Event Notification Report for April 4, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/03/2001 - 04/04/2001 ** EVENT NUMBERS ** 37634 37880 37883 37884 37885 37886 37887 37888 37889 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37634 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 12/27/2000| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 12:47[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 12/27/2000| +------------------------------------------------+EVENT TIME: 10:31[EST]| | NRC NOTIFIED BY: RANDY HAISLET |LAST UPDATE DATE: 04/03/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE DOERFLEIN R1 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |NLTR LICENSEE 24 HR REPORT O| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING SYSTEM (RCIC) DECLARED INOPERABLE | | | | The licensee was performing the procedure to reset the RCIC isolation, after | | a surveillance was completed, when the closed inboard steam isolation valve | | (MO-1301-16) went to dual indication while opening the outboard steam | | isolation valve (MO-1301-17). Both steam isolation valves to the RCIC | | turbine were closed and the RCIC system was declared inoperable. The | | licensee is investigating the problem. | | | | Active limiting conditions for operation were entered for the RCIC system | | and the primary containment isolation function of the RCIC inboard steam | | isolation valve (MO-1301-16). | | | | The licensee notified the NRC Resident Inspector. | | | | * * * RETRACTED AT 1414 EDT ON 4/3/01 BY ERIC OLSON TO FANGIE JONES * * * | | | | The licensee is retracting this event notification. The following was | | submitted as the basis for the retraction. | | | | "On December 27, 2000, the RCIC system was taken out of service to perform | | routine surveillance in accordance with PNPS procedures 8.M.2-2.6.1 and | | 8.M.2-2.6.4. After resetting the RCIC isolation after performance of the | | High Steam Flow surveillance, operations personnel opened valve, MO-1301-17. | | Approximately 5 seconds into the opening stroke, MO-1301-16, the inboard | | isolation valve, gave dual indication. During the initial opening of the | | MO-1301-17 valve, the RCIC turbine inlet steam line began to pressurize due | | to trapped pressure between the MO-1301-16 and MO-1301-17 valves and | | increased to approximately 437 psig when it began to decrease at about one | | pound per two seconds. The Control Room operator then gave MO-1301-16 valve | | a closed signal after the valve indicated dual indication for 16 seconds and | | the valve then indicated full closed. The steam line continued to | | depressurize at the same rate until operations closed the MO-1301-17 valve. | | This indicated that although MO-1301-16 showed dual Indication, it was | | closed and the seating surfaces were tight and the containment isolation | | function was operable. | | | | "The test that was being performed was testing the primary containment | | isolation system (PCIS) and this surveillance was satisfactory with both | | inboard and outboard isolation valves closing upon initiation. Additionally, | | MO-1301-16 was stroke timed in accordance with PNPS procedure 8.5.5.4 and | | the times were within the expected limits. | | | | "After the initial indication of leakage, the Control Room management | | conservatively declared MO-1301-16 and the RCIC system inoperable until | | further investigation could be performed. Troubleshooting was conducted in | | accordance with PNPS procedure 3.M.1-34. The conclusion was that while dual | | indication had occurred, the valve had been closed and primary containment | | isolation was operable. | | | | "For (a)(2)(i) (B): not reportable. The initial indication of leakage | | through containment Isolation valve MO-1301-16 was evaluated. The source of | | the pressure was steam trapped between the isolation valves during the | | previous testing. The valve was subsequently determined to have been closed | | and containment isolation was maintained. | | | | "For (a)(2)(v): not reportable. There was no component or system failure. | | The containment isolation function was maintained. | | | | "For (a)(2)(vii): not reportable. It was determined that there was no | | component or system failure. The containment isolation function was | | maintained. | | | | "Please note that RCIC was 'made' inoperable by closing the referenced | | motor-operated valves (MO-1301-16 and MO-1301-17) to perform their primary | | containment isolation function in accordance with Technical Specification | | 3/4.7.A.2. After the operability determination, the valves were opened and | | RCIC was again operable per TS 3/4.5.D." