Event Notification Report for May 9, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/08/2001 - 05/09/2001 ** EVENT NUMBERS ** 37970 37971 37972 37973 37974 37975 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37970 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NEB DIV OF RADIOACTIVE MATERIALS |NOTIFICATION DATE: 05/07/2001| |LICENSEE: NEB PUBLIC POWER DISTRICT |NOTIFICATION TIME: 16:22[EDT]| | CITY: SUTHERLAND REGION: 4 |EVENT DATE: 05/01/2001| | COUNTY: STATE: NE |EVENT TIME: [CDT]| |LICENSE#: NE-10-03-03 AGREEMENT: Y |LAST UPDATE DATE: 05/08/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JEFF SHACKELFORD R4 | | |LARRY CAMPER NMSS | +------------------------------------------------+SUSAN FRANT NMSS | | NRC NOTIFIED BY: JOHN FASSELL | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT | | | | The event took place at a coal plant where a nuclear gauge is installed on a | | coal chute. Not following established maintenance procedures led to workers | | entering the chute with the source exposed. A field of approximately 450 | | mr/hr was created. Whole body exposure was calculated based on a five hour | | stay time resulting in an estimate of 2.25 Rem for the most exposed | | individual. Two other individuals were involved with lower total exposure. | | | | | | The source involved is believed to be Cs-137 with an activity between 100 | | and 200 mCi. | | | | * * * UPDATE ON 05/08/01 AT 1429 ET BY JOHN FASSELL TAKEN BY MACKINNON * * | | * | | | | Four workers were exposed instead of three and all four of the workers were | | radiation workers for the Neb Public Power District. Calculated whole body | | radiation exposure to the four workers: 2250 mrem, 1361 mrem, 611 mrem, and | | 450 mrem. The whole body dose was based on total exposure time multiplied | | by the maximum measured rate at the beam port, 450 mrem/hr. The individuals | | were approximately one foot away from the beam port | | | | The operations center informed the R4DO (Shackelford) and NMSS EO (Hickey). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37971 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 05/08/2001| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 01:52[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/08/2001| +------------------------------------------------+EVENT TIME: 00:09[EDT]| | NRC NOTIFIED BY: VEITCH |LAST UPDATE DATE: 05/08/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 22 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WAS MANUALLY SCRAMMED FROM 22% POWER DUE TO FAILURE OF RECIRC PUMP | | TO RESTART | | | | A manual scram was inserted at 0009 on 5/8/01. The scram was conducted in | | accordance with plant procedures, IOI-8 "Manual Scram," due to a failure of | | the reactor recirculation pump "A" to restart during a downshift from fast | | to slow speed operation. Plant response to the manual scram was as | | anticipated, all rods fully inserted, no ECCS actuations occurred and no | | SRVs opened. Reactor vessel water level reached Level 3 (177.7 inches) and | | operators entered the Plant Emergency Instructions. At 0016 the Plant | | Emergency Instructions were exited. The cause of the "A" recirculation pump | | failure to restart is being investigated. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37972 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 05/08/2001| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 12:44[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/08/2001| +------------------------------------------------+EVENT TIME: 10:04[EDT]| | NRC NOTIFIED BY: JIM PRIEST |LAST UPDATE DATE: 05/08/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM COOK R1 | |10 CFR SECTION: | | |*SHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN | | | | On 5/8/01, at approximately 1004, the Hope Creek Generating Station | | initiated a unit shutdown to comply with the provisions of Technical | | Specification (TS) 3.0.3, TS 3.0.3 was entered at 0820 when both trains of | | the Main Steam Line Isolation Valve Sealing System (MSIVSS) were declared | | inoperable. The 'B' MSIVSS had been inoperable since 5/4/01 due to a | | malfunctioning flow transmitter with the associated TS, 3.6.1.4 1 entered. | | On 5/8/01, at 0508, a Potential Transformer fuse failure associated with | | the 'C' Class 1E 4.16kV bus tripped two of four channels of Loss of Voltage | | relay protection for that bus. The tripped channels provide start | | permissives for the 'C' EDG and have actuated to the tripped condition to | | provide those permissives. During subsequent investigation of the extent | | and consequences of the fuse failure, it was determined at 0820 hours that | | the fuse failure also affected the 'C' Emergency Diesel Generator (EDG) | | synchroscope rendering the 'C' EDG inoperable due to its inability to meet | | the surveillance requirement of TS 4.8.1.1.2.h.10 Since the 'C' EDG | | provides the 1E power to the 'A' MSIV Sealing System both trains of the MSIV | | Sealing System were considered inoperable and TS 3.0.3 was entered. | | | | Investigation into the cause of the fuse failure is ongoing. With the | | exception of the 'A' Control Room Emergency Filtration System, all other | | safety-related systems were operable at the time of the event. | | | | The licensee notified the NRC resident inspector, the State of New Jersey | | and Lower Alloways Creek Township. