Event Notification Report for July 17, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/16/2001 - 07/17/2001 ** EVENT NUMBERS ** 38142 38143 38144 38145 38146 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38142 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 07/15/2001| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 23:32[EDT]| | RXTYPE: [3] CE |EVENT DATE: 07/15/2001| +------------------------------------------------+EVENT TIME: 21:58[CDT]| | NRC NOTIFIED BY: RAY PELLEGRIN |LAST UPDATE DATE: 07/16/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: ALERT |CHUCK CAIN R4 | |10 CFR SECTION: |TAD MARSH NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |NADER MAMISH IRO | | |SAM COLLINS NRR | | |JIM MULLINS EPA | | |CANUPP FEMA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ALERT DECLARED DUE TO TOXIC GAS RELEASE NEAR PLANT SITE | | | | The licensee declared an Alert (EAL EP-4-010 "Toxic Chemical Contingency") | | due to an anhydrous ammonia release at the Occidental Chemical facility | | located near the site. The licensee reported that no ammonia has been | | detected onsite; however, personnel sheltering has been implemented. The | | release is ongoing and the chemical facility cannot estimate when the | | release will be secured. The NRC entered Monitoring at 0012EDT on 7/16/01. | | | | * * * UPDATE 0300EDT ON 7/16/01 FROM LICENSEE COMMUNICATOR TO S.SANDIN * * | | * | | | | The licensee terminated the Alert at 0200CDT after verifying that all | | exiting conditions were satisfied. The licensee informed the NRC resident | | inspector and will inform state/local agencies. The NRC exited Monitoring | | at 0315EDT on 7/16/01. Notified FEMA(Canupp), DOE(Stambaugh), | | EPA-DOT(Loreck), USDA(Conley) and HHS-CDC(Cruz). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38143 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 07/16/2001| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 11:20[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/16/2001| +------------------------------------------------+EVENT TIME: 09:58[EDT]| | NRC NOTIFIED BY: BILL MASON |LAST UPDATE DATE: 07/16/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAY HENSON R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING MAINTENANCE | | | | "The channel 2 of the 2B streamline pressure was in test. The channel 3 of | | the 2B streamline pressure was taken out of service (transmitter). This | | resulted in meeting the logic for main streamline isolation (2/3). This | | resulted in a reactor trip on overtemperature delta temperature. Auxiliary | | feedwater autostarted due to decreasing steam generator water levels. This | | event started as a result of preventative maintenance of steam generator | | pressure 2B channel 2." | | | | All rods fully inserted. Unit 2 is stable in mode 3 at 2235 psig and 556 | | degrees F with decay heat removal bypassing the main streamline isolation | | valves to the main condenser. Efforts are underway to restore main | | feedwater and secure the operating auxiliary feedwater pumps (both | | electrical and the turbine driven). During the transient all three primary | | PORVs lifted and reseated while secondary safety valves also cycled. There | | is no known primary-to-secondary tube leakage. All emergency equipment is | | available, if needed. The licensee informed the NRC resident inspector and | | does not plan a press release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38144 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 07/16/2001| | UNIT: [1] [2] [] STATE: GA |NOTIFICATION TIME: 14:51[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/16/2001| +------------------------------------------------+EVENT TIME: 10:33[EDT]| | NRC NOTIFIED BY: DORMAN |LAST UPDATE DATE: 07/16/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JAY HENSON R2 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD A MAJOR LOSS OF OFFSITE PUBLIC ALERTING SIREN SYSTEM | | | | While performing the weekly siren test, 35 of 47 sirens failed to respond. | | The weekly test was performed at 1033 EDT. Preliminary investigation | | suggests a problem with the sirens electronic memory chip. Troubleshooting | | and repairs are in progress. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38145 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NORTECH ENVIRONMENTAL |NOTIFICATION DATE: 07/16/2001| |LICENSEE: NORTECH ENVIRONMENTAL |NOTIFICATION TIME: 16:36[EDT]| | CITY: FAIRBANKS REGION: 4 |EVENT DATE: 07/16/2001| | COUNTY: STATE: AK |EVENT TIME: 08:00[YDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 07/16/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID GRAVES R4 | | |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHEEK | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NORTECH ENVIRONMENTAL REPORTED THAT AN X-RAY FLUORESCENCE DEVICE WAS STOLEN | | FROM THEIR OFFICES | | | | The device was stolen sometime this past weekend, but was just discovered | | this morning at 0800 YDT to be missing. The device was a Niton XL model 309 | | serial #U1002 containing 14 millicuries of cadmium-109 (serial #NR0853). | | This device was a hand held device used to analyze for lead in paint. The | | local police and Niton have been notified. The State will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38146 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TENNESSEE VALLEY AUTHORITY |NOTIFICATION DATE: 07/16/2001| |LICENSEE: TENNESSEE VALLEY AUTHORITY |NOTIFICATION TIME: 16:57[EDT]| | CITY: MUSCLE SHOALS REGION: 2 |EVENT DATE: 07/13/2001| | COUNTY: STATE: AL |EVENT TIME: [CDT]| |LICENSE#: 01-06113-04 AGREEMENT: Y |LAST UPDATE DATE: 07/16/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAY HENSON R2 | | |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KNUETTEL / FLANIGAN | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE REPORTED THE RELEASE OF CONTAMINATED MATERIAL | | | | On 7/13/01 two 30 gallon trash cans containing expendable contaminated lab | | items such as pipette tips, gloves, empty bottles, beakers, etc. were | | emptied into a dumpster. These items were at very low levels and had been | | collected in the two trash cans since January. The typical analysis that is | | done in the laboratory is on nuclear plant effluent samples from which these | | items received their contamination. Only the items used to handle the | | effluent sample material were discarded in the two trash cans. The material | | itself was not disposed in these trash cans. The dumpster was taken to the | | Hillsboro landfill in Lawrence County, AL this morning. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021