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Jack McFadden) | | was informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37880 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 04/02/2001| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 06:53[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/02/2001| +------------------------------------------------+EVENT TIME: 04:02[CST]| | NRC NOTIFIED BY: BEAUDIN |LAST UPDATE DATE: 04/04/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVE LOVELESS R4 | |10 CFR SECTION: | | |*DEG 50.72(b)(3)(ii)(A) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GREATER THAN 1 PERCENT OF STEAM GENERATOR # 3 TUBES FOUND TO BE POTENTIALLY | | DEGRADED. | | | | At approximately 0402 CT on 04/02/01, Comanche Peak discovered that more | | than 1% (52 out of 4772 tubes) of the inspected tubes in Steam Generator # 3 | | are potentially degraded. The degraded tubes are being evaluated to be | | removed from service. This event meets the criteria of C-3 as described in | | their Technical Specification section 5.5.9. Additional data is being | | collected and will be analyzed to assist in determining the cause of the | | event. An LER will be issued to further document this issue. The other | | three Steam Generator tubes are being inspected. | | | | The NRC Resident Inspector will be notified of this event by the licensee. | | | | * * * UPDATE ON 04/03/01 AT 0653 ET BY RAUL MARTINEZ TAKEN BY MACKINNON * * | | * | | | | GREATER THAN 1 PERCENT OF STEAM GENERATOR # 4 TUBES FOUND TO BE POTENTIALLY | | DEFECTIVE. | | | | At approximately 0500 CT on 04/03/01 Comanche Peak discovered that more than | | 1% (49 out of 4777 tubes) of the inspected tubes in Steam Generator # 4 are | | potentially defective. The defective tubes are being evaluated to be | | removed from service. | | | | This event meets the criteria of C-3 as described in the their Technical | | Specification section 5.5.9. Additional data is being collected and will be | | analyzed to assist in determining the cause of the event. | | | | The licensee is presently inspecting Steam Generators 1 and 2. R4DO (Linda | | Smith) notified. | | | | The NRC Resident Inspector will be notified of this update by the licensee. | | | | ***** UPDATE AT 0015 EDT ON 04/04/01 FROM RAUL MARTINEZ TO LEIGH TROCINE | | ***** | | | | GREATER THAN 1% OF THE INSPECTED STEAM GENERATOR #2 TUBES WERE FOUND TO BE | | POTENTIALLY DEFECTIVE. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At approximately 2237 [CDT] on [04/03/01,] Comanche Peak Unit 1 discovered | | that more than 1% of the inspected tubes in steam generator #2 [were] | | potentially defective. The defective tubes are being evaluated to be | | removed from service." | | | | "This event meets the criteria of C-3 as described in [...] Technical | | Specification section 5.5.9 and is being reported pursuant to the | | requirements of 10 CFR 50.72(b)(3)(ii)(A). Additional data is being | | collected and will be analyzed to assist in determining the cause of the | | event." | | | | "[The total number] of inservice tubes in [steam generator] #2 = 4,476 | | tubes[, and the total number] of tubes discovered defective at this time = | | 52 tubes." | | | | The licensee plans to notify the NRC resident inspector. The NRC operations | | officer notified the R4DO (Linda Smith). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37883 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MALLINCKRODT, INC. |NOTIFICATION DATE: 04/03/2001| |LICENSEE: MALLINCKRODT,INC. |NOTIFICATION TIME: 11:59[EDT]| | CITY: MINNEAPOLIS ST. PAUL REGION: 3 |EVENT DATE: 04/03/2001| | COUNTY: STATE: MN |EVENT TIME: [CDT]| |LICENSE#: 24-17450-02MD AGREEMENT: N |LAST UPDATE DATE: 04/03/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MICHAEL JORDAN R3 | | |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WILLIAM CRAWFORD | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PHARMACY RECEIVED GENERATOR WITH SLIGHTLY HIGH SURFACE READING | | | | The Mallinckrodt Pharmacy received a generator with a surface reading of | | slightly greater than the 200 millirem per hour from the Mallinckrodt | | facility in St. Louis, Missouri. There was no surface contamination, the | | swipe test was negative. The package had a transport index of 6.0 with a | | yellow 3 label package with transport index of 1.5. The manufacturer has | | been notified and is investigating the event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37884 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 04/03/2001| |LICENSEE: GEO SOLUTIONS |NOTIFICATION TIME: 14:10[EDT]| | CITY: SAN LUIS OBISPO REGION: 4 |EVENT DATE: 04/03/2001| | COUNTY: STATE: CA |EVENT TIME: [PDT]| |LICENSE#: 6286-40 AGREEMENT: Y |LAST UPDATE DATE: 04/03/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA SMITH R4 | | |CHARLES COX NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RECA OMAR | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MOISTURE DENSITY GAUGE RUN OVER AND DAMAGED | | | | Geo Solutions reported to the State of California that a Humbolt moisture | | density gauge was run over at a work site in Atascadero, CA. The case is | | cracked, but the insides appear intact. The licensee is contacting the | | vendor for proper handling. There is no further information at this time. | | | | * * * UPDATED AT 1732 EDT ON 4/3/01 BY RECA OMAR TO FANGIE JONES * * * | | | | Geo Solutions Radiation Safety Officer made a further report about the | | gauge. The source is intact, the electronics are still working, and a | | survey indicated no leakage. The gauge has been placed in storage until the | | vendor takes possession and performs a leak test. A construction bulldozer | | ran over the gauge. | | | | The R4DO (Linda Smith) and the NMSS EO (Patricia Holahan) were notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37885 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 04/03/2001| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 15:03[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/03/2001| +------------------------------------------------+EVENT TIME: 12:00[CDT]| | NRC NOTIFIED BY: ERNEST MATES |LAST UPDATE DATE: 04/03/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTIFICATION OF LOCAL GOVERNMENT AGENCY DUE TO SPURIOUS SIREN ACTUATION | | | | The licensee notified Claiborne County Civil Defense that a single offsite | | emergency siren sounded spuriously for about 25 minutes today starting about | | 1200 CDT. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37886 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 04/03/2001| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 16:12[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/03/2001| +------------------------------------------------+EVENT TIME: 16:09[EDT]| | NRC NOTIFIED BY: C. D. MARPLE |LAST UPDATE DATE: 04/03/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KEN BARR R2 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STATE AGENCY NOTIFIED OF INJURED LOGGERHEAD TURTLE FOUND IN THE INTAKE | | CANAL | | | | The licensee notified the Florida Fish and Wildlife Conservation Commission | | regarding an injured loggerhead turtle found in the plant's intake canal. | | The turtle will be sent out for rehabilitation. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37887 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 04/04/2001| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 02:19[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 04/03/2001| +------------------------------------------------+EVENT TIME: 23:58[CDT]| | NRC NOTIFIED BY: RON WIGGINS |LAST UPDATE DATE: 04/04/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 27 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FROM 27% POWER DUE TO A RECIRULATION PUMP TRIP FOR | | UNKNOWN REASONS WHILE THE UNIT WAS IN SINGLE LOOP OPERATION | | | | The following text is a portion of a facsimile received from the licensee: | | | | "[The] unit was operating [in] single loop (2A [recirculation] pump | | operating) when the 2A [recirculation] pump tripped. The [nuclear station | | operator] manually scrammed the unit as required by procedure. During the | | event, Group II and III isolations were received. All equipment operated as | | expected. [The] unit is [currently] stable in Mode 3. Restart is being | | evaluated." | | | | The licensee stated that reactor vessel water level decreased to +5 inches | | and that the Group II and III isolation setpoint was +8 inches. The Group | | II and III isolations have been reset, and ventilation has been restored. | | | | The normal reactor feedwater system is currently being utilized to supply | | water to the reactor vessel, and containment parameters are normal. The | | steam dumps to the condenser were available but not needed. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37888 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 04/04/2001| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 07:22[EDT]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 04/03/2001| +------------------------------------------------+EVENT TIME: 23:51[CDT]| | NRC NOTIFIED BY: DAVID TIDWELL |LAST UPDATE DATE: 04/04/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KEN BARR R2 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM ON WEST SCRAM DISCHARGE VOLUME HIGH WATER LEVEL DUE TO | | APPARENT LEAKAGE THROUGH THE SCRAM VALVES | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During a refueling outage while picking up a hold order on the control rod | | drive system, water level in the scram discharge volume instrument volume | | started to rise from apparent leakage through the scram valves. At 2351 | | [CDT,] a reactor scram was received on the west scram [discharge volume] | | high water level. All expected alarms and actuations were received. All | | control rods were initially 'full in,' and no rod movement occurred." | | | | The licensee stated that there was nothing unusual or misunderstood and that | | all systems functioned as required. The licensee also stated that at the | | time of the event, work was being performed on the scram discharge volume | | drain valves which prevented the scram discharge volume from draining. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37889 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 04/04/2001| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 10:50[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/04/2001| +------------------------------------------------+EVENT TIME: 10:12[EDT]| | NRC NOTIFIED BY: DAVE WILLIAMS |LAST UPDATE DATE: 04/04/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |KEN BARR R2 | |10 CFR SECTION: |TAD MARSH NRR | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED OBSO|RICHARD WESSMAN IRO | | |GARY BELCHER FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR COOLANT SYSTEM LEAKAGE >10 GPM AS OBSERVED FROM CONTROL ROOM | | INDICATIONS | | | | "EMERGENCY PLAN ENTRY DUE TO CONTROL ROOM INDICATION OF REACTOR COOLANT | | SYSTEM LEAKAGE GREATER THAN 10 GPM. IT APPEARS THAT SHUTDOWN COOLING RELIEF | | VALVE V-3483 LIFTED WHILE ATTEMPTING TO PLACE '1A' TRAIN OF SHUTDOWN COOLING | | IN SERVICE. WHEN V-3481, HOT LEG SUCTION VALVE, WAS OPENED, APPROXIMATELY | | 300 GALLONS OF REACTOR COOLANT WAS DIVERTED TO A HOLDUP TANK OVER A PERIOD | | OF 2 MINUTES. THE LEAK, ESTIMATED AT 150 GPM, WAS ISOLATED BY CLOSING HOT | | LEG SUCTION VALVE V-3480. AN UNUSUAL EVENT WAS ENTERED AND TERMINATED | | IMMEDIATELY AT 1012 HOURS AS THE LEAK HAD BEEN TERMINATED AT THE TIME OF THE | | NOTIFICATION. | | | | "THIS EVENT IS SIMILAR TO EVENT #37882." | | | | RCS PRESSURE AND TEMPERATURE IS CURRENTLY 260 PSIG AND 250 DEGREES F, | | RESPECTIVELY. THE RELIEF VALVE SETPOINT IS 330 PSIG. FOLLOWING THE | | PREVIOUS EVENT, THE RELIEF VALVE V-3483 WAS REMOVED AND BENCH TESTED WITH NO | | ABNORMALITIES RELATED TO THE SETPOINT PRESSURE FOUND. PRESENTLY, THERE ARE | | TWO (2) RCPs RUNNING WITH A THIRD AVAILABLE AND THE "1B" SHUTDOWN COOLING | | TRAIN IN SERVICE. THE LICENSEE PER A PROCEDURAL REQUIREMENT INVOLVING LOW | | PRESSURE OPERATION OF THE RCPs (RCP SEAL PROTECTION) IS IN A 12 HOUR TIME | | PERIOD ENDING AT 1600 HOURS. THE CURRENT PLANS ARE TO INCREASE RCS PRESSURE | | TO GREATER THAN 350 PSIG. BOTH STEAM GENERATORS ARE AVAILABLE TO REMOVE | | DECAY HEAT. UNIT 1 HAS BEEN SHUTDOWN FOR APPROXIMATELY 50 HOURS. AN EVENT | | RESPONSE TEAM HAS BEEN ASSEMBLED TO RECOMMEND APPROPRIATE CORRECTIVE ACTIONS | | FOLLOWING COMPLETION OF AN INVESTIGATION. | | | | THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021