Event Notification Report for February 14, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/13/2001 - 02/14/2001 ** EVENT NUMBERS ** 37731 37737 37738 37739 37740 37741 37742 37743 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37731 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. ARMY |NOTIFICATION DATE: 02/09/2001| |LICENSEE: U.S. ARMY |NOTIFICATION TIME: 11:19[EST]| | CITY: REGION: 3 |EVENT DATE: 02/08/2001| | COUNTY: STATE: IL |EVENT TIME: [CST]| |LICENSE#: 12-00722-06 AGREEMENT: Y |LAST UPDATE DATE: 02/13/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KEN BROCKMAN R4 | | |DR. COOL NMSS | +------------------------------------------------+BRENT CLAYTON R3 | | NRC NOTIFIED BY: JOYCE KUYKENDALL | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST SOURCE AT FT. RILEY, KANSAS | | | | The U.S. Army Aberdeen Proving Grounds reported the loss of a chemical agent | | detector, model number M43A1. The detector contains 300 microcuries of | | Am-241. The exact date, time and circumstances of the loss are not known. | | | | * * * UPDATE 1150EST ON 2/13/01 FROM JEFF HAVENNER TO S. SANDIN * * * | | | | The Rock Island Depot updated this report to provide the following | | additional details: The detector was lost during an Infantry training | | exercise. The unit involved is currently at Ft. Irwin, CA and unavailable | | for questioning. The RSO at Ft. Riley intends to conduct a search of the | | exercise area when the snow melts. Notified R1DO(Anderson), R3DO(Phillips) | | and NMSS(Sturz). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37737 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MA RADIATION CONTROL PROGRAM |NOTIFICATION DATE: 02/13/2001| |LICENSEE: AEATECH QSA, INC. |NOTIFICATION TIME: 10:00[EST]| | CITY: REGION: 1 |EVENT DATE: 02/12/2001| | COUNTY: STATE: MA |EVENT TIME: 14:45[EST]| |LICENSE#: 12-8361 AGREEMENT: Y |LAST UPDATE DATE: 02/13/2001| | DOCKET: 99-0014 |+----------------------------+ | |PERSON ORGANIZATION | | |CLIFFORD ANDERSON R1 | | |GREG PICK R4 | +------------------------------------------------+FREDRICK STURZ NMSS | | NRC NOTIFIED BY: ROBERT GALLAGHAR | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SEALED SOURCE DELIVERED TO THE INCORRECT ADDRESS | | | | On 01/25/01 AEA Technology QSA, Inc., shipped a packaged 500 mCi | | promethium-147 sealed source via FED EX to Impact Systems located in Los | | Gatos, CA. On 02/01/2001 Impact Systems called AEA Technology QSA asking | | where the package was. AEA Technology QSA, Inc., contacted FED EX and was | | informed that the package had been delivered to Fastech Integration, Inc., | | located at 101 Albright St., Los Gatos, CA. | | | | FED EX went back to the address to reclaim the package and to complete the | | delivery to Impact Systems. FED EX said that they would notify AEA | | Technology QSA, Inc., and let them know if there was a problem. | | | | AEA Technology QSA, Inc., received a second call from Impact Systems on | | 02/07/01 asking where the package was. AEA Technology QSA, Inc., | | immediately contacted FED EX on 02/07/01. On 02/12/01 FED EX informed AEA | | Technology QSA, Inc., that they had gone back to Fastech Integration, Inc., | | and spoke to the individual who has signed for the package, but the receiver | | stated she did not have the package. | | | | The State of Massachusetts informed the State of California of this event | | and are still following up on this event. | | | | * * * UPDATE AT 1511 EST ON 2/13/01 BY ROBERT GALLAGHAR TO FANGIE JONES * * | | * | | | | The source has been located by Fastech Integration, Inc. and delivered to | | Impact Systems, the company that ordered the source. The package was | | intact. The State of Massachusetts will inform the State of California of | | the event update. | | | | The R1DO (Clifford Anderson), R4DO (Greg Pick), and NMSS (Fred Sturz) have | | been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37738 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 02/13/2001| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 10:57[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 02/13/2001| +------------------------------------------------+EVENT TIME: 10:40[EST]| | NRC NOTIFIED BY: JACK BREEN |LAST UPDATE DATE: 02/13/2001| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KEN