The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for February 8, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           02/07/2001 - 02/08/2001

                              ** EVENT NUMBERS **

37716  37723  37724  37725  37726  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37716       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 02/05/2001|
|    UNIT:  [1] [2] []                STATE:  TX |NOTIFICATION TIME: 05:02[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        02/05/2001|
+------------------------------------------------+EVENT TIME:        03:15[CST]|
| NRC NOTIFIED BY:  STEVEN KASPAR                |LAST UPDATE DATE:  02/07/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |BLAIR SPITZBERG      R4      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       9        Power Operation  |9        Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 10 CFR 73.71(b) SECURITY REPORT                                              |
|                                                                              |
| Safeguards system degradation related to detection/monitoring. Immediate     |
| compensatory measures taken upon discovery. Contact the NRC Operations       |
| Center for additional details.                                               |
|                                                                              |
| The NRC resident inspector will be informed of this event by the licensee.   |
|                                                                              |
| * * RETRACTION ON 02/07/01 AT 1132 ET BY GREG JANAK TAKEN BY MACKINNON* * *  |
|                                                                              |
| This event is being retracted because the individuals who entered the        |
| Protected Area were fully authorized and had completed the search process.   |
| The procedure was, however, violated.  This event is being made a loggable   |
| event only, Not Reportable.  R4DO (Sanborn) notified.                        |
|                                                                              |
| The NRC Resident Inspector was notified of this retraction by the licensee.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37723       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  U.S.  ARMY                           |NOTIFICATION DATE: 02/07/2001|
|LICENSEE:  U.S.  ARMY                           |NOTIFICATION TIME: 10:47[EST]|
|    CITY:  ABERDEEN                 REGION:  1  |EVENT DATE:        02/03/2001|
|  COUNTY:                            STATE:  MD |EVENT TIME:        12:00[EST]|
|LICENSE#:  91-30563-01           AGREEMENT:  Y  |LAST UPDATE DATE:  02/07/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |RONALD BELLAMY       R1      |
|                                                |BRENT CLAYTON        R3      |
+------------------------------------------------+BRIAN SMITH          NMSS    |
| NRC NOTIFIED BY:  JOYCE KUYKENDALL             |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAB2 20.2201(a)(1)(ii)   LOST/STOLEN LNM>10X    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TWO CHEMICAL AGENT DETECTORS AND ONE CHEMICAL MONITOR STOLEN.                |
|                                                                              |
|                                                                              |
| Two M22GID3 Chemical Agent Detectors, and one Chemical Agent Monitor  where  |
| shipped in a connex container (closed secured container) by railway from Ft  |
| Campbell, KY to Ft Polk, LA. Upon arrival to Ft Polk it was discovered that  |
| the connex container had been broken into and the two M22GID3 Chemical Agent |
| Detectors and one Chemical Agent Monitor were missing.  Ft Polk military     |
| police are investigating this event.                                         |
| Each Chemical Agent  Detector contains 30mCi of Ni-63 and the Chemical Agent |
| Monitor contains 15mCi of Ni-63.                                             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37724       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  SC DIV OF HEALTH & ENV CONTROL       |NOTIFICATION DATE: 02/07/2001|
|LICENSEE:  B-D INCORPORATED                     |NOTIFICATION TIME: 11:14[EST]|
|    CITY:  SUMTER                   REGION:  2  |EVENT DATE:        02/07/2001|
|  COUNTY:                            STATE:  SC |EVENT TIME:        10:00[EST]|
|LICENSE#:  315                   AGREEMENT:  Y  |LAST UPDATE DATE:  02/07/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |KEN BARR             R2      |
|                                                |BRIAN SMITH          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DAVID KING                   |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAD1 20.2202(a)(1)       PERS OVEREXPOSURE      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| POSSIBLE OVEREXPOSURE                                                        |
|                                                                              |
| B-D, Incorporated located in Sumter, South Carolina reported the following   |
| event to the State of South Carolina.                                        |
| B-D, Incorporated has a 2.3 million curie irradiator onsite.                 |
|                                                                              |
| On 02/02/01, B-D, Incorporated received from Landauer the radiation exposure |
| data on their film badges for the months of November through December, 2000. |
| The Radiation Safety Officer for B-D Incorporated did not review the film    |
| badge results until 02/05/01.  Upon reviewing the data, the RSO discovered   |
| that one of the film badges had been exposed beyond its limit (> 1000 Rad).  |
| The person whom the film badge had belonged to was administered a blood test |
| today, 02/07/01.                                                             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   37725       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  COGEMA MINING, INC.                  |NOTIFICATION DATE: 02/07/2001|
