically started and injected and restored Reactor       |
| Pressure  Vessel (RPV) level.                                                |
|                                                                              |
| A primary containment-level 2 isolation occurred and the Reactor             |
| Recirculation pumps tripped at minus 50 inches as expected.  Unit 1 was      |
| affected due to standby gas treatment auto start and the reactor building    |
| vent system isolation.                                                       |
|                                                                              |
| The lowest Reactor water level reached was minus 55 inches (106 inches above |
| the top of active fuel) as indicated by the Division 2 instrumentation and   |
| was recovered to normal level with RCIC and HPCS within a few minutes.       |
| Approximately 10,000 gallons of water was injected.                          |
|                                                                              |
| Bus 241Y was automatically re-energized from the (0) Common Diesel           |
| Generator.                                                                   |
|                                                                              |
| Dry-well pressure increased due to the expected loss of primary containment  |
| cooling.  The highest pressure reached was approximately (1) one psig.       |
| Primary Containment Cooling has been restored.  There are no indications of  |
| a leak inside the primary containment.                                       |
|                                                                              |
| RPV pressure is being controlled at 800 to 1000 psig by the use of RCIC.     |
| Main Steam Line drains, and manual operation of Safety Relief Valve (as      |
| necessary).  RPV level has been restored to normal and feedwater is being    |
| used.                                                                        |
|                                                                              |
| Subsequent in the Reactor Scram, the 2A RHR Pump failed to start when        |
| manually initiating from the Main Control Room (for suppression pool         |
| cooling).                                                                    |
|                                                                              |
| System isolations have been restored with exception of reactor water cleanup |
| and the Reactor Recirculation Hydraulic Power Units on U-2.                  |
|                                                                              |
| The station is taking action to investigate the cause of the initial loss of |
| 241Y and the unrelated failure to start of the 2A RHR pump.   At this time,  |
| there appears to be a blown fuse for the 241Y bus Under Voltage logic which  |
| prevented the 2A RHR pump from starting.                                     |
|                                                                              |
| The plant is stable.                                                         |
|                                                                              |
| The NRC resident inspector has been notified.                                |
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Page Last Reviewed/Updated Wednesday, March 24, 2021