BARR R2 | |10 CFR SECTION: | | |*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FLORIDA FISH AND WILDLIFE CONSERVATION COMMISSION WAS NOTIFIED THAT A SICK | | SEA TURTLE NEEDED REHABILITATION. | | | | The licensee rescued a sea turtle from the intake canal. As a result, the | | licensee notified the Florida Fish and Wildlife Conservation Commission that | | the turtle had been rescued and needed rehabilitation. | | | | The resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37739 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COOPER POWER SYSTEMS INC |NOTIFICATION DATE: 02/13/2001| |LICENSEE: COOPER POWER SYSTEMS INC |NOTIFICATION TIME: 11:53[EST]| | CITY: FRANKSVILLE REGION: 3 |EVENT DATE: 01/18/2001| | COUNTY: STATE: WI |EVENT TIME: [CST]| |LICENSE#: 48-173-83-02 AGREEMENT: N |LAST UPDATE DATE: 02/13/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MONTE PHILLIPS R3 | | |FRITZ STURZ NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: OWEN | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE REPORTED A MISSING ELECTRON CAPTURE DETECTOR | | | | During a physical inventory of radiation sources, the licensee reported that | | an electron capture detector for a gas chromatograph, used in a chem lab, | | was missing on the last inventory performed on 01/18/01. The device was a | | PerkinElmer model PE009-0282 serial # 1648 containing Ni-63 <15 millicuries. | | A search was made, but the device did not show up. It was last inventoried | | approximately three years ago. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37740 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNION HOSPITAL |NOTIFICATION DATE: 02/13/2001| |LICENSEE: UNION HOSPITAL |NOTIFICATION TIME: 15:42[EST]| | CITY: TERRE HAUTE REGION: 3 |EVENT DATE: 02/13/2001| | COUNTY: VIGO STATE: IN |EVENT TIME: [CST]| |LICENSE#: 12-16457-01 AGREEMENT: N |LAST UPDATE DATE: 02/13/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MONTE PHILLIPS R3 | | |E. WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DEAN TAYLOR | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST SOURCE - SEED USED FOR PROSTATE PROCEDURE | | | | The hospital discovered that one seed out of 110 seeds, apparent activity is | | .311 mCi I-125 (full activity is .587 mCi) was missing after the completion | | of an implant procedure. An extensive search of the operating room, | | equipment, drains, laundry, and hallways failed to discover the missing | | seed. The patient was scanned and the best analysis is that the patient | | received the proper number of seeds. There is little or no threat to the | | public health or safety. The hospital contacted NRC Region 3. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37741 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ARIZONA RADIATION REGULATORY AGENCY |NOTIFICATION DATE: 02/13/2001| |LICENSEE: RICKER-ATKINSON-McBEE & ASSOC. |NOTIFICATION TIME: 17:11[EST]| | CITY: REGION: 4 |EVENT DATE: 02/13/2001| | COUNTY: STATE: AZ |EVENT TIME: [MST]| |LICENSE#: 07-406 AGREEMENT: Y |LAST UPDATE DATE: 02/13/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |E. WILLIAM BRACH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WILLIAM WRIGHT | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT OF A STOLEN TROXLER GAUGE | | | | "This first notice constitutes EARLY notice of events of POSSIBLE safety or | | public interest significance. The information is that which is available | | after preliminary investigation and is basically all that is known by the | | Agency Staff at this time. | | | | "Date: 02/13/01 | | Time: 0430-0815 AM, MST | | First Notice No. 01-01: | | | | "Arizona Licensee: Ricker-Atkinson-McBee & Assoc. | | License: No. 07-406 | | | | "Description of the event: Between the hours of 0430 AM and 0815 AM a | | Troxler Moisture Density Gauge, Model #3440, S/N 26981 was stolen from the | | licensee's facility while locked and chained in the bed of the users 2000 | | Dodge Dakota Pickup Truck, Arizona Lic. #523FCY. The gauge and scatter block | | were removed from the transport case and the case remained in the pickup. A | | reward of $500.00 is being offered by the licensee upon return of the | | gauge. | | | | "The states of Utah, California, Colorado, New Mexico, and U.S. NRC Region | | IV, USNRC-DC, USFBI and the governor's office are being informed of this | | incident." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37742 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 02/13/2001| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 21:18[EST]| | RXTYPE: [3] CE |EVENT DATE: 02/13/2001| +------------------------------------------------+EVENT TIME: 16:54[CST]| | NRC NOTIFIED BY: CHARLES DeDEAUX |LAST UPDATE DATE: 02/13/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GREG PICK R4 | |10 CFR SECTION: | | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 A/R Y 82 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING TURBINE VALVE TESTING | | | | "On 2/13/2001 at 1654 CST Waterford 3 sustained a reactor trip from 82% RTP. | | The reactor trip was most probably caused by variable over power trip, which | | is a core protection calculator auxiliary trip. Actuation of the emergency | | feedwater system also occurred due to shrinkage of coolant in the steam | | generator caused by the reactor trip; however, no emergency feedwater was | | actually fed into the steam generators. Actuation of the emergency feedwater | | system is a normal occurrence following a reactor trip. This condition is | | reportable under 10CFR50.72(b)(2)(iv)(B), any event or condition that | | results in actuation of the reactor protection system when the reactor is | | critical, which is a 4 hour report; and 10CFR50.72(b)(3)(iv)(A), any event | | or condition that results in valid actuation of the emergency feedwater | | system, which is an 8 hour report. At the time of the trip Waterford 3 was | | performing turbine valve testing per OP-903-007. Governor Valve 3 was being | | tested and sporadically started opening and closing." | | | | The plant is stable in Hot Standby with excess heat removed via forced | | circulation to the steam generators and steam released through the bypasses | | to the main condensers. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37743 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 02/14/2001| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 02:51[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 02/14/2001| +------------------------------------------------+EVENT TIME: 01:50[EST]| | NRC NOTIFIED BY: MARK LEONE |LAST UPDATE DATE: 02/14/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | NRR | |*ESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LOSS OF A 480-VOLT BUS DUE TO A PERSONNEL ERROR DURING SURVEILLANCE | | TESTING RESULTED IN THE AUTOMATIC START OF THREE EMERGENCY DIESEL | | GENERATORS. | | | | At 0150 on 02/14/01, 480-volt bus 3A was lost due to incorrect operation of | | a switch during performance of a surveillance test. An individual | | performing the test needed to simultaneously hold a switch in the bypass | | position while a test button was pressed, and the switch was not held in the | | correct position. As a result, an undervoltage signal was inserted on the | | bus when the test button was pushed, and all three emergency diesel | | generators automatically started as designed. | | | | The licensee stated that the emergency diesel generators do not | | automatically load on the loss of an internal bus and that all automatic | | functions operated properly. The licensee also stated that the loss of any | | 480-volt bus places the unit in a shutdown action statement in accordance | | with Technical Specification 3.0.1. However, power (via an emergency diesel | | generator) was restored to the bus in accordance with procedures at 0215, | | and restoration of power satisfied the action statement requirements in | | Technical Specification 3.0.1 within 25 minutes. The licensee is currently | | in the process of restoring normal bus power supply. | | | | The licensee stated that bus 3A is one of the power supplies for the 22 | | safety injection pump. This bus also supplies power to the 21 residual heat | | removal pump, 22 and 25 service water pumps, 24 fan cooler unit, 21 | | auxiliary boiler feed pump, 22 charging pump, 21 backup heater for the | | pressurizer, and 23 instrument bus (via the 23 battery charger). | | | | The licensee plans to notify the NRC resident inspector and applicable | | government agencies. The licensee may also issue a press release. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021