Event Notification Report for August 30, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/29/2001 - 08/30/2001 ** EVENT NUMBERS ** 38246 38247 38248 38249 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38246 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 08/29/2001| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 06:25[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/29/2001| +------------------------------------------------+EVENT TIME: 04:04[CDT]| | NRC NOTIFIED BY: FRANK WEAVER |LAST UPDATE DATE: 08/29/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DALE POWERS R4 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 27 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANNED MANUAL REACTOR SCRAM TO REPAIR A REACTOR RECIRCULATION PUMP FLOW | | CONTROL VALVE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Grand Gulf Nuclear Station manually scrammed from 27% [core thermal power] | | in preparation to repair reactor recirculation pump 'A' flow control valve | | B33F060A. All control rods fully inserted, and all other safety systems | | responded as designed. Condensate booster pump 'A' tripped for no apparent | | reason. Investigation into why the 'A' condensate booster pump tripped is | | underway." | | | | The licensee notified the NRC resident inspector. | | | | * * * RETRACTED AT 1305 EDT ON 8/29/01 BY DAVID HANKS TO FANGIE JONES * * * | | | | The licensee is retracting this event notification. After further review, | | the licensee determined that the manual reactor scram was part of a | | pre-planned sequence of events and as such was not reportable under 10 CFR | | 50.72(b)(3)(iv)(A). | | | | The licensee notified the NRC Resident Inspector. The R4DO (Gail Good) has | | been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38247 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 08/29/2001| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 11:02[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 08/29/2001| +------------------------------------------------+EVENT TIME: 10:04[EDT]| | NRC NOTIFIED BY: MIKE GOBELI |LAST UPDATE DATE: 08/29/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID LEW R1 | |10 CFR SECTION: |JOHN TAPPERT NRR | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION |RICHARD ROSANO/NRR IAT | |DDDD 73.71 UNSPECIFIED PARAGRAPH |AARON DANIS/NMSS IAT | | |GREG SMITH/REGION 1 IAT | | |NADER MAMISH IRO | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING A 30-GALLON DIESEL OIL SPILL FROM A FREIGHT | | TRAIN WHICH DERAILED AND BREACHED THE PROTECTED AREA BOUNDARY | | | | A freight train derailed and breached the protected area boundary. There | | were no personnel injuries as a result of this event. However, 30 gallons | | of diesel oil spilled from the train. The oil was contained by trap rocks | | and did not reach receiving waters. | | | | Security personnel have been posted as a result of the protected area | | barrier breach, and fire protection personnel are currently on scene | | cleaning up the diesel oil spill. The licensee is in the process of | | notifying the Connecticut Department of Environmental Protection of the oil | | spill. The licensee also requested that local police investigate the cause | | of the train derailment. | | | | In addition to the initial 4-hour event report for the offsite notification, | | the licensee plans to call back with an update to include the reporting | | criterion for the breach in the protected area barrier. | | | | The licensee notified the NRC resident inspector and plans to notify | | applicable state and local officials. | | | | ***** UPDATE FROM MIKE GOBELI TO LEIGH TROCINE AT 1115 ON 08/29/01 ***** | | | | The licensee provided this update to include an additional 1-hour security | | reporting criterion to the initial 4-hour event report for the offsite | | notification. The licensee determined that this event was also reportable | | in accordance with 10 CFR 73.71(b)(1), Appendix G, I(1)(c), for a | | degradation or discovered vulnerability in a safeguards system that could | | allow unauthorized or undetected access to a protected area, controlled | | access area, or vital area. | | | | The NRC operations officer notified the R1DO (David Lew), NRR EO (John | | Tappert), IRO (Nader Mamish), NRR IAT (Richard Rosano), NMSS IAT (Aaron | | Danis), Region 1 IAT (Greg Smith), Region 1 (Curtis Cowgill), Headquarters | | OPA (Beth Hayden), and Region 1 OPA (Neil Sheehan). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38248 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 08/29/2001| |LICENSEE: SCHLUMBERGER |NOTIFICATION TIME: 12:53[EDT]| | CITY: REGION: 4 |EVENT DATE: 07/28/2001| | COUNTY: HARDIN STATE: TX |EVENT TIME: [CDT]| |LICENSE#: L01833 AGREEMENT: Y |LAST UPDATE DATE: 08/29/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GAIL GOOD R4 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HELEN WATKINS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - ABANDONED WELL LOGGING SOURCE | | | | The following is taken from a facsimile from Texas Department of Health | | Bureau of Radiation Control for Incident 7794: | | | | Date of Occurrence: 7/28/2001 | | | | Source Identification: 1.7 Ci, Cs-137, Density Source, serial # A1884 | | 16 Ci, Am-241:Be, Neutron Source, serial #A3001 | | | | Well Identification: Blackstone Energy | | Well: Carpenter Corp #1 | | Field: Wildcat, Hardin County Texas | | | | Seal Results: 500 ft. of cement on top of the tool at 10,700 ft. A | | deflection device and another 50 ft. of cement to be added at a later date | | when the well is completed. | | Recovery Attempts: Multiple attempts from 8/22/2000 to 8/25/2000 | | | | Depth of Sources: 1.7 Ci, Cs-137, Density Source, serial # A1884 @ 10,732 | | ft., 16 Ci, Am-241:Be, Neutron Source, serial #A3001 @10,714 ft. | | Depth of Well: 12,000 ft | | | | Identification: Plaque as required by Part 39 ordered and will be attached | | to the well. | | | | Initial Telephone Contact: Ruben Cortez, Texas Bureau of Radiation Control | | at 4:51 PM CDT on July 27, 2001 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38249 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 08/30/2001| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 06:23[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/29/2001| +------------------------------------------------+EVENT TIME: 22:55[EDT]| | NRC NOTIFIED BY: SCOTT RICHARDSON |LAST UPDATE DATE: 08/30/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN MADERA R3 | |10 CFR SECTION: | | |AINA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF ABNORMALLY LOW ESSENTIAL SERVICE WATER FLOW TO EACH DIESEL | | GENERATOR | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This is Scott Richardson calling from the DC Cook Nuclear Plant with an | | [8]-hour non-emergency notification in accordance with 10CFR50.72(b)(3)(v) | | for 'Any event or condition that at the time of discovery could have | | prevented the fulfillment of the safety function of structures or systems | | that are needed to: (A) Shut down the reactor and maintain it in a safe | | shutdown condition . . . . . . ' " | | | | "While performing an Essential Service Water (ESW) surveillance test on Unit | | 2, it was noted that the ESW flow to each Diesel Generator was abnormally | | low. This condition could have prevented the Diesel Generators from | | fulfilling their safety function. This condition was caused by sand and | | sediment in the ESW system and impacted both units." | | | | "Subsequent system flushes and valve cycling [have] eliminated the low flow | | condition in both Unit 1 and 2 Diesel Generators." | | | | "We will continue to monitor ESW system performance. Further investigation | | of this event is in progress to determine the root cause of the low flow | | anomaly." | | | | "Unit 2 will be [shutting] down [and] going to [Cold Shutdown] beginning in | | the next 3 hours." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021