Event Notification Report for April 19, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/18/2001 - 04/19/2001 ** EVENT NUMBERS ** 37761 37900 37905 37925 37926 37927 37928 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37761 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 02/19/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 03:00[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/18/2001| +------------------------------------------------+EVENT TIME: 22:45[EST]| | NRC NOTIFIED BY: VICTOR WALZ |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 | |10 CFR SECTION: |JOHN ZWOLINSKI NRR | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION SYSTEM (HPCI) DECLARED INOPERABLE | | | | "During normal monitoring of the standby lineup of the High Pressure Coolant | | Injection System (HPCI), the building rounds operator noticed that the HPCI | | discharge flow switch (23FS-78) was indicating 140 gpm with zero actual | | flow. This flow switch controls the operation of the HPCI pump minimum flow | | valve during HPCI operations. Upon further investigation by the operating | | crew, it was also determined that the HPCI pump discharge flow transmitter | | was exhibiting sporadic flow spikes of 50 to 100 gpm with zero system flow. | | This flow signal is used to control HPCI turbine speed and flowrate. Based | | on these findings, the HPCI system was declared inoperable per Technical | | Specification 3.5.c and a 7 day Limiting Condition for Operation was | | entered." | | | | The licensee called in an engineering team to address this problem. The | | licensee will inform the NRC resident inspector. | | | | * * * RETRACTION 1529 4/18/01 FROM PAGE TAKEN BY STRANSKY * * * | | | | "On 2/19/01 at 0300 EST, the James A. Fitzpatrick nuclear power plant | | notified the NRC that the High Pressure Coolant injection (HPCI) System had | | been declared inoperable due to indicated flow on a local discharge flow | | switch indication and sporadic flow spikes on the pump discharge flow | | transmitter while the system was in the standby lineup. The report was made | | pursuant to 10CFR50.72(b)(3)(v)(D) under Event Notification number 37761. | | | | "Based upon further review, it has been determined that, despite the | | problems noted, HPCI would have performed its safety function. The local | | HPCI discharge flow switch indication has no safety-related function. The | | associated safety-related switches operated within the prescribed setpoint | | tolerances. The hydraulic and mechanical portions of the system cannot | | respond to change as quickly as the electronic components, and therefore | | were not affected by the higher frequency sporadic spiking on the pump | | discharge flow transmitter. Maintenance was performed to address the | | associated degraded conditions. | | | | "Based upon the ability of the HPCI System to perform its safety function, | | the above notification is being retracted." | | | | The NRC resident inspector will be informed of this retraction. Notified | | R1DO (Ruland). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37900 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 04/08/2001| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 22:15[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 04/08/2001| +------------------------------------------------+EVENT TIME: 16:15[EDT]| | NRC NOTIFIED BY: RICHARD LANGE |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |*INA 50.72(b)(3)(v)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH EMERGENCY DIESEL GENERATORS DECLARED INOPERABLE | | | | "Both Division 1 and Division 2 standby diesel generators were declared | | inoperable. This report is being made per 10CFR50.72(b)(3)(v)(A), in that | | both standby diesels were in a condition such that they may not have been | | able to fulfill their intended safety function. | | | | "The division 1 diesel generator was declared inoperable because both diesel | | generator room exhaust fans were found rotating backwards. The division 2 | | diesel generator was declared inoperable due to one exhaust fan rotating | | backwards and the outside air temperature exceeding 72�F. The cause of the | | fan blades' reverse rotation is under evaluation. Reverse fan blade | | rotation may cause longer in-rush starting currents which could cause the | | fan motors to trip. | | | | "With two diesel generators inoperable, the plant entered Technical | | Specification 3.8.1, a 2-hour shutdown Action Statement. | | | | "Division 1 and 2 diesel room exhaust fans stopped rotating, and the outside | | air temperature lowered to less than 72�F The Technical Specification Action | | Statements were exited. Periodic monitoring of the fans has been established | | to address reoccurrence of the condition." