Event Notification Report for February 15, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/14/2001 - 02/15/2001 ** EVENT NUMBERS ** 37743 37744 37745 37746 37747 37748 37749 37750 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37743 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 02/14/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 02:51[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 02/14/2001| +------------------------------------------------+EVENT TIME: 01:50[EST]| | NRC NOTIFIED BY: MARK LEONE |LAST UPDATE DATE: 02/14/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 | |10 CFR SECTION: |JOHN ZWOLINSKI NRR | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LOSS OF A 480-VOLT BUS DUE TO A PERSONNEL ERROR DURING SURVEILLANCE | | TESTING RESULTED IN THE AUTOMATIC START OF THREE EMERGENCY DIESEL | | GENERATORS. | | | | At 0150 on 02/14/01, 480-volt bus 3A was lost due to incorrect operation of | | a switch during performance of a surveillance test. An individual | | performing the test needed to simultaneously hold a switch in the bypass | | position while a test button was pressed, and the switch was not held in the | | correct position. As a result, an undervoltage signal was inserted on the | | bus when the test button was pushed, and all three emergency diesel | | generators automatically started as designed. | | | | The licensee stated that the emergency diesel generators do not | | automatically load on the loss of an internal bus and that all automatic | | functions operated properly. The licensee also stated that the loss of any | | 480-volt bus places the unit in a shutdown action statement in accordance | | with Technical Specification 3.0.1. However, power (via an emergency diesel | | generator) was restored to the bus in accordance with procedures at 0215, | | and restoration of power satisfied the action statement requirements in | | Technical Specification 3.0.1 within 25 minutes. The licensee is currently | | in the process of restoring normal bus power supply. | | | | The licensee stated that bus 3A is one of the power supplies for the 22 | | safety injection pump. This bus also supplies power to the 21 residual heat | | removal pump, 22 and 25 service water pumps, 24 fan cooler unit, 21 | | auxiliary boiler feed pump, 22 charging pump, 21 backup heater for the | | pressurizer, and 23 instrument bus (via the 23 battery charger). | | | | The licensee plans to notify the NRC resident inspector and applicable | | government agencies. The licensee may also issue a press release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37744 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HONEYWELL INTERNATIONAL, INC. |NOTIFICATION DATE: 02/14/2001| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 07:44[EST]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 02/14/2001| | |EVENT TIME: 02:30[CST]| | |LAST UPDATE DATE: 02/14/2001| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |MONTE PHILLIPS R3 | | DOCKET: 04003392 |FRED BROWN NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HUGH ROBERTS | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |JBBE 40.60(b)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SANITARY WELL WATER FAILURE DUE TO A LINE RUPTURE (24-Hour Report involving | | the potential inability to mitigate the circumstances of an accident) | | | | Honeywell Metropolis Works is a fuel cycle facility that performs UF6 | | conversion. | | | | At approximately 0230 CST, a 6-inch diameter sanitary process line ruptured. | | As a result, the licensee secured (shut down) both the safety showers and | | the process. The ruptured line has been isolated, and process water has | | been valved into the safety showers. However, the licensee has not yet | | brought up the process. Repair planning is underway. | | | | The licensee plans to notify the NRC Region 3 office, an onsite NRC | | inspector (Mary Thomas), and the NRC resident inspector at Paducah (Courtney | | Blanchard). (The USEC Paducah facility is located across the river.) | | | | Call the NRC operations officer for a licensee contact telephone number. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37745 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MERCY HOSPITAL |NOTIFICATION DATE: 02/14/2001| |LICENSEE: MERCY HOSPITAL |NOTIFICATION TIME: 09:37[EST]| | CITY: PORT HURON REGION: 3 |EVENT DATE: 02/13/2001| | COUNTY: STATE: MI |EVENT TIME: 23:30[EST]| |LICENSE#: 211563801 AGREEMENT: N |LAST UPDATE DATE: 02/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MONTE PHILLIPS R3 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHUCK SMITH | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MISADMINISTRATION AT MERCY HOSPITAL IN PORT HURON, MICHIGAN | | | | A patient was receiving a treatment with a gynecological implant containing | | two cesium-137 sources (with 13.74 milligrams radium equivalent each). The | | patient was reportedly restless and moving around quite a bit, and the | | applicator was in its proper position