Event Notification Report for March 15, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/14/2001 - 03/15/2001 ** EVENT NUMBERS ** 37831 37835 37836 37837 37838 37839 37840 37841 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37831 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/13/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:24[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/12/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:45[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/14/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GEOFFREY WRIGHT R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE HALCOMB | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 - 24 HOUR REPORT | | | | The following is taken from the faxed report: | | | | ON 3/12/01 AT 1745 HOURS X-705 OPERATIONS PERSONNEL WERE CONDUCTING ROUTINE | | INSPECTIONS OF THE TUNNEL BASEMENT AREA WHEN THEY IDENTIFIED THAT THE | | SCAVENGER SYSTEM WOULD NOT OPERATE IN THE 'AUTOMATIC' OR THE 'MANUAL' MODE. | | NCSA-0705_035.A05 REQUIREMENT 5d STATES "THE SCAVENGER PUMP SWITCH VERIFIED | | NOT TO BE IN THE 'MANUAL' MODE WHILE UNATTENDED." THE STATUS OF THE | | SCAVENGER PUMP SWITCH WAS IN 'AUTOMATIC' MODE BUT IT WAS IDENTIFIED WHEN | | TESTED THAT THE PUMP WOULD NOT OPERATE IN THE 'AUTOMATIC' OR THE 'MANUAL' | | MODE BUT WOULD OPERATE IN THE 'MANUAL BY-PASS' MODE. THIS VIOLATES THE | | INTENT OF THE NCSA REQUIREMENT WHEREBY THE PUMP WOULD NOT START | | AUTOMATICALLY NOR WAS THE PUMP MANNED IN THE 'MANUAL' MODE. THE FACT THAT | | A TIME FRAME EXISTED WHEN THE PUMP WOULD NOT START IN THE 'AUTOMATIC' MODE | | AND DURING THIS SAME TIME FRAME THE PUMP WAS NOT MANNED IN THE 'MANUAL' | | MODE CONSTITUTES A LOSS OF ONE CONTROL WHICH IS RELIED ON TO MEET THE DOUBLE | | CONTINGENCY PRINCIPAL, | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | LOW = The failure of the Scavenger Pump to operate In the automatic mode | | represents the loss of one control (5d) relied upon for double contingency. | | The failure of the Scavenger Pump to operate in the automatic mode would | | allow the Scavenger System Storage Tank to overflow and solution to collect | | on the floor of the basement The size of the floor area and the remaining | | control on the amount of solution transferred make a criticality nearly | | non-credible. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR): | | | | Six of eight Fissile Solution Storage Banks fail in such a way that all of | | the Fissile Solution collects in the tunnel basement floor. This is | | sufficient Fissile Solution to exceed the safe depth of 1.5 inches for | | solutions containing greater than 100 wt.% U-235. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | Volume Control was lost when the Scavenger Pump failed. Geometry Control was | | maintained throughout this event. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OP CRITICAL MASS): | | | | The Tunnel Storage System receives Fissile Solution for various operations | | in the X-705 Facility. The most likely form is UO2F2 in solution with a | | maximum enrichment of 100 wt.% U-235. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | Automatic Mode of Scavenger Pump failed. Pump not manned in Manual Mode, 5d | | Control lost. Note: Pump would operate in the Manual By-Pass Mode but the | | pump was unmanned. Since no Fissile Solution leaked and allowed >1.5 inches | | of solution to collect on the floor the second control was maintained. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | Entered Anomalous Condition. Assigned Operator to man the system until | | facility status was verified. Immediately verified no evolutions in progress | | that could challenge the Scavenger System. Tagged out the power supplies to | | all facility equipment that could challenge the Scavenger System. Emergent | | Work authorized by Plant Shift Superintendent for repairs to Scavenger | | System. Called in off-duty Nuclear Criticality Safety Staff to assess | | compliance, create Anomalous Condition Report and oversee the efforts to | | establish the lost control. Control established at 2038 hours by manning the | | pump controls. | | | | The licensee notified the NRC Resident Inspector as well as the DOE | | representative. | | | | * * * UPDATE 1808EST ON 3/14/01 FROM JOE HALCOMB TO S. SANDIN * * * | | | | The following update was submitted to clarify the above report: | | | | "03/14/01 - Update #1 - The Nuclear Criticality Safety (NCS) Group performed | | a follow up assessment of the above event. A revision to the NCS Anomalous | | Condition Report was issued and it determined that the malfunction of the | | scavenger system did not constitute a loss of an NCS control and that double | | contingency was maintained. The previous issue would not have been reported | | based on the revised NCS Anomalous Condition Report." | | | | The licensee informed the NRC resident inspector and DOE site | | representative. Notified R3DO(Wright) and NMSS(Hickey). