Event Notification Report for March 26, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/23/2001 - 03/26/2001 ** EVENT NUMBERS ** 37682 37684 37779 37799 37809 37844 37861 37862 37863 37864 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37682 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 01/24/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 07:36[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/23/2001| +------------------------------------------------+EVENT TIME: 07:25[EST]| | NRC NOTIFIED BY: ABRAMSKI |LAST UPDATE DATE: 03/23/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |STEVEN DENNIS R1 | |10 CFR SECTION: | | |*INB 50.72(b)(3)(v)(B) POT RHR INOP | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION SYSTEM DECLARED INOPERABLE. | | | | The flow controller for the High Pressure Coolant Injection (HPCI) system is | | indicating approximately 1400 gpm with the HPCI system in the standby | | condition. Because the cause of this condition is not known at this time, | | the HPCI system is considered inoperable. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * RETRACTED AT 1528 EST ON 3/23/01 BY MARK ABRAMSKI TO FANGIE JONES * * | | * | | | | "Engineering evaluation subsequent to this event has determined that the | | HPCI system would have performed its' intended function as credited in the | | LOCA analysis and therefore this 10 CFR 50.72 notification is retracted." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Kenneth | | Jenison) has been notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37684 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 01/25/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 06:53[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 01/25/2001| +------------------------------------------------+EVENT TIME: 02:47[EST]| | NRC NOTIFIED BY: M ADRAMSKI |LAST UPDATE DATE: 03/23/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |*INB 50.72(b)(3)(v)(B) POT RHR INOP | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) DECLARED INOPERABLE. | | | | At 0247 ET on 01/25/01, the flow transmitter controller for HPCI system | | spiked from zero to approximately 1500 gpm. The HPCI system was in standby | | lineup at the time. The flow indication has been slowly drifting down. | | | | A similar event occurred on 01/23/01 at 0725ET. HPCI was declared | | inoperable. The flow transmitter, 23FT-82, and flow switch, 23FS-78, were | | vented and a small amount of air was noted. The flow indication returned to | | zero (normal standby indication). After a HPCI operability surveillance | | test, HPCI was declared operable at 1332 ET on 01/24/01. | | | | After the second flow indication perturbation on 01/25/01, HPCI was again | | declared inoperable with an LCO start date of 01/23/01 at 0725 ET (7 days to | | returned HPCI to operable status). The cause of this condition is still | | under investigation. All other systems are operable. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * RETRACTED AT 1528 EST ON 3/23/01 BY MARK ABRAMSKI TO FANGIE JONES * * | | * | | | | "Engineering evaluation subsequent to this event has determined that the | | HPCI system would have performed its' intended function as credited in the | | LOCA analysis and therefore this 10 CFR 50.72 notification is retracted." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Kenneth | | Jenison) has been notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37779 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 02/24/2001| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 03:24[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 02/24/2001| +------------------------------------------------+EVENT TIME: 03:06[EST]| | NRC NOTIFIED BY: RAY MARTIN |LAST UPDATE DATE: 03/25/2001| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GLENN MEYER R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N N 0 Refueling |0 Refueling | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFEGUARDS DEGRADATION RELATED TO AREA BOUNDARY | | | | IMMEDIATE COMPENSATORY ACTIONS TAKEN UPON DISCOVERY | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. ADDITIONAL DETAILS MAY | | BE OBTAINED FROM THE OPERATIONS CENTER. | | | | * * * RETRACTED AT 2121 EST ON 3/25/01 BY RAY MARTIN TO FANGIE JONES * * * | | | | The licensee is retracting this event based on reportability evaluation. | | Additional details may be obtained from the operations center. | | | | The licensee intends to notify the NRC Resident Inspector. The R1DO | | (Kenneth Jenison) was informed. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37799 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 03/02/2001| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 10:10[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 03/02/2001| +------------------------------------------------+EVENT TIME: 05:30[EST]| | NRC NOTIFIED BY: KENNEDY |LAST UPDATE DATE: 03/23/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT DECLARED RCIC INOPERABLE. | | | | During a panel walkdown, it was discovered that the RCIC flow controller | | setpoint pointer was indicating erratically. Therefore, the flow controller | | was declared inoperable resulting in RCIC being declared inoperable. | | Troubleshooting is currently being performed on the controller. This | | condition put the plant in a 14-day LCO action statement. | | | | The NRC Resident Inspector will be notified. | | | | * * * UPDATE 1055EST ON 3/23/2001 FROM ERIC OLSON TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | "During a control room tour on Friday, March 2, 2001, the output of the | | reactor core isolation cooling system (RCIC) controller FIC-1340-1 was | | observed oscillating between downscale (-value) up to approximately +2% as | | indicated on the output demand meter. Initial testing measured voltages at | | the input test terminals and found a steady flow signal applied to the | | controller. Voltage measurements taken at the output test jacks found the | | output oscillating between 9 to 11 milliamps, consistent with the | | oscillation of 2% on the demand meter. In an effort to help pinpoint the | | source of this problem, the set-point tape was adjusted down to the minimum | | value allowing the deviation meter to come on scale (� 10% measuring the | | signal error between flow input and set-point). In this mode, oscillation of | | the deviation meter was observed, consistent with demand. The controller was | | then taken to manual and the output demand meter became stable. These two | | simple functional checks suggested the source of oscillation was limited to | | the automatic control circuitry of the GEMAC controller, based on the stable | | voltage measurement at the controllers input and the stable output when | | placed in manual. The most probable cause for the oscillation would be | | weak/aging power supply capacitors used in the controller's automatic | | circuitry. | | | | "The RCIC system was declared inoperable and the NRC was notified at 1010 on | | March 2, 2001 in accordance with 10CFR50.72(b)(3)(v) based on the belief | | that the controller was not operable. | | | | "Troubleshooting was performed and it was decided to replace the controller | | with the identical controller from the RCIC alternate shutdown panel (ASP). | | RCIC was then tested using procedure 8.5.5.1 with satisfactory results. The | | controller that had been removed from the RCIC panel was bench tested and | | the results indicated that the controller would have allowed the RCIC system | | to reach a stable rated 400 gpm flow control. | | | | "On Friday March 9, 2001, the controller from the alternate shutdown panel | | was also noted to be oscillating about the '0' position, repeating the | | condition described in PR01.9190. Problem report PR01.9210 was written to | | describe this similar condition. It was concluded that the RCIC test could | | be performed with the controller exhibiting some oscillation. The test | | results demonstrated that the controller and therefore, RCIC was operable. | | Further troubleshooting is in progress to determine the cause of the | | oscillations. One possibility is that the source of the oscillations has to | | do with equipment grounding and other equipment tests occurring on Fridays. | | Further investigation is in progress. | | | | "The reporting criteria of 10 CFR 50.73 were evaluated as follows; | | | | "For (a)(2)(v); not reportable. The initial observation on Friday, March 2, | | 2000, of oscillations on FIC-1340-1 indicated that the individual controller | | was inoperable and needed maintenance. The controller was replaced with the | | identical controller from the alternate shutdown panel (ASP). The newly | | installed controller was tested and RCIC was verified to be operable. Bench | | testing of the removed controller indicated that it would have performed its | | safety function. A similar oscillation was noted on the new controller on | | Friday March 9, 2001. RCIC was tested even though the controller appeared to | | be oscillating. The testing verified the operability of the installed | | controller and confirmed the conclusion that the original controller would | | have been operable. Since the original controller would have been operable, | | the observed oscillations could not have prevented the fulfillment of the | | RCIC safety function and therefore, is not a reportable condition. | | | | "It is recommended that the 10 CFR 50.72 notification made on March 2, 2001 | | be retracted." | | | | The licensee informed the NRC resident inspector. Notified R1DO(Jenison). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37809 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 03/05/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:56[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 03/05/2001| +------------------------------------------------+EVENT TIME: 16:00[EST]| | NRC NOTIFIED BY: K BELDEN |LAST UPDATE DATE: 03/23/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROOM EMERGENCY VENTILATION DECLARED INOPERABLE. | | | | Control Room Emergency Ventilation was declared inoperable at 1600 hours. | | This was a result of the Lab carbon sample analysis not meeting Technical | | Specification 3.4.5.c of greater than 90% radioactive methyl iodine | | removal capability when tested. This required entering into a 7 day | | shutdown Limiting Condition for Operation. Carbon sample analysis is | | required per Technical Specification to be performed once per cycle (2 | | years). Licensee is in the process of replacing the carbon. | | | | The NRC Resident Inspector was notified of this event. | | | | * * * RETRACTED AT 1411 EST ON 3/23/01 BY JOHN PARRISH TO FANGIE JONES * * | | * | | | | After further testing and calculations it was determined that the value was | | above the technical specification requirements and the event was not | | reportable and retracts the event notification. | | | | The licensee intends to notify the NRC Resident Inspector. The R1DO | | (Kenneth Jenison) has been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37844 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/17/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:55[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/16/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 11:00[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/23/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GEOFFREY WRIGHT R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SPAETH | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR 91-01 BULLETIN - GEOMETRY VIOLATION | | | | At 1100 on 3/16/01, a seal test buggy was found without signs or tags as | | required by NCSA-PLANT_031 (Potable Sampling/Test Buggies and Carts). Upon | | investigation of the test buggy, the chemical trap was found to have a | | nominal diameter of four inches and a length of twenty two inches. The four | | inch diameter violates the passive design control 2(b) which requires a | | three inch nominal diameter and a thirty three inch length. Nuclear | | Criticality personnel have determined the maximum loading of the effected | | trap to be 76 gram U-235 at 3% assay. 76 grams is lower than the 350 gram | | safe mass limit. The NCSE contingency analysis considers credible, a | | maximum five inch nominal diameter to remain subcritical. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | Safety significance is considered very low. The NCSA requirement is three, | | three inch nominal diameter chemical traps. However, the NCSE allows for | | three, five inch nominal diameter chemical traps and remain subcritical, | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | Based on the bounding calculations for five inch diameter chemical traps, | | there no critical pathways involved | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | Geometry is the controlled parameter that was violated | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | The amount of uranium is unknown, however, it is not expected to be above | | 350 grams U-235 due to the operation performed with this buggy and the fact | | that the maximum loading of a 4" X 22" chemical trap is only 76 grams U-235 | | at 3% assay. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES | | | | The control violated was the geometry control of the chemical trap. The | | chemical trap was required to be three inch schedule 40 pipe, but it was | | found to be a nominal four inch diameter pipe. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED; | | | | The test buggy was posted with temporary signs as required by | | NCSA-PLANT_031. The buggy will remain in the anomalous condition boundary | | until NDA results are obtained. Disposition of the buggy will be determined | | based on the NDA results. | | | | The NRC Resident Inspector was notified. The DOE Representative will be | | informed. | | | | * * * UPDATE AT 1346 EST ON 3/23/01 BY JIM McCLEARY TO FANGIE JONES * * * | | | | "NDA measurements show the chemical trap described above contains 1.6 +/- | | 0.8 grams and the pump contains 1 gram of U-235. Total U-235 content | | including error is 3.4 grams U-235. TSR 3.11.2 requires an NSCE for | | operations with uranium enriched to 1 wt% and contains 15 grams or higher | | U-235. Therefore this buggy is not a fissile material operation and not a | | violation of NCSA-PLANT_031." | | | | The licensee notified the NRC Resident Inspector and the DOE representative. | | The R3DO (Gary Shear) and NMSS EO (Brian Smith) were notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37861 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CALIFORNIA RADIATION CONTROL PRGM |NOTIFICATION DATE: 03/23/2001| |LICENSEE: TWINING LABS |NOTIFICATION TIME: 19:02[EST]| | CITY: FRESNO REGION: 4 |EVENT DATE: 03/16/2001| | COUNTY: STATE: CA |EVENT TIME: 07:00[PST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 03/23/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN PELLET R4 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT GREGGER | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN MOISTURE DENSITY GAUGE | | | | The Twining Labs reported a stolen Troxler moisture density gauge, Model | | 3430, serial # 20467. The sources are nominal 30 millicuries of Cs-137 and | | 10 millicuries Am-241/Be. The local police were notified (police report # | | 01-23615) and a reward was posted for the return. The theft occurred on | | 3/16/01 about 0700 PST. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37862 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COLUMBIA GENERATING STATIREGION: 4 |NOTIFICATION DATE: 03/24/2001| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 08:35[EST]| | RXTYPE: [2] GE-5 |EVENT DATE: 03/24/2001| +------------------------------------------------+EVENT TIME: 03:08[PST]| | NRC NOTIFIED BY: C. PERINO |LAST UPDATE DATE: 03/24/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |*SHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SHUTDOWN REQUIRED BY TECHNICAL SPECIFICATIONS | | | | "This report is being made in accordance with 10 CFR 50.72(b)(2)(i). | | | | "Columbia Generating Station started a plant shutdown 03:08. At 23:15 | | yesterday, a rise in drywell pressure was observed Coolant leakage was | | confirmed by a rising trend in drywell particulate monitors. Upon | | investigation, this leakage was confirmed to be due to cycling RCIC-V-63, | | the RCIC steam supply inboard isolation valve, during the performance of a | | Surveillance Procedure. | | | | "At 23:30, a rise in drywell unidentified leakage rate was observed. At | | 01:56 an entry into Technical Specification 3.4.5.B for greater than a 2 gpm | | rise in a 24 hour period was made. At 03:08, an entry into Technical | | Specification 3.4.5 A was made for unidentified leakage greater than 5 gpm. | | At this time, the decision to begin a controlled reactor shutdown was made. | | | | "RCIC-V-63 was backseated to terminate leakage at 03:55. At 03:58 it was | | determined the backseating successfully stopped the leakage. The downpower | | was terminated at 04:19. Indications of leakage are trending down. At 04:30, | | the leakage had decreased below the Technical Specification limits and | | reactor power was increased to 100%." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37863 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 03/24/2001| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 10:39[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/24/2001| +------------------------------------------------+EVENT TIME: 00:30[CST]| | NRC NOTIFIED BY: STEVEN SEWELL |LAST UPDATE DATE: 03/24/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 88 Power Operation |88 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION REGARDING DISCHARGE OF WATER OFFSITE | | | | "On 3/24/01, at 0845, a determination was made that a report to the TNRCC | | [Texas Natural Resource Conservation Commission] is required for a discharge | | of water to Squaw Creek Reservoir. An estimated 1000 gallons of fire | | protection water was discharged due to a ruptured pipe in warehouse C. The | | water contains no hazardous constituents that have assigned reportable | | quantities; however, a report to the TNRCC will be made in accordance with | | water quality regulations." | | | | The NRC resident inspector has been informed of this report by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37864 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 03/24/2001| | UNIT: [1] [] [] STATE: AR |NOTIFICATION TIME: 19:24[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 03/24/2001| +------------------------------------------------+EVENT TIME: 16:01[CST]| | NRC NOTIFIED BY: FRED VANBUSKIRK |LAST UPDATE DATE: 03/24/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN PELLET R4 | |10 CFR SECTION: | | |*DEG 50.72(b)(3)(ii)(A) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRESSURE BOUNDARY DEGRADATION FOUND DURING TESTING AFTER SHUTDOWN | | | | "On March 18, 2001, following shutdown for a scheduled refueling outage, | | Arkansas Nuclear One (ANO) Unit I performed a routine visual inspection of | | the Reactor Vessel (RV) head area per NRC Generic Letter 88-05. This | | inspection revealed an increase in the amount of boric acid crystals in the | | area of one Control Rod Drive Mechanism (CRDM) nozzle over the amount that | | had been present during the previous inspection. Results of the visual | | inspection were inconclusive regarding the source of the leakage. No other | | CRDM nozzle showed similar boron buildup. Prior to unit shutdown, on March | | 16 the total unidentified Reactor Coolant System leak rate was determined to | | be 0.087 gpm, significantly less than the 1 gpm allowed by Technical | | Specifications. After the RV head was removed and placed on the storage | | stand, additional inspections were conducted. At approximately 1601 on March | | 24, 2001, eddy current and ultrasonic testing revealed an RCS pressure | | boundary leak. Using ultrasonic test (UT) methods one crack was identified | | in the wall of CRDM nozzle #56. The UT data indicates that the crack is on | | the downhill side of the nozzle. It extends approximately 0.8 inches below | | the weld and extends upward to approximately 1.0 inches above the weld. The | | depth of the crack is approximately 0.2 inches. This crack is consistent | | with industry experience associated with Primary Water Stress Corrosion | | Cracking (PWSCC) in similar components that have been evaluated as part of | | the NRC Genetic Letter 97-01 response. These cracks do not pose a | | significant safety risk during plant operation. ANO plans to perform repairs | | during the current outage. Since the crack resulted in leakage through the | | Reactor Coolant System pressure boundary, this condition is being reported | | as a non-emergency eight-hour report in accordance with 10 CFR | | 50.72(b)(3)(ii), degradation of a principal safety barrier." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021