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * RETRACTED AT 1400 EDT ON 4/18/01 BY THOMAS RESTUCCIO TO FANGIE JONES * | | * * | | | | The licensee is retracting the event notification based on the following: | | | | "Event notification 37900 was written due to the inoperability of Division I | | and II emergency diesel generators. The diesel generators were declared | | inoperable due to the diesel generator room exhaust fans spinning backwards. | | The issue was that under reverse rotation, starting currents may exceed trip | | values rendering the exhaust fans inoperable and, as a result, causing the | | diesel generators to be declared inoperable. | | | | "At the time of discovery it was identified that the diesel generator | | exhaust fans for Division I and II were observed to be rotating backwards at | | approximately 10-15 rpms. An engineering analysis performed by the licensee | | has determined that the tans can be spinning backwards up to 235 rpm and | | will start and operate normally if needed. There will be no adverse affect | | on the fans operability to perform their design safety function." | | | | The licensee notified the NRC Resident Inspector. The R1DO (William Ruland) | | was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37905 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ROBINSON REGION: 2 |NOTIFICATION DATE: 04/10/2001| | UNIT: [2] [] [] STATE: SC |NOTIFICATION TIME: 18:49[EDT]| | RXTYPE: [2] W-3-LP |EVENT DATE: 04/10/2001| +------------------------------------------------+EVENT TIME: 13:30[EDT]| | NRC NOTIFIED BY: HAROLD CHERNOFF |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |*DEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF REACTOR COOLANT SYSTEM PRESSURE BOUNDARY LEAKAGE POSSIBLY VIA A | | CONTROL ROD DRIVE MECHANISM ASSEMBLY SEAL WELD | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 4/10/01, during the removal of mirror insulation from the reactor vessel | | head while shut down, deposits of residual boric acid were found on the | | periphery of the Reactor Pressure Vessel Head outside of the Control Rod | | Drive Mechanism (CRDM) Shroud. Subsequent investigation, by visual | | inspection of the area within the shroud, revealed additional amounts of | | boric acid. The source of the leak, based on initial observation, appears | | to be a CRDM assembly seal-weld leak about 18 inches above the vessel head | | insulation. A leak from this location would constitute Reactor Coolant | | System Pressure Boundary leakage. Initial inspection of the reactor vessel | | head areas, in the vicinity of the boric acid deposits outside of the | | shroud, revealed no damage to the reactor vessel head." | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE ON 04/18/01 @ 1123 BY GARROU TO GOULD * * * RETRACTION | | | | On 4/10/01, during the removal of mirror insulation from the reactor vessel | | head while shut down. | | deposits of residual boric acid crystals were found on the periphery of the | | Reactor Pressure Vessel | | Head outside of the Control Rod Drive Mechanism (CRDM) shroud. Subsequent | | inspection at CRDM canopy seal welds and the reactor vessel head in the | | vicinity of the boric acid crystal deposits was conducted with the head off | | the reactor vessel and the shroud and some mirror insulation removed. The | | identified source of the observed boric acid crystals was two very small | | locations on the canopy seal weld of CRDM No. 68 at location B10. | | | | Leakage through the canopy seal weld is not pressure boundary leakage as | | described in the Technical Specifications and Bases. The structural | | integrity of the CRDM housing is maintained by the threaded connection. | | The canopy seal weld does not maintain the structural integrity of the | | reactor coolant system. Therefore, the original notification made pursuant | | to 10CFR 50.72(b)(3)(ii)(A) is retracted. | | | | The NRC Resident Inspector was notified. | | | | Reg 2 RDO(Landis) was notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37925 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 04/17/2001| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 17:40[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/17/2001| +------------------------------------------------+EVENT TIME: 15:42[EDT]| | NRC NOTIFIED BY: SUE SIMPSON |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM RULAND R1 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALID CONTAINMENT VENTILATION ISOLATION | | | | "While in Mode Undefined (core offloaded), Salem Unit 1 received a | | Containment Ventilation Isolation signal due to elevated count rate on | | 1R11A, the Containment Particulate Radiation Monitor. The 1R11A setpoint is | | set two times background in accordance with Tech Spec 3.3.3.1 for Mode 6. | | Background count