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37973 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: HENRY FORD HOSPITAL |NOTIFICATION DATE: 05/08/2001| |LICENSEE: HENRY FORD HOSPITAL |NOTIFICATION TIME: 14:10[EDT]| | CITY: DETROIT REGION: 3 |EVENT DATE: 04/20/2000| | COUNTY: STATE: MI |EVENT TIME: 12:00[EDT]| |LICENSE#: 21-04109-16 AGREEMENT: N |LAST UPDATE DATE: 05/08/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE JORGENSEN R3 | | |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ALAN JACKSON | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | Unintended deviation from a written directive in the use of an | | investigational temporary brachytherapy implantation device on 04/20/00. | | Device is the Proxima Therapeutics, GliaSite RTS (a 2-4 cm balloon | | catheter). The device is being investigated under the NABTT # 9801 | | Multi-center open label clinical study to evaluate the performance of the | | Proxima GliaSite RTS in patients with recurrent brain tumors undergoing | | surgical resection. | | | | In this study, the GliaSite RTS is implanted in the tumor resection bed at | | the time of surgery. Two weeks following surgery, a solution of lotrex and | | saline is infused into he balloon catheter in order to deliver the radiation | | dose. Following a specified dwell time, the lotrex is removed from the | | balloon and the balloon is then surgically removed from the patient's brain. | | Prior to therapy, radiographic contrast media is infused into the balloon to | | verify the balloon placement. This contrast media is removed just prior to | | the infusion to the lotrex. All fluid volumes are tracked to determine the | | exact volume of fluid in the balloon at all times. | | | | In the specific treatment plan where the deviation from the written | | directive occurred, was prescribed by a Radiation Oncologist and infused | | into a balloon by a Nuclear Medicine Physician with a dwell time of 70 | | hours. | | | | Following the prescribed dwell time the lotrex was removed and an initial | | assay of the retrieved lotrex demonstrated a 60% apparent reduction in | | retrieved activity as compared to the administered activity. The reduced | | activity measured in the retrieval fluid was to be due to a mixture of | | contrast media with the lotrex in the fluid. By diluting the retrieved | | fluid, to remove attenuation characteristics of the contrast media, the | | total administered activity was measured. | | | | Since the contrast media was causing attenuation of the radioactivity in the | | retrieved fluid, resulting in a reduction of the Dose Calibrator readings, | | it is assumed the radiation dose to the tissue surrounding the balloon was | | also reduced. The absorbed dose to the tissue cannot be determined | | accurately due to the uncertainty in the homogeneity of the iodine-125 and | | contrast media in the GliaSite RTS during the therapy. Therefore, the | | attenuation characteristics and absorbed energy within the tissue cannot be | | accurately modeled. | | | | During the investigation of this incident, all steps contained within the | | Henry Ford Hospital and NABTT #9801 Quality Management Programs were | | followed. This incident notification of the patient, physicians and all | | attending staff within 4 hours following the retrieval of the lotrex that an | | apparent discrepancy in the activity retrieved existed. In addition, all | | trash and urine were verified to have been retrained and surveys of these | | waste showed negligible readings. All room surveys also showed no | | contamination. The patient, as well as fluid retrained from the surgical | | site and the GliaSite RTS all demonstrated no contamination. The patient | | was not harmed by the event. | | | | To prevent contrast contamination during this therapy in the future an | | additional flushing of all fluid from the balloon prior to infusion of the | | lotrex will be done. | | | | The NABTT #9801 study is intended as a Phase 1 device trail rather than a | | clinical efficacy trail. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37974 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 05/08/2001| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 18:56[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/08/2001| +------------------------------------------------+EVENT TIME: 16:28[CDT]| | NRC NOTIFIED BY: BILL CLARK |LAST UPDATE DATE: 05/08/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SPECIFIED SYSTEM ACTUATION | | | | "With the plant in a refueling outage, during restoration of the CRD system, | | ongoing maintenance prevented restoring and opening the scram discharge | | volume vents and drains. Leakage slowly filled the scram discharge volume. | | At 1628, level reached the trip setpoint and initiated a RPS trip signal. | | This is considered a valid initiation signal. All systems responded as | | expected. No control rod movement occurred and no refueling operations were | | in progress. Scram has not been reset due to ongoing maintenance." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37975 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 05/08/2001| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 19:24[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/08/2001| +------------------------------------------------+EVENT TIME: 15:28[CDT]| | NRC NOTIFIED BY: RICK NANCE |LAST UPDATE DATE: 05/08/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP - LOW STEAM GENERATOR LEVEL | | | | On 05/08/2001, Unit 2 experienced a automatic Reactor Trip due to low water | | level in the 2A Steam Generator. Prior to the reactor trip, Instrument and | | Control Technicians were tuning the 2A Main Feed Water Regulating Valve | | digital control system. The 2A Main Feed Water Regulating Valve went fully | | closed, and the Control Room Staff was unable to reopen the valve. | | | | At the same time as the Reactor Trip, the Auxiliary Feed Water System | | actuated due to low water level in the 2A Steam Generator. After the | | Reactor Trip all Control Rods Fully inserted into the core, all automatic | | systems operated as designed, and no primary to secondary leakage was | | detected. | | | | The plant is stable in Mode 3, reactor coolant pumps are running and decay | | heat is being removed by using the main turbine bypass valves. Steam | | generator water level has been restored and main feed is being used to feed | | the steam generators. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021