Event Notification Report for March 1, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/28/2001 - 03/01/2001 ** EVENT NUMBERS ** 37785 37786 37787 37788 37789 37791 37792 37793 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37785 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 02/28/2001| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 09:55[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 02/27/2001| +------------------------------------------------+EVENT TIME: 11:45[EST]| | NRC NOTIFIED BY: MORRISSEY |LAST UPDATE DATE: 02/28/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ACTUAL INTRODUCTION OF CONTRABAND INTO THE PROTECTED AREA. | | | | Immediate compensatory measures were taken upon discovery. | | | | Contact the HOO for additional information. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37786 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MISSISSIPPI DIV OF RAD HEALTH |NOTIFICATION DATE: 02/28/2001| |LICENSEE: GE INSPECTION SERVICES |NOTIFICATION TIME: 12:30[EST]| | CITY: REGION: 2 |EVENT DATE: 02/28/2001| | COUNTY: STATE: MS |EVENT TIME: 10:30[CST]| |LICENSE#: MS863-01 AGREEMENT: Y |LAST UPDATE DATE: 02/28/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |STEPHEN CAHILL R2 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: B. J. SMITH | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE OVEREXPOSURE OF RADIOGRAPHER | | | | The licensee notified the State of Mississippi that the TLD reading for an | | employee during the period of January 2001 was 14.624 rem. However, the TLD | | readings for the radiographer's assistants during the same period were | | normal, and the individual's pocket dosimeter indicated a total dose of | | approximately 350 mrem during the period. The licensee's RSO is | | investigating this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37787 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 02/28/2001| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 14:40[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/28/2001| +------------------------------------------------+EVENT TIME: [PST]| | NRC NOTIFIED BY: STEVEN DAVID |LAST UPDATE DATE: 02/28/2001| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA HOWELL R4 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO DISCOVERY OF THREATENED SPECIES ONSITE | | | | The licensee notified the National Marine Fisheries Service that a live | | green sea turtle was discovered in the plant intake structure. The turtle | | was released into the Pacific Ocean. The NRC resident inspector has been | | informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37788 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 02/28/2001| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 14:42[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 01/12/2001| +------------------------------------------------+EVENT TIME: 12:08[EST]| | NRC NOTIFIED BY: KELLEY MARSH |LAST UPDATE DATE: 02/28/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEPHEN CAHILL R2 | |10 CFR SECTION: |VERN HODGE NRR | |CCCC 21.21 UNSPECIFIED PARAGRAPH |RICHARD CONTE R1 | | |ANTON VEGEL R3 | | |LINDA HOWELL R4 | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 REPORT REGARDING A SUBSTANTIAL SAFETY HAZARD WITH A WOODWARD | | GOVERNOR EGB UNIT | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 1/12/01, V. C. Summer Nuclear Station (VCSNS) determined that a | | Substantial Safety Hazard could exist with Woodward governor EGB units | | failing to properly control the Emergency Diesel Generator [(EDG)]. A | | condition report (received on 1/12/01) from B. F. Goodrich/Fairbanks Morse | | indicated there was binding of the terminal shaft internal to an EGB unit | | removed from the 'A' EDG at VCSNS. The disassembly inspection found that | | the binding of the terminal shaft was due to the use of clamping screws, | | which were 1/8 inch longer than specification, resulting in binding on the | | output servo piston connecting rod. | | | | "This error was made during the prior refurbishment of the EGB by Engine | | Systems Inc. (ESI), the Woodward Governor nuclear representative, on | | 2/24/00. The use of the longer screws resulting in binding in the unit is | | considered a defect, which was introduced during the repair process by ESI. | | | | "[VCSNS] utilizes these EGB units on both the 'A' and 'B' EDGs. The above | | condition produced severe frequency oscillations on the output of the 'A' | | EDG. This condition could have been introduced to any EGB during | | refurbishment by ESI, passed acceptance testing, and be present on both | | EDGs. In an emergency condition, both EDGs could fail, resulting in the | | loss of safety function for the emergency on-site power supply. | | | | "The EGB units currently installed on both EDGs have been refurbished by | | Fairbanks Morse