Event Notification Report for August 23, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/22/2001 - 08/23/2001 ** EVENT NUMBERS ** 38225 38226 38227 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38225 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 08/22/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 08:07[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 08/22/2001| +------------------------------------------------+EVENT TIME: 05:08[EDT]| | NRC NOTIFIED BY: JOHN KRAKUSZESKI |LAST UPDATE DATE: 08/22/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM ON TURBINE TRIP DUE TO A LOAD REJECT | | | | "In accordance with 10 CFR 50.72 b (2) iv (B) a RPS actuation occurred | | following a generator load reject. Reactor Scram occurred at 0508 August | | 22, 2001 due to a turbine trip signal generated from the load reject. All | | six ERVs opened to control reactor pressure due to the initial load reject. | | A negative phase sequence was experience on 345 kV lines resulting in a trip | | of generator 86 G1& G2 relays. All control rods fully inserted following | | the automatic reactor scram. | | | | "Also, in accordance with 10 CFR 50.72 b (3) iv (A) an MSIV isolation was | | experienced when reactor pressure reached 850 psig with the mode switch in | | RUN as expected. The operator was in the process of taking the mode switch | | to SHUTDOWN but before this action was complete the MSIV isolation signal | | was generated as pressure dropped below 850 psig. High Pressure Coolant | | Injection initiated due to vessel level <53 inches as expected. Vessel | | level dropped to approximately 43 inches. Following the MSIV isolation | | level increased to the high-level trip setpoint as expected and was returned | | to the normal band. MSIVs were reopened for pressure control and a | | feedwater pump was restarted to augment vessel level control. | | | | "SOPs and EOPs were entered to stabilize the plant and control reactor | | pressure and level in normal bands. Cooldown to cold shutdown is in | | progress. Current reactor temperature is 439 degrees F with reactor | | pressure 361 psig. | | | | "All containment parameters are normal and offsite power is available. No | | maintenance or surveillance activities were occurring at the time of the | | Reactor Scram." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38226 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SC DIV OF HEALTH & ENV CONTROL |NOTIFICATION DATE: 08/22/2001| |LICENSEE: GEO ENVIRONMENTAL CONSULTANTS |NOTIFICATION TIME: 08:30[EDT]| | CITY: NORTH REGION: 2 |EVENT DATE: 08/20/2001| | COUNTY: STATE: SC |EVENT TIME: 12:30[EDT]| |LICENSE#: 060-0992-1 AGREEMENT: Y |LAST UPDATE DATE: 08/22/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |EDWARD MCALPINE R2 | | |FREDERICK STURZ NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MELINDA BRADSHAW | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - STOLEN TROXLER GAUGE | | | | The licensee is licensed out of North Carolina working under reciprocity in | | South Carolina. A Troxler Model 3430 moisture density gauge was stolen from | | the back of the company pickup truck while working at the North Auxiliary | | Air Force Base in North, South Carolina. The gauge was not secured or | | chained down when stolen. The gauge contains 40 mCi Am-241:Be and 8 mCi | | Cs-137. The North Police Department has been notified and is investigating. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38227 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HONEYWELL INTERNATIONAL, INC. |NOTIFICATION DATE: 08/22/2001| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 11:43[EDT]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 07/27/2001| | |EVENT TIME: [CDT]| | |LAST UPDATE DATE: 08/22/2001| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |RONALD GARDNER R3 | | DOCKET: 04003392 |JAMES CREED (R3) IAT | +------------------------------------------------+JOHN DAVIDSON (NMSS) IAT | | NRC NOTIFIED BY: HUGH ROBERTS |FRED BROWN NMSS | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING SHIPMENT OF CaF SETTLING POND CLEANUP WASTE | | | | A shipment of CaF settling pond waste left the site on July 25, 2001 and | | apparently did not arrive on July 27, 2001 at the Andrews County WCS in | | Texas. The shipment, one of several, consisted of 44,480 pounds of 80% CaF | | and 20% lime with less than 500 ppm natural uranium contained in it. The | | natural uranium is calculated at about 19 pounds total contained in the | | shipment. The driver reported that the shipment was delivered, but there is | | no paperwork to support the delivery. | | | | The licensee notified NRC Region 3 (Monte Phillips), the EPA, and the | | Illinois State Police, who are investigating. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021