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37835 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SAINT VINCENT MEDICAL CENTER |NOTIFICATION DATE: 03/14/2001| |LICENSEE: BEST INDUSTRIES |NOTIFICATION TIME: 09:17[EST]| | CITY: BRIDGEPORT REGION: 1 |EVENT DATE: 03/12/2001| | COUNTY: STATE: CT |EVENT TIME: 17:00[EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 03/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETE ESELGROTH R1 | | |KEVIN RAMSEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: J. MELI | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEFECTIVE IODINE-125 SEEDS. | | | | One hundred thirty-three (133) I-125 sources each with an activity of | | approximately 0.3 millicuries were received by the Saint Vincent Medical | | Center located in Bridgeport, CT. The I-125 seeds are used for prostate | | implants. Upon receiving the sources they were counted and the seeds' | | activity was checked. They were then placed in a sterilization tray which | | has 10 wells (the seeds were distributed among the 10 wells). The tray | | has a cover which allows for steam circulation. The same day or the | | following morning the trays were sent forth to be sterilized. After | | sterilization the seeds are taken out of the sterilizer and the sterilizer | | surveyed. Nothing detectable was noted. Later that day the seeds were | | removed from the wells and loaded into needles. At the conclusion of this | | process the licensee did a survey of the area. It was then when the | | licensee found a rather high level of radiation, not high enough to be a | | seed. After further investigation the licensee concluded that the | | sterilization tray was contaminated and highly contaminated in the area of | | at least 5 of the 10 wells. The licensee's assumption is that one or more | | the seeds opened up during sterilization. The seeds were fine prior to | | sterilization. Total estimated removable contamination found on the tray | | was 4 microcuries. A more through survey was performed on everything that | | had came in contact with the tray. It was found that the inner wrapping | | that goes around the tray before it is placed in the sterilizer was | | contaminated. Nothing else that had come in contact with the tray was | | found to be contaminated. Personnel do not seem to be contaminated. The two | | people who were involved in the loading process are scheduled to have | | thyroid uptake exams today. This incident was reported to the seed | | manufacturer, Best Industries, and the seeds will be shipped back to them. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37836 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 03/14/2001| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 13:11[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 03/14/2001| +------------------------------------------------+EVENT TIME: 10:30[EST]| | NRC NOTIFIED BY: HUGH HAWKINS |LAST UPDATE DATE: 03/14/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETE ESELGROTH R1 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO VARIOUS AGENCIES CONCERNING AN OIL SPILL ONSITE | | | | "At 10:30 AM on 3/14/2001 the following agencies were notified of an oil | | leak on site. | | | | New Hampshire DES | | National Response Center | | US Coast Guard | | Environmental Protection Agency (EPA) | | | | "About 1 gallon of oil was observed on top of a concrete pad near the | | vehicle maintenance shop. The oil came through the pad via cracks in the | | concrete. There is an oil line that runs under this pad from a 6000 gallon | | above ground tank. The tank has been isolated, local storm drains have been | | protected and a contractor is on site to excavate the area and determine the | | extent of the problem. The notifications were made as a precautionary | | measure since the quantity of oil under the concrete pad is unknown. The | | oil was first observed on 3/13/01 at approximately 1600." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37837 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CHRISTIANA CARE HEALTH SERVICE |NOTIFICATION DATE: 03/14/2001| |LICENSEE: CHRISTIANA CARE HEALTH SERVICE |NOTIFICATION TIME: 13:15[EST]| | CITY: WILMINGTON REGION: 1 |EVENT DATE: 03/14/2001| | COUNTY: STATE: DE |EVENT TIME: 07:10[EST]| |LICENSE#: 07-12153-02 AGREEMENT: N |LAST UPDATE DATE: 03/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETE ESELGROTH R1 | | |FRITZ STURZ NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: EDWARD TORVIK | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT INVOLVING POTENTIAL PERSONNEL OVEREXPOSURE | | | | At approximately 0710EST a technician at the Christiana Care Health Services | | spilled a tube in the corner of the hot lab containing between 30-50 ml of | | Technetium-99m milked from the generator. The activity was measured as 650 | | millicuries immediately prior to the spill. The hot lab was promptly | | evacuated. There was no personnel contamination involved. Initial rad | | surveys of the affected area showed between 80 and 200 mr/hr prior to | | decontamination. Following final decontamination measured rad levels taken | | at 1000EST were approximately 10 to 40 mr/hr. Access to the lab has been | | restored, however, the corner area is taped off and covered by plastic to | | minimize the spread of contamination and allow for decay. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37838 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 03/14/2001| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 16:37[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/09/2001| +------------------------------------------------+EVENT TIME: 06:45[EST]| | NRC NOTIFIED BY: HARRY RUSSELL |LAST UPDATE DATE: 03/14/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLING INJECTION (HPCI) RENDERED INOPERABLE DUE TO FAULTY | | BATTERY CHARGER | | | | "Investigation of the failure of battery charger 1R42-S031 on 3/9/2001 | | (reference Condition Report 2001001827) has determined that the Unit 1 HPCI | | system was inoperable from the time of receipt of the first 'HPCI System | | Inverter Circuit Failure' annunciator until the time charger 1R42-S031 was | | removed from service. During this time (approximately 15 to 20 minutes), the | | HPCI system inverter was tripping on high voltage and resetting | | automatically when voltage levels returned to normal. The voltage | | fluctuations causing the inverter to trip and reset were caused by an | | internal fault in charger 1R42-S031: a bad fuse was making intermittent | | connection resulting in intermittent firing of the charger's | | silicon-controlled rectifiers (SCRs) and rapidly changing current and | | voltage outputs. These fluctuations and the random tripping of the HPCI | | system inverter rendered the HPCI system unreliable, and hence inoperable, | | until the cause of the fluctuations was corrected, that is, until the | | charger was removed from service. Determined to be reportable 3-14-2001 @ | | 1338 EST." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37839 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 03/14/2001| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 18:02[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/14/2001| +------------------------------------------------+EVENT TIME: 15:08[EST]| | NRC NOTIFIED BY: ROBERT R. BOESCH |LAST UPDATE DATE: 03/14/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |PETE ESELGROTH R1 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | |*INB 50.72(b)(3)(v)(B) POT RHR INOP | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED AN UNEXPECTED LOSS OF SHUTDOWN COOLING DUE TO TRIPPING OF | | VARIOUS POWER SUPPLY BREAKERS | | | | "Unit 2 was in Mode 5 on the fifth day of its 10th Refuel and Inspection | | Outage. At 1508 hours, the unit experienced an unexpected loss of Division 1 | | RPS Power supply. The loss of power was a result of the Electrical | | Protection Assembly (EPA) A & C breakers and motor generator output breaker | | tripping. The cause is under investigation. | | | | "The loss of power caused the RHR Shutdown Cooling suction valve HV251F009 | | to close. This is a common suction valve to both divisions of RHR and | | resulted in the complete loss of RHR Shutdown Cooling. The reactor currently | | has its head removed with the reactor cavity flooded up with the gates to | | the spent fuel pool removed. A Supplemental Decay Heat Removal system was in | | service at the time, but was not considered fully capable of decay heat | | removal. Reactor coolant temperature increased less than 2 degrees during | | the 37 minutes SDC was out of service. The RPS power supply was switched to | | its alternate supply and SDC was restored at 1545 hours. In accordance with | | 10CFR50.72(b)(3)(v) this represents a loss of a safety system which removes | | residual heat and requires an 8 hour ENS call. In addition to the isolation | | of RHR SDC, RWCU isolated due to containment valve HV244F001 closing, and | | Unit 2 HVAC Zone 3 (refuel floor) isolated. These isolations constitute an | | actuation of a Containment Isolation signal that affected multiple systems, | | and is reportable per | | 10CFR50.72(b)(3)(iv)(A)." | | | | Peak temperature after losing SDC was 105 degrees. The licensee informed the | | NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37840 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 03/14/2001| | UNIT: [2] [] [] STATE: PA |NOTIFICATION TIME: 20:13[EST]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 03/14/2001| +------------------------------------------------+EVENT TIME: 14:10[EST]| | NRC NOTIFIED BY: ROSS MOONITZ |LAST UPDATE DATE: 03/14/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETE ESELGROTH R1 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI DECLARED INOPERABLE DUE TO FAILURE OF EXHAUST LINE VACUUM RELIEF VALVES | | TO FUNCTION DURING IST TESTING | | | | "During routine testing of the Unit 2 High Pressure Coolant Injection system | | (HPCI) exhaust line vacuum relief valves (VRV), it was discovered that both | | VRVs failed to open at their In Service Test (IST) required differential | | pressure value. The Unit 2 HPCI system has been declared inoperable and | | repairs are in progress. | | | | "This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) due | | to a failure of a single train system which prevents fulfillment of a safety | | function." | | | | With HPCI inoperable this places Unit 2 in a 14-day Limiting Condition of | | Operation. All other ECCS systems have been verified operable. | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37841 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 03/14/2001| | UNIT: [] [2] [] STATE: FL |NOTIFICATION TIME: 20:20[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 03/14/2001| +------------------------------------------------+EVENT TIME: 17:52[EST]| | NRC NOTIFIED BY: DAVE WILLIAMS |LAST UPDATE DATE: 03/14/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED A TURBINE TRIP - REACTOR TRIP ON LOSS OF LOAD | | | | "At 1752 hours on 3/14/01, the St. Lucie Unit 2 reactor automatically | | tripped on a turbine loss of load signal. Prior to the trip, the output | | breaker on the 2A Control Element Drive motor generator set opened for an | | unknown reason. Shortly thereafter, various Control Rod trouble alarms | | annunciated and the Control Rods dropped into the core due to loss of power | | on the Control Rod busses. The loss of power to the Control Rod busses | | initiated a turbine trip, which in turn generated a Reactor Protective | | System trip signal on loss of load. All Control Rods inserted fully. | | Standard Post Trip actions were completed satisfactorily with all safety | | functions met. | | | | "Following the trip, it was noticed that the 2A1 non-safety related 6.9KV | | electric busses did not automatically transfer to the Startup Transformers. | | This resulted in the loss of power to the 2A1 and 2B2 Reactor Coolant Pumps | | and the 2A Main Feedwater pump. The cause for the failure to transfer is | | being investigated. Due to the loss of the Reactor Coolant Pumps, the | | Reactor Coolant System was manually depressurized to 1850 psia per plant | | procedures. | | | | "The Auxiliary Feedwater Actuation System automatically actuated on low | | Steam Generator level as expected for reactor trips from high power level. | | Steam Generator level is currently being maintained by the 2B Main Feedwater | | pump. | | | | "The reactor is currently stable in Mode 3 and the cause of the trip is | | under investigation." | | | | No primary safety or reliefs lifted during the transient. Decay heat is | | being removed via the bypass valves to the main condenser. The AFW pumps | | are operating but not supplying feed to the Steam Generators. The licensee | | had not verified whether any atmospheric dumps cycled. There is no known | | Steam Generator tube leakage at this time. Normal offsite power remains | | available and there was no impact on Unit 1 which is operating at 100% | | power. Unit 2 will remain in Hot Standby pending development and completion | | of corrective actions. The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021