with properly specified parts. Fairbanks Morse will perform | | all future EGB refurbishment work for VCSNS. Other cause and corrective | | actions associated with the governor issues are being addressed under Root | | Cause Analysis report RCA 01-0235, 'Diesel Generator 'A' Governor Problems.' | | " | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37789 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COLUMBIA GENERATING STATIREGION: 4 |NOTIFICATION DATE: 02/28/2001| | UNIT: [2] [] [] STATE: WA |NOTIFICATION TIME: 15:13[EST]| | RXTYPE: [2] GE-5 |EVENT DATE: 02/28/2001| +------------------------------------------------+EVENT TIME: 10:57[PST]| | NRC NOTIFIED BY: MIKE KELLER |LAST UPDATE DATE: 02/28/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA HOWELL R4 | |10 CFR SECTION: |CHARLES MILLER IRO | |NINF INFORMATION ONLY |ED GOODWIN NRR | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EARTHQUAKE FELT ONSITE | | | | At 1057PST an earthquake in Western Washington State with a magnitude of 7.0 | | was felt onsite. The epicenter is located 11.3 miles NE of Olympia, WA and | | 14.9 miles West South West of Tacoma, WA. The depth of the earthquake was | | 30 miles. Seismic sensors did not detect the seismic activity. Plant | | inspection performed after the earthquake found no abnormal conditions. | | | | The NRC Resident Inspector was notified of this information call by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37791 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 03/01/2001| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 03:19[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 03/01/2001| +------------------------------------------------+EVENT TIME: 00:17[EST]| | NRC NOTIFIED BY: SIMPSON |LAST UPDATE DATE: 03/01/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEPHEN CAHILL R2 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 1 Startup |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WAS MANUALLY TRIPPED AT LESS THAN 1% POWER | | | | | | A manual reactor trip was initiated at 0017 on 3/01/01 due to 2 shutdown | | control rods remaining on the bottom while initiating control rod | | withdrawal. This occurred during low power physics testing and a trouble | | shooting plan for a misaligned Shutdown bank B Control rod (G-9). The rod | | had already been realigned to the other rods in shutdown bank B @ 43 steps. | | The Shutdown bank was inserted into the core to zero steps per the trouble | | shooting plan. After the step counters and rod control were reset and | | Shutdown bank B rods were being withdrawn, it was discovered that 2 rods had | | not moved and were still on the bottom with 14 steps demanded. The Shutdown | | bank was re-inserted to zero steps (fully inserted). After further | | discussion, the shift supervisor called for a manual reactor trip. The | | reactor operator tripped the Reactor and the Crew entered the Emergency | | Operation Procedures (EOP-1.0, Reactor trip/safety injection, and EOP-1.1, | | Reactor trip recovery). All systems functioned as designed. The problem | | with the rod control system is not understood and trouble shooting is | | continuing. | | | | | | Note: The 2 rods that did not move were rods G-9 and L-5, both in Shutdown | | bank B. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37792 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 03/01/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 05:42[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 03/01/2001| +------------------------------------------------+EVENT TIME: 05:00[EST]| | NRC NOTIFIED BY: KICH |LAST UPDATE DATE: 03/01/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED STATE AND COUNTY OFFICIALS OF A TRANSIT STRIKE IN | | WESTCHESTER COUNTY. | | | | The licensee was notified that transit employees of the Liberty Bus Company | | in Westchester County will be going on strike. The licensee made the | | offsite notifications to assure that the contingency plans are in effect to | | deal with the strike. | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37793 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 03/01/2001| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 06:33[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 03/01/2001| +------------------------------------------------+EVENT TIME: 05:00[EST]| | NRC NOTIFIED BY: YOUNG |LAST UPDATE DATE: 03/01/2001| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED STATE AND COUNTY OFFICIALS OF A TRANSIT STRIKE IN | | WESTCHESTER COUNTY. | | | | The licensee was notified that transit employees of the Liberty Bus Company | | in Westchester County will be going on strike. The licensee made the | | offsite notifications to assure that the contingency plans are in effect to | | deal with the strike. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021