Event Notification Report for April 23, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/20/2001 - 04/23/2001 ** EVENT NUMBERS ** 37934 37935 37936 37937 37938 37939 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37934 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 04/20/2001| | UNIT: [2] [] [] STATE: PA |NOTIFICATION TIME: 10:19[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 03/10/2001| +------------------------------------------------+EVENT TIME: 13:30[EDT]| | NRC NOTIFIED BY: SAARE |LAST UPDATE DATE: 04/20/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM RULAND R1 | |10 CFR SECTION: | | |*INV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INVALID ACTUATION OF THE "B" EMERGENCY SERVICE WATER PUMP OCCURRED | | | | This 60-day optional report, as allowed by 10 CFR 50.73(a)(1), is being made | | under the reporting requirement in 10CFR50.73(a)(2)(iv)(A) to describe an | | invalid actuation of a specified system, specifically Emergency Service | | Water (ESW). | | | | On March 10, 2001, during performance of a surveillance test on the | | Emergency Diesel Generator Logic, an invalid actuation of the "B" ESW pump | | occurred. The event was caused by a jumper inadvertently being left | | installed when the surveillance test required the jumper to be momentarily | | installed. The jumper simulated an initiation signal on 1 EDG. As the | | test progressed, the "B" ESW pump received an initiation signal and | | started. | | | | The "B" ESW pump started as expected for the given conditions and was | | subsequently returned to standby per plant procedures. No deficiencies | | were noted during operation of the "B" ESW pump. | | | | This event has been entered into the site-specific corrective action program | | for resolution. | | | | The resident has been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37935 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OK DEQ RAD MANAGEMENT |NOTIFICATION DATE: 04/20/2001| |LICENSEE: GEO SYSTEMS ENGINEERING, INC. |NOTIFICATION TIME: 12:40[EDT]| | CITY: TULSA REGION: 4 |EVENT DATE: 04/20/2001| | COUNTY: STATE: OK |EVENT TIME: 06:20[CDT]| |LICENSE#: 27597-02-OK AGREEMENT: Y |LAST UPDATE DATE: 04/20/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MAKE BRODERICK | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - STOLEN HUMBOLDT NUCLEAR GAUGE | | | | The device was stolen from a truck after the chain had been cut, the travel | | case was locked. The theft was reported to the Tulsa police department and | | a reward will be offered by the licensee. The device was a Humboldt model | | 5001B serial #3475 containing Cs-137 and Am-241. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37936 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 04/21/2001| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 02:31[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 04/20/2001| +------------------------------------------------+EVENT TIME: 19:31[CDT]| | NRC NOTIFIED BY: SCOTT MAGLIO |LAST UPDATE DATE: 04/21/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANTICIPATED EMERGENCY DIESEL GENERATOR START DURING THE PERFORMANCE OF | | TESTING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This is notification of valid system actuation in accordance with | | 10CFR50.72(b)(3)(iv)(A)." | | | | "At 1931 [CDT] on 04/20/01, the 'B' emergency diesel generator (EDG) | | automatically started during testing of the local emergency start | | pushbutton. This was conducted as part of a pre-planned test for | | restoration following maintenance. However, during the test, the system | | actuated in a way that was not part of the planned test. Initial test of | | the signal was unsuccessful, and the start signal was not reset prior to | | restoring the EDG to the standby lineup. Subsequently, when the start | | failure relay was locally reset, the EDG automatically started." | | | | "The unit was in no MODE at the time of the actuation." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37937 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 04/21/2001| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 07:02[EDT]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 04/21/2001| +------------------------------------------------+EVENT TIME: 03:20[CDT]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 04/21/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 HPCI INOPERABLE DUE TO FAILED TURBINE EXHAUST LINE VACUUM BREAKER | | CHECK VALVES | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 0320 [CDT] on April 21, 2001, Unit [2] HPCI was declared inoperable when | | two check valves failed to meet acceptance criteria during the performance | | of [procedure] QCOS 2300-18, HPCI STEAM EXHAUST VACUUM BREAKER LINE CHECK | | VALVES IST FUNCTIONAL TEST. Two of the four HPCI turbine exhaust line | | vacuum breaker check valves were found to have failed to close. The exhaust | | line containing the failed check valves was isolated at the start of the | | surveillance using motor-operated isolation valves contained in the exhaust | | line. The failed check valves remain isolated." | | | | The licensee stated that Unit 2 is in a 14-day limiting condition for | | operation as a result of this issue. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37938 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 04/21/2001| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 10:19[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/21/2001| +------------------------------------------------+EVENT TIME: 08:53[EDT]| | NRC NOTIFIED BY: ERIC OLSON |LAST UPDATE DATE: 04/21/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM RULAND R1 | |10 CFR SECTION: | | |*INA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANTICIPATED AUTOMATIC MAIN STEAM ISOLATION VALVE (MSIV) CLOSURE AND | | REACTOR WATER CLEANUP [RWCU] SYSTEM ISOLATION DUE TO LEVEL RACK REFERENCE | | LEG NOTCHING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During cooldown of the reactor vessel with all rods fully inserted, the | | [MSIVs] automatically closed in response to a reactor high level concurrent | | with low reactor pressure (main steam line pressure <810 with reactor level | | at | | +55.4 inches). Reactor pressure was at 100 psig when the isolation | | occurred. Approximately 1 hour later, another level perturbation occurred | | resulting in automatic isolation of the [RWCU] system and the inboard MSIV | | drain valve. The level perturbations are occurring in the 'A' train level | | rack only. It appears to be caused by non-condensable gasses coming out of | | solution in the 'A' level rack reference leg (notching). The 'A' train | | water level indication system is considered to be inoperable, and the | | applicable [limiting condition for operation] actions have been taken." | | | | The licensee stated that a planned reactor scram was performed prior to this | | event in order to facilitate commencement of a scheduled refueling outage. | | Apparently, the RWCU system isolation resulted from a spurious low level | | signal to the actuation system when the reference leg was being back filled. | | This was reported to be so quick that it was not seen on any control room | | instruments. The RWCU system has been placed back in service and is being | | used for level control. The MSIVs are still closed, but the isolation | | signal has been reset. However, the notching phenomenon is still being | | experienced. | | | | The licensee plans to change the decay heat removal path from the main steam | | system and place the RCIC system in test mode. As the reference leg is back | | filled and flushed out, the licensee plans to plan to go back to utilization | | of the main steam system. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37939 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 04/21/2001| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 19:17[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/21/2001| +------------------------------------------------+EVENT TIME: 14:54[CDT]| | NRC NOTIFIED BY: JOHN CARLSON |LAST UPDATE DATE: 04/21/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES MARSCHALL R4 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 58 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED AUTOMATIC REACTOR SCRAM DURING TURBINE CONTROL VALVE TESTING | | | | During plant start-up from forced outage 01-01, with the plant at 58% power, | | an automatic reactor scram occurred. The scram occurred during the main | | turbine control valve testing due to an apparent turbine pressure control | | system malfunction. Automatic reactor scram occurred at the RPV High | | Pressure Scram Setpoint. All other systems functioned as expected during | | and after the transient. The unit is currently stable in Mode 3, Hot | | Shutdown, with reactor pressure and level within normal bands. | | Investigation in progress to determine cause of malfunction. Safety Relief | | Valves opened and closed during the transient. All Emergency Core Cooling | | Systems are fully operable and the electrical grid is stable. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021