rate prior to the CVI was 2100 cpm (counts per minute). The | | alarm setpoint was 2980 cpm. | | | | "The observed count rate when the actuation occurred was 3300 cpm. | | Maintenance activities in progress included the breech of 14SJ43, Cold Leg | | Injection Check Valve. Elevated airborne activity was expected due to this | | evolution and had been discussed by Control Room personnel. When 1R11A | | exceeded its setpoint, all containment ventilation isolation valves closed | | as designed. This actuation has not impacted the Unit 1 outage. | | | | "Plant status before and after event: | | Reactor Coolant System drained to mid-loop | | RCS at approximately 90�F | | Core completely offloaded | | Mode Undefined" | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * Retraction 1213 4/18/2001 from Sue Simpson taken by Bob Stransky * * | | * | | | | "This notification is a retraction of the 8-hour report made IAW | | 10CFR50.72(b)(3)(iv)(A) on April 17, 2001 (event time 1542, reported at | | 1740). | | | | "This event notification is being retracted because subsequent investigation | | determined that the containment ventilation isolation does not meet the | | definition of reportable system actuations listed in | | 10CFR50.72(b)(3)(iv)(B)." | | | | The NRC resident inspector will be informed by the licensee. Notified R1DO | | (Ruland). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37926 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 04/18/2001| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 12:38[EDT]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 04/18/2001| +------------------------------------------------+EVENT TIME: 11:50[EDT]| | NRC NOTIFIED BY: DAVID MORRIS |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KERRY LANDIS R2 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANNED OFFSITE NOTIFICATION REGARDING THE DISCOVERY OF A DEAD AMERICAN | | CROCODILE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[At 1150 on 04/18/01, the licensee was] notified by Land Utilization of a | | deceased American Crocodile. [It was] discovered at [the] far west end of | | the cooling canals. [The] State of Florida will be notified by Land | | Utilization later today." | | | | The licensee notified the NRC resident inspector and plans to notify the | | State. It was reported that the State may inform other federal agencies. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37927 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: HI DEPARTMENT OF HEALTH |NOTIFICATION DATE: 04/18/2001| |LICENSEE: CONSTRUCTION ENGINEERING LABS |NOTIFICATION TIME: 15:29[EDT]| | CITY: KAU REGION: 4 |EVENT DATE: 04/17/2001| | COUNTY: STATE: HI |EVENT TIME: 15:30[HST]| |LICENSE#: 53-23293-01 AGREEMENT: N |LAST UPDATE DATE: 04/18/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES MARSCHALL R4 | | |DONALD COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: J. NAKASONE | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC LICENSED SOURCE INVOLVED IN AUTOMOBILE ACCIDENT | | | | The caller reported that an NRC licensed moisture/density gauge was involved | | in an automobile accident. The gauge was in its case, which was undamaged. | | Radiation readings taken at the scene were less than 1 mR/hr. The state | | contacted the NRC licensee, and has already reported the event to NRC Region | | IV. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37928 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 04/18/2001| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 17:45[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 04/18/2001| +------------------------------------------------+EVENT TIME: 14:05[EDT]| | NRC NOTIFIED BY: LARRY TAYLOR |LAST UPDATE DATE: 04/18/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KERRY LANDIS R2 | |10 CFR SECTION: | | |*UNA 50.72(b)(3)(ii)(B) UNANALYZED COND OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFE SHUTDOWN TRAIN ELECTRICAL SEPARATION NOT ADEQUATE | | | | "HNP is in mode one, 100% power and stable. HNP personnel have determined | | during an engineering review that fuses intended to maintain safe shutdown | | train separation in the event of a fire in the 'A' Switchgear room are not | | capable of performing their intended function due to a design error. A fire | | in one fire area could result in the inability to isolate a Pressurizer | | Power Operated Relief Valve (PORV) and associated block valve. These fuses | | were intended to protect against this condition by isolating the PORV Block | | Valve circuit on an electrical short due to a fire. These fuses provide | | power for indication on the plant computer only. | | | | "The fuses creating this condition have been removed restoring proper train | | separation." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021