|LICENSEE:  COGEMA MINING, INC.                  |NOTIFICATION TIME: 14:00[EST]|
|    CITY:  LINCH                    REGION:  4  |EVENT DATE:        02/05/2001|
|  COUNTY:                            STATE:  WY |EVENT TIME:             [MST]|
|LICENSE#:  SUA-1341              AGREEMENT:  N  |LAST UPDATE DATE:  02/07/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |GARY SANBORN         R4      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+DANIEL GILLEN        NMSS    |
| NRC NOTIFIED BY:  JOHN VASELIN                 |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NMIN                     MINING EVENT           |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CONDITION OF LICENSE REPORT INVOLVING MINE IN EXCURSION STATUS               |
|                                                                              |
| "Notification of a Reportable Event per License Section 11.2                 |
|                                                                              |
| "Reported Event:                                                             |
|                                                                              |
| A routine quarterly (every 3 months) water sample collected on February 5,   |
| 2001 from monitor well M2, exceeded 2 of its 3 upper control limits (UCLs).  |
| A confirmation sample was collected February 6, which also exceeded 2 UCLs.  |
| Monitor well M2 was then placed on excursion status as per license Section   |
| 11.2 and its sampling frequency increased to weekly. M2 is a perimeter ore   |
| zone monitor well located approximately 300 feet east of the restored        |
| Production Unit 2 boundary, at the Irigaray Mine, Johnson County Wyoming.    |
| The nearest community is Linch, Wyoming, approximately 23 miles to the       |
| southeast.                                                                   |
|                                                                              |
| Analysis Data:                                                               |
|                                                                              |
| Conductivity                                       Uranium                   |
| Date                                     Chloride mg/l     umhos/cm2         |
| Alkalinity mg/l       mg/I U3O8                                              |
| Sampled                            UCL 18.0               UCL 685            |
| UCL 131.1                no UCL                                              |
| 2-05-01                                19.5                         806      |
| 95.3                           <0.4                                          |
| 2-06-01                                20.5                         799      |
| 97.3                           <0.4                                          |
|                                                                              |
| Health and Environmental Hazards:                                            |
|                                                                              |
| None                                                                         |
|                                                                              |
| investigative Action:                                                        |
|                                                                              |
| Conduct further sampling to try to determine the extent and direction of the |
| excursion.                                                                   |
|                                                                              |
| Written Notification:                                                        |
|                                                                              |
| A written notification will be submitted to NRC Uranium Recovery Branch      |
| Chief within 7 days."                                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37726       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 02/07/2001|
|    UNIT:  [] [2] []                 STATE:  TX |NOTIFICATION TIME: 23:15[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        02/07/2001|
+------------------------------------------------+EVENT TIME:        18:29[CST]|
| NRC NOTIFIED BY:  RICK NANCE                   |LAST UPDATE DATE:  02/07/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GARY SANBORN         R4      |
|10 CFR SECTION:                                 |                             |
|*RPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|*ESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     M/R        Y       10       Power Operation  |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 2 MANUAL REACTOR TRIP FOLLOWING THE LOSS OF THE "A" REACTOR COOLANT     |
| PUMP DURING ELECTRICAL BUS REALIGNMENT                                       |
|                                                                              |
| "SOUTH TEXAS PROJECT ELECTRIC GENERATING STATION, UNIT 2, MAKES THE          |
| FOLLOWING REPORT PER 10 CFR 50.72(b)(2)(iv)(B).                              |
|                                                                              |
| "AT 1829 ON 2/7/01, OPERATORS MANUALLY TRIPPED THE REACTOR FOLLOWING LOSS OF |
| POWER TO A REACTOR COOLANT PUMP DURING ELECTRICAL BUS REALIGNMENT.  PLANT    |
| DESIGN REQUIRES FOUR REACTOR COOLANT PUMPS RUNNING WHEN THE REACTOR IS       |
| CRITICAL.  THERE IS NO AUTOMATIC REACTOR TRIP FOR A LOSS OF A SINGLE REACTOR |
| COOLANT PUMP BELOW 40% REACTOR POWER.                                        |
|                                                                              |
| "WE ALSO MAKE THE FOLLOWING REPORT PER 10 CFR 50.72(b)(3)(iv)(A).            |
|                                                                              |
| "DURING ELECTRICAL BUS REALIGNMENT, POWER WAS LOST TO TRAIN 'A' 4.16KV       |
| ENGINEERED SAFETY FEