Event Notification Report for March 14, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/13/2001 - 03/14/2001 ** EVENT NUMBERS ** 37805 37831 37832 37833 37834 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37805 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 03/03/2001| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 18:48[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 03/03/2001| +------------------------------------------------+EVENT TIME: 10:28[CST]| | NRC NOTIFIED BY: JOHN MYERS |LAST UPDATE DATE: 03/13/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA HOWELL R4 | |10 CFR SECTION: | | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | |*INB 50.72(b)(3)(v)(B) POT RHR INOP | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VARIOUS SAFETY SYSTEM ACTUATIONS DURING A PLANNED SHUTDOWN | | | | "While performing a planned shutdown for maintenance, an automatic scram and | | group isolations occurred due to low Reactor water level. | | | | "The sequence of events was as follows: Initial manual scram was inserted at | | 09:42 CST to complete the shutdown as part of the plant shutdown procedure. | | Following the initial manual scram, 'B' Reactor Feed Pump (RFP) tripped on | | high water level. 'A' RFP was previously secured as part of the shutdown | | procedure. For undetermined reasons, 'B' RFP was unable to be returned to | | service. An attempt was made to start the 'A' RFP but efforts were stopped | | due to high vibrations received on 'A' RFP. Reactor Core Isolation Cooling | | (RCIC) was manually started to provide make up to the RPV [Reactor Pressure | | Vessel]. The subsequent shrink due to the relatively cool water being added | | caused water level to lower to the low level scram set point (level 3), and | | at 10:28 CST an automatic scram initiated, together with Group 2 (Primary | | Containment), Group 3 (Reactor Water Cleanup) and Group 6 (Secondary | | Containment) isolations. The Scram and automatic isolations functioned as | | designed, except Group 3 had been previously actuated due to high | | Non-regenerative Heat Exchanger temperature while initiating blowdown to the | | main condenser for level control. Level was restored to approximately 17 | | inches above the low level scram set point and the scram was reset. RCIC | | flow was lowered in anticipation of swell due to heating, and level again | | lowered. A manual scram was inserted approximately 4 inches prior to the low | | level scram set point. Level was recovered using RCIC, and, following | | resetting of the scram, water level was restored to the normal level, RCIC | | secured, and condensate system used to raise level to the shutdown level | | band. Level is presently being maintained using the condensate system. | | | | "Investigation is on-going for the cause of being unable to restore 'B' RFP | | to service following the high level trip, and the reason for the high | | temperature isolation of RWCU [Reactor Water Cleanup]. | | | | "The Senior Resident Inspector has been notified." | | | | The licensee is making preparations to place the unit in cold shutdown in | | the next 2-4 hours. | | | | * * * UPDATE 1215EST ON 3/13/01 FROM DAVID VANDERKAMP TO S. SANDIN * * * | | | | The licensee is providing the following clarification as an update: | | | | "This is a follow-up report for event #37805 which was reported 3/3/2001 by | | Cooper Nuclear Station (CNS). The purpose of this follow-up is to clarify | | information provided in the initial eight hour report and to provide | | additional event information. | | | | "The initial report described reactor water level anomalies during a normal | | planned shutdown for a scheduled mid-cycle outage. The initial report | | indicated that the 'B' reactor feedwater pump could not be reset and | | restarted. It was also reported that the 'A' reactor feedwater pump was | | unavailable. However, a more accurate characterization of the condition is | | that the 'A' reactor feedwater pump was started after being shutdown for | | some time. Due to the cold condition, vibration levels higher than | | expected were observed. The highest vibrations seen were well below the | | procedural limit requiring turbine trip. Operators made a conscious decision | | not to use the 'A' reactor feedwater pump other injection sources were | | available. The 'A' reactor feedwater pump was available and operators were | | aware of its availability, if needed. | | | | "The shrink of water level that caused the automatic scram on low water | | level was initially attributed to the injection of cold water by RCIC. | | Subsequent evaluation has found that the shrink was due to a combination of | | the RCIC injection and that of steaming down due to normal pressure control | | via the Main Turbine Bypass Valves. Operators did not fully understand this | | interaction at the time of its occurrence. | | | | "An additional condition not described in the initial report is concerned | | with a transient on the Reactor Equipment Cooling (REC) System. In an | | attempt to control high reactor water level, a blowdown was established via | | the Reactor Water Cleanup (RWCU) System. This blowdown was excessive and | | caused boiling in the REC system at the RWCU Non-Regenerative Heat | | Exchanger. This boiling resulted in a rapid expansion of the REC system | | volume with the excess spilling out the REC surge tank vent. An automatic | | isolation of the RWCU system due to high temperature terminated the | | condition. Subsequent collapse of the steam voids in the REC System caused | | the level in the REC surge tank to drop below the Technical Specifications | | allowed value for 5 minutes. During this time period the REC System was | | declared inoperable and then was returned to operable status after operators | | refilled the surge tank. The REC System continued to operate during this | | transient. | | | | "The REC System is designed to provide cooling water for the removal of heat | | from equipment, such as the room coolers for the core spray pump rooms and | | HPCI pump room, required for a safe reactor shutdown following a Design | | Basis Accident or transient. With a loss of room cooling, the ability of the | | Emergency Core Cooling Systems to perform their required safety functions | | can no longer be assured. The investigation into the REC surge tank event | | continues, and the evidence to date indicates that the REC System transient | | was very short and REC remained available during the entire event. In | | addition, the reactor was shutdown during this transient. This potential | | loss of safety function is reportable as an eight hour report under | | 10CFR50.72(b)(3)(v)(B) pending a final evaluation. This is in addition to | | the eight hour report (Event #37805) previously made due to the valid | | actuation of the Reactor Protection System and Containment Isolation | | Systems. Both of these reports will be discussed in one Licensee Event | | Report (LER)." | | | | The licensee will inform the NRC resident inspector. Notified | | R4DO(Johnson). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37831 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/13/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:24[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/12/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:45[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/13/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GEOFFREY WRIGHT R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE HALCOMB | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 - 24 HOUR REPORT | | | | The following is taken from the faxed report: | | | | ON 3/12/01 AT 1745 HOURS X-705 OPERATIONS PERSONNEL WERE CONDUCTING ROUTINE | | INSPECTIONS OF THE TUNNEL BASEMENT AREA WHEN THEY IDENTIFIED THAT THE | | SCAVENGER SYSTEM WOULD NOT OPERATE IN THE 'AUTOMATIC' OR THE 'MANUAL' MODE. | | NCSA-0705_035.A05 REQUIREMENT 5d STATES "THE SCAVENGER PUMP SWITCH VERIFIED | | NOT TO BE IN THE 'MANUAL' MODE WHILE UNATTENDED." THE STATUS OF THE | | SCAVENGER PUMP SWITCH WAS IN 'AUTOMATIC' MODE BUT IT WAS IDENTIFIED WHEN | | TESTED THAT THE PUMP WOULD NOT OPERATE IN THE 'AUTOMATIC' OR THE 'MANUAL' | | MODE BUT WOULD OPERATE IN THE 'MANUAL BY-PASS' MODE. THIS VIOLATES THE | | INTENT OF THE NCSA REQUIREMENT WHEREBY THE PUMP WOULD NOT START | | AUTOMATICALLY NOR WAS THE PUMP MANNED IN THE 'MANUAL' MODE. THE FACT THAT | | A TIME FRAME EXISTED WHEN THE PUMP WOULD NOT START IN THE 'AUTOMATIC' MODE | | AND DURING THIS SAME TIME FRAME THE PUMP WAS NOT MANNED IN THE 'MANUAL' | | MODE CONSTITUTES A LOSS OF ONE CONTROL WHICH IS RELIED ON TO MEET THE DOUBLE | | CONTINGENCY PRINCIPAL, | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | LOW = The failure of the Scavenger Pump to operate In the automatic mode | | represents the loss of one control (5d) relied upon for double contingency. | | The failure of the Scavenger Pump to operate in the automatic mode would | | allow the Scavenger System Storage Tank to overflow and solution to collect | | on the floor of the basement The size of the floor area and the remaining | | control on the amount of solution transferred make a criticality nearly | | non-credible. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR): | | | | Six of eight Fissile Solution Storage Banks fail in such a way that all of | | the Fissile Solution collects in the tunnel basement floor. This is | | sufficient Fissile Solution to exceed the safe depth of 1.5 inches for | | solutions containing greater than 100 wt.% U-235. | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | Volume Control was lost when the Scavenger Pump failed. Geometry Control was | | maintained throughout this event. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OP CRITICAL MASS): | | | | The Tunnel Storage System receives Fissile Solution for various operations | | in the X-705 Facility. The most likely form is UO2F2 in solution with a | | maximum enrichment of 100 wt.% U-235. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | Automatic Mode of Scavenger Pump failed. Pump not manned in Manual Mode, 5d | | Control lost. Note: Pump would operate in the Manual By-Pass Mode but the | | pump was unmanned. Since no Fissile Solution leaked and allowed >1.5 inches | | of solution to collect on the floor the second control was maintained. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | Entered Anomalous Condition. Assigned Operator to man the system until | | facility status was verified. Immediately verified no evolutions in progress | | that could challenge the Scavenger System. Tagged out the power supplies to | | all facility equipment that could challenge the Scavenger System. Emergent | | Work authorized by Plant Shift Superintendent for repairs to Scavenger | | System. Called in off-duty Nuclear Criticality Safety Staff to assess | | compliance, create Anomalous Condition Report and oversee the efforts to | | establish the lost control. Control established at 2038 hours by manning the | | pump controls. | | | | The licensee notified the NRC Resident Inspector as well as the DOE | | representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37832 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: PENNSYLVANIA STATE UNIVERSITY |NOTIFICATION DATE: 03/13/2001| |LICENSEE: PENNSYLVANIA STATE UNIVERSITY |NOTIFICATION TIME: 11:39[EST]| | CITY: UNIVERSITY PARK REGION: 1 |EVENT DATE: 03/13/2001| | COUNTY: STATE: PA |EVENT TIME: [EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 03/13/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETE ESELGROTH R1 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC BOELDT | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING TRITIUM TUBE FROM EXIT SIGN | | | | During removal of tritium exit signs from the campus, one of the signs in | | the Academic Projects Building was found to be missing one of four tubes of | | tritium. The tube originally contained a maximum of 6 Curies in April, 1983 | | and 2.3 Curies today, it is not considered a hazard to the public. The | | licensee does not know if the tube was missing when the sign was installed | | or has been removed since. The sign was originally in a different building. | | The sign is a Everglow Safety Sign, model #710-1 and serial #14867. The | | licensee will contact NRC Region 1 (Thompson). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37833 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/13/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:18[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/13/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:15[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/13/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |GEOFFREY WRIGHT R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE HALCOMB | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY EQUIPMENT FAILURE RELATED TO STEAM LEAK ON AUTOCLAVE #3 | | | | "At 1415 hours on 3/13/01 after questioning by the Senior NRC Resident | | Inspector concerning a steam leak on autoclave (A/C) #3 in the X-344, it was | | discovered that an as found reading (pressure decay test) was not performed | | on A/C #3 prior to the Maintenance department replacing the o-ring during | | the evening of 3/12/01. Without performing the pressure decay test there is | | no possible method to verify if the o-ring would have performed its safety | | function. This test would have been used to determine if an observed steam | | leak on A/C #3 that occurred at 1050 hours during the early phase of an | | applicable heating mode on 3/12/01 would have been classified as a Safety | | Equipment Failure per the plant's NRC Event reporting Criteria. | | | | "Since the As Found Reading (pressure decay test) was not performed, the | | failure of the o-ring as observed by the steam leak on A/C #3 in the X-344 | | building, is being reported as a 'Safety Equipment Failure' per table 6.9.1 | | section J of the SAR." | | | | Operations has informed the NRC resident inspector and the DOE site | | representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37834 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 03/13/2001| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 18:07[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 03/13/2001| +------------------------------------------------+EVENT TIME: 14:45[EST]| | NRC NOTIFIED BY: JOHN HODDY |LAST UPDATE DATE: 03/13/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETE ESELGROTH R1 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) DECLARED INOPERABLE DUE EXCESSIVE | | MOISTURE IN LUBE OIL | | | | "At approximately 1100 hours, operators observed oil puddled around the HPCI | | lube oil sump vents and observed a slightly higher than normal sump level. | | The system engineer was consulted and recommended lowering sump level and | | sampling for moisture. | | | | "At 1445, water was observed in the sample taken from the HPCI lube oil | | sump. The amount of water observed (approximately 1/2 gallon) was such that | | compliance with a maximum recommended lube oil moisture content of 5% could | | not be assured. A conservative decision was made to declare HPCI | | inoperable. The system is inoperable but available. The plant is in a 7 | | day LCO per T.S. 3.5.C." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021