Event Notification Report for August 13, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/10/2001 - 08/13/2001 ** EVENT NUMBERS ** 38196 38197 38198 38199 38200 38201 38202 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38196 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 08/10/2001| |LICENSEE: TERRACON ENGINEERING |NOTIFICATION TIME: 09:25[EDT]| | CITY: Dallas REGION: 4 |EVENT DATE: 08/09/2001| | COUNTY: STATE: TX |EVENT TIME: [CDT]| |LICENSE#: L05268 AGREEMENT: Y |LAST UPDATE DATE: 08/10/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN HUMBOLDT 5001C NUCLEAR GAUGE | | | | | | The gauge was lost during the hours of darkness July 15-16, 2001, from the | | back of a truck that was parked overnight at the home of the driver. The | | gauge and it's transport case were removed from a parked pickup truck by | | cutting the chain securing the gauge to the bed of the truck. Also stolen | | during this incident was the operator's toolbox and assorted hand tools. | | The gauge is a Humboldt Model 5001C, Serial # 2606, containing two | | radioactive sources: 10 millicuries of cesium-137, Serial #6171GQ; and 40 | | millicuries of americium-241;Be, Serial # NJ02767. A police report was | | filed on July 16, 2001, with the Dallas Police Department (Report # | | 0551265-K). A press release offering a $250 reward for the return of the | | gauge was run in the Dallas Morning News for two days. The gauge has not | | been recovered as of this date. The licensee has been cited for failure to | | maintain the gauge under constant surveillance. The state of Texas has | | informed the Radiation Control authorities in Mexico, Arizona, New Mexico, | | Arkansas, and Louisiana, as well as the Humboldt Radiation Safety Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38197 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 08/10/2001| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 11:21[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/10/2001| +------------------------------------------------+EVENT TIME: 11:15[EDT]| | NRC NOTIFIED BY: LEWIS |LAST UPDATE DATE: 08/10/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANN MARIE STONE R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |98 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION SHUTDOWN DUE TO TWO AUXILIARY FEEDWATER PUMPS BEING | | INOPERABLE. | | | | | | Commenced Unit 2 plant shutdown to comply with Technical Specification | | 3.7.1.2.b: Two Auxiliary Feedwater pumps inoperable. Unit 2 Turbine Driven | | Auxiliary Feedwater pump was inoperable due to scheduled maintenance. Unit | | 2 "2 East" Motor Driven Auxiliary Feedwater pump was declared inoperable due | | to a failure of associated room cooling (room cooler inoperable) required by | | administrative procedure PMP 4030.001.001, Impact of Safety Related | | Ventilation on the Operability of Technical Specification Equipment. All | | other systems fully are operable. | | | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38198 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HONEYWELL INTERNATIONAL, INC. |NOTIFICATION DATE: 08/10/2001| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 11:24[EDT]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 08/10/2001| | |EVENT TIME: 09:45[CDT]| | |LAST UPDATE DATE: 08/10/2001| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |ANNE MARIE STONE R3 | | DOCKET: 04003392 |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: W. LESSIG | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SMALL URANIUM HEXAFLUORIDE RELEASE ONSITE | | | | The licensee reported that from 0945 to 0950 CDT, a small UF6 release | | occurred in the feeds material building. No material left the site, nor did | | the licensee declare an Alert. Two individuals were exposed to fumes from | | the leak. Those individuals were treated with oxygen at the facility and | | transported to a local hospital. The UF6 leak has been stopped. | | | | The exact quantity of material released has yet to be determined. The | | licensee is currently conducting an investigation of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38199 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 08/10/2001| | UNIT: [1] [2] [3] STATE: CT |NOTIFICATION TIME: 13:18[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 08/10/2001| +------------------------------------------------+EVENT TIME: 10:15[EDT]| | NRC NOTIFIED BY: GENE OLSON |LAST UPDATE DATE: 08/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | |2 N Y 92 Power Operation |92 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANNED OFFSITE NOTIFICATION REGARDING A FISH KILL IN THE DISCHARGE QUARRY | | DUE TO A RECENT SUSTAINED HEAT WAVE IN THE NORTHEAST | | | | The following text is a portion of a facsimile received from the licensee: | | | | "A visual inspection by Millstone [station biologists] on August 10, 2001, | | revealed approximately 50 dead [Tautog] (blackfish) in the discharge quarry | | by the fish barrier. A subsequent dive into the quarry by station | | biologists [revealed] 2 additional dead Tautog along the fish barrier. No | | additional moralities or other species were found on the bottom of the | | quarry." | | | | "The fish most likely died as a result of the sustained elevated | | temperatures during the week of August 6, 2001, experienced throughout New | | England and Connecticut. Intake water temperatures have risen above 70 | | degrees F with discharge temperatures about 98 degree F. Water temperatures | | in the quarry have climbed to above 90 degrees F at times during the week. | | Tautog are known to have decreased resistant when water temperatures are | | above 90 degrees F." | | | | "Station [biologists] continue to monitor fish in the quarry." | | | | The licensee stated that there was nothing unusual about the temperature | | deltas across the condensers and that discharge temperatures are normal. | | The licensee also stated that load has been reduced on Unit 2 in order to | | keep condenser pressure below the condenser low pressure alarm setpoint and | | to maintain discharge temperatures within acceptable limits. The discharge | | temperatures for Unit 3 were reported to be normal with the unit at full | | power. | | | | The licensee plans to notify the NRC resident inspector and the State | | Department of Environmental Protection. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38200 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 08/10/2001| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 19:52[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 08/10/2001| +------------------------------------------------+EVENT TIME: 18:10[EDT]| | NRC NOTIFIED BY: ROSS MOONITZ |LAST UPDATE DATE: 08/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 84 Power Operation |84 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF GREATER THAN 25% OF THE EMERGENCY PREPAREDNESS SIRENS DUE TO POWER | | OUTAGES FROM ELECTRICAL STORMS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[A total of 26 out of] 97 emergency preparedness sirens (>25%) are out of | | service due to power outages from electrical storms. [This includes 20 out | | of] 27 in York County, 2 in Herford County, 2 in Lancaster County, 1 in | | Cecil County, and 1 in Chester County. Plans are in progress to restore | | power." | | | | The licensee reported that all systems functioned as required and that there | | was nothing unusual or misunderstood. The licensee also reported that there | | was no loss of offsite power. | | | | The licensee notified the NRC resident inspector. | | | | ***** UPDATE FROM JACK POPIELARSKI TO LEIGH TROCINE RECEIVED AT 2101 ON | | 08/10/01 ***** | | | | The licensee also notified York County. The NRC operations officer notified | | the R1DO (Holody). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38201 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 08/10/2001| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 23:02[EDT]| | RXTYPE: [1] GE-2 |EVENT DATE: 08/10/2001| +------------------------------------------------+EVENT TIME: 21:15[EDT]| | NRC NOTIFIED BY: ERIC DEMONCH |LAST UPDATE DATE: 08/10/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 84 Power Operation |84 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNPLANNED REACTOR PROTECTION SYSTEM (RPS) SYSTEM/SAFETY SYSTEM ACTUATIONS | | WHILE CRITICAL | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[The unit] received [an] isolation of the [transverse incore probe (TIP)] | | purge system and the offgas system during [an] electrical transient on the | | 230kV distribution system. [The licensee believes] the isolations were | | caused by the voltage fluctuations felt in the plant from the grid. Since | | the TIP purge isolation is processed through [the reactor protection system | | (RPS)] and offgas from the offgas [radiation] monitors, this falls under | | actuation of a safety system while critical." | | | | "[The licensee] reset isolations and restored systems to normal." | | | | The licensee stated that the isolation signals that were processed did not | | show up on any alarms. Alarms were received but nothing specific to | | indicate the isolations. This may have been due to voltage | | fluctuations/losses as a result of power/instrument panels that transferred | | to their alternate power supplies. The voltage fluctuations on the in-house | | 4160V buses were attributed to the electrical transient on the 230kV | | distribution system. | | | | There was severe weather in the area at the time of this event. As a | | result, one of two 230kV outgoing power lines and both 34.5kV feed lines | | were lost. All of these lines have since been returned to service. The | | licensee stated that offsite power was never lost because one 230kV line | | remained available to backfeed/supply the 34.5kV buses. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38202 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 08/12/2001| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 12:16[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/12/2001| +------------------------------------------------+EVENT TIME: 07:46[CDT]| | NRC NOTIFIED BY: DEAN CURTLAND |LAST UPDATE DATE: 08/12/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE MARIE STONE R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM DUE TO DECREASING REACTOR WATER LEVEL AND GROUP 1 | | ISOLATION DUE TO LOW REACTOR PRESSURE WHILE IN RUN | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 07:46:00 [CDT], a reactor water low-level alarm was received. The | | reactor operator verified the low-level condition and took manual control of | | feedwater level control. The operator matched feedwater and steam flow. At | | 07:46:28 [CDT], the 'B' feedwater pump tripped on low suction pressure. A | | manual scram was inserted at 07:46:42 [CDT] due to lowering reactor water | | level. Level dropped below 170 [inches] on the reactor scram [as expected], | | and [Group 2, 3, and 4 isolations] were received. All isolations went to | | completion. At 07:47:48 [CDT], a Group 1 isolation was received on the 850 | | psig low reactor pressure in Run isolation signal. The operator was in the | | process of [taking] the mode switch [out of] Run, but the isolation occurred | | before this action could be completed. All [main steam isolation valves] | | closed on the Group 1 isolation signal. Reactor level increased to the high | | level trip following the reactor scram, as expected, and the 'A' feedwater | | pump tripped. Due to the Group 1 isolation, the operating crew elected to | | manually initiate Low Low Set pressure control using the safety relief | | valves. A relief valve was opened, arming Low Low Set, and the two valves | | lowered reactor pressure to 900 psig. The Group 1 was reset, and main steam | | line drains to the condenser are being used to control pressure. The 'A' | | feedwater pump high level trip has been reset and is maintaining level." | | | | "All systems responded as expected. The plant is currently in Hot Shutdown | | at 800 psig. Plans are being reviewed to determine the length of the forced | | outage. Preliminary investigations indicate that the 'B' feedwater pump | | minimum flow valve may have failed open to initiate the event." | | | | The licensee stated that there were no maintenance or surveillance | | activities ongoing at the time of the event. All control rods fully | | inserted following the manual reactor scram. All containment parameters are | | currently normal, and offsite power is available. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021