at 2100. However, when nurses checked | | on positioning of applicator at 2330 on 02/13/01, it was discovered that | | the applicator had gotten past the sutures and come out completely. The | | implant treatment procedure was terminated at that time. | | | | Based on the minimum and maximum amount of time that the applicator may have | | been in the proper position, the patient received between 66% and 71% of the | | intended dose. Conservative calculations (assuming that the applicator came | | out at 2100) revealed doses to unintended areas were not anticipated to | | cause adverse health complications as a result of this exposure. The | | patient has been informed. | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37746 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 02/14/2001| |LICENSEE: RONE ENGINEERS |NOTIFICATION TIME: 10:00[EST]| | CITY: DALLAS REGION: 4 |EVENT DATE: 02/03/2001| | COUNTY: STATE: TX |EVENT TIME: [CST]| |LICENSE#: L02356 AGREEMENT: Y |LAST UPDATE DATE: 02/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN, JR. (fax) | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING A STOLEN TROXLER NUCLEAR DENSITY GAUGE | | | | The following text is a portion of a facsimile received from the Texas | | Department of Health, Bureau of Radiation Control: | | | | "This is an initial notification of a stolen nuclear gauge. The gauge was | | stolen on Saturday February 3, 2001, from the parking lot of the Midway | | Point Restaurant, [...], Dallas, Texas, while the [driver] ate lunch between | | jobs. The Licensee's initial report indicates that the gauge was secured in | | it's transport case and chained to the company pickup with chain and lock. | | The driver noted that the gauge, the lock, and chain were all missing. The | | stolen gauge was a Troxler Model 3430, Serial Number 31580. The gauge | | contained two sources: 8 millicuries of Cs-137, Source Serial No. 750-6419, | | and 40 millicuries of Am-241:Be, Source Serial No. 47-28229. A Police | | Report was filed with the Dallas Police Department (Report Service | | #0083748-K - [...]). The operator reported the loss to his supervisor and a | | report was telephoned to this Agency on February 5, 2001. Two written | | reports were faxed to the Agency [...]. The gauge has not been recovered to | | date. An Agency investigation is ongoing. The Texas Licensee (L02356) is | | Rone Engineers [located in] Dallas, Texas [...]." | | | | (Call the NRC operations officer for contact information.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37747 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 02/14/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 10:49[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 02/14/2001| +------------------------------------------------+EVENT TIME: 04:08[EST]| | NRC NOTIFIED BY: PHIL SANTINI |LAST UPDATE DATE: 02/14/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 | |10 CFR SECTION: |TAD MARSH NRR | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE FIRE HEADER IMPAIRMENT AND SURVEILLANCE PER STATION | | ADMINISTRATIVE ORDER (SAO) 703 (24-Hour Report in accordance with the | | license) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "The high pressure Fire Water Protection System is degraded due to planned | | maintenance work. The inner and outer high-pressure fire headers are split | | to provide protection for work on the valves for [the] 12 Fire Main Booster | | Pump. [The] 12 Fire Main Booster Pump is inoperable during this tag-out. | | The diesel fire pump is in service as the alternate fire protection for the | | outside fire header. [The] 11 Fire Main Booster Pump is in service for the | | inside header. SAO-703 states [that] one fire main booster pump out of | | service is a 7-day action statement to return it to operable status. The | | headers being separated or any part of the fire protection piping or valves | | not being able to perform [their] function other than the specific instances | | described in SAO-703 [require] an alternate fire protection system shall be | | established. This was established within 24 hours to ensure compliance with | | SAO-703 as described above. A special report shall be submitted to the NRC | | Regional Administrator of the Region 1 Office outlining this issue within 14 | | days." | | | | The licensee notified the NRC resident inspector and plans to notify the NRC | | Region 1 office (Pete Eselgroth). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37748 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 02/14/2001| |LICENSEE: DRASH CONSULTING ENGINEERS, INC. |NOTIFICATION TIME: 12:33[EST]| | CITY: HARLINGEN REGION: 4 |EVENT DATE: 01/01/2001| | COUNTY: STATE: TX |EVENT TIME: [CST]| |LICENSE#: TX L04724 AGREEMENT: Y |LAST UPDATE DATE: 02/14/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HELEN WATKINS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT OF STOLEN HUMBOLDT GAUGE | | | | The following text is a portion of a facsimile received from the Texas | | Department of Health, Bureau of Radiation Control: | | | | "On Monday January 1, 2001, a moisture/density gauge was stolen from the | | back of a pickup truck that was parked at an apartment complex in Harlingen, | | Texas. The technician who had used the gauge went to his apartment from | | 10:00 am to 1:00 pm after completing work at one job site. When the | | technician was getting into his truck, he noticed the lid on the gauge | | transport case was cracked open and the gauge was missing. | | | | "The stolen gauge is a Humboldt Model 5001-C, serial number 1467. The gauge | | contained two sources: | | 10 millicuries of Cs-137, source serial No. 692GH, and 40 millicuries of | | Am-241:Be, source serial No. | | NJO1429. | | | | "The Licensee notified the Harlingen Police Department, this Agency, and the | | manufacturer. The Licensee placed an ad in a local newspaper offering a $500 | | reward for the return of the gauge." | | | | Call the NRC operations officer for contact information. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37749 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 02/14/2001| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 17:05[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 02/14/2001| +------------------------------------------------+EVENT TIME: 08:51[CST]| | NRC NOTIFIED BY: BRUCE SCHOENBACH |LAST UPDATE DATE: 02/14/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GREG PICK R4 | |10 CFR SECTION: | | |*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH TRAINS OF CONTAINMENT COOLERS AND ONE TRAIN OF CONTAINMENT SPRAY | | INOPERABLE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 2/14/01, the 'A' train containment cooling train was removed from | | service at 0507 CST for associated circuit breaker work. At 0851 CST the 'B' | | Train Essential Service Water pump was started to support performance of the | | 'A' Train SIS/CIS Slave Relay Test. | | | | "The 'B' Essential Service Water pump failed to achieve rated flow and | | pressure and was declared inoperable at 0851 CST. This resulted in entry | | into Technical Specification LCO 3.6.6, Required Action F.1 for both trains | | of containment coolers inoperable and one train ('B') of Containment Spray | | inoperable. LCO 3.6.6 Required Action F.1 also requires entry into LCO | | 3.0.3. Technical Specification 3.0.3 was entered at 0851 CST and exited at | | 1123 CST when the 'A' train of Containment Cooling was returned to service. | | The plant remains in Technical Specification LCO 3.7.8 Required Action A.1 | | (72-Hour Action Statement) for one train ('B') of Essential Service Water | | inoperable. | | | | "This condition at the time of discovery could have prevented the | | fulfillment of the safety function of structures or systems that are needed | | to control the release of radioactive material or mitigate the consequences | | for an accident. It was concluded that this event was reportable per | | 10CFR50.72(b) (3) (v) since: | | | | (1) Both trains of containment cooling were lost as a result of the | | unanticipated failure of the 'B' train Essential Service Water pump in | | conjunction with the 'A' train containment coolers being removed from | | service. | | (2) Cascading through technical specification resulted in the loss of 'B' | | train containment spray system. | | | | "The failure of the 'B' train Essential Service Water pump is under | | evaluation." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37750 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 02/14/2001| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 20:00[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 02/14/2001| +------------------------------------------------+EVENT TIME: 16:00[CST]| | NRC NOTIFIED BY: GARY HARRINGTON |LAST UPDATE DATE: 02/14/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |*UNA 50.72(b)(3)(ii)(B) UNANALYZED COND OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 96 Power Operation |96 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ANALYSES OF AN ELECTRICAL BOX DOES NOT MEET THE FIRE RESISTANCE OF APPENDIX | | R | | | | The Kewaunee Engineering staff, while conducting a review, recognized that | | they could provide no analyses to support compliance to 10CFR50, Appendix R, | | for an electrical wiring pull box. The box provides an enclosure for | | dedicated safe shutdown equipment wiring, 'A' train equipment. The box is | | located in an alternate safe shutdown equipment room, 'B' train, where the | | box provides protection against fire. However, though the analyses of the | | box provides assurance that the design will protect the 'A' train equipment | | wiring from a fire, it does not provide a three hour barrier consistent with | | Appendix R requirements. Therefore, this places the plant in an unanalyzed | | condition. The box was designed and installed in the early to mid 1980s. | | Compensatory measures have been taken to ensure continued safe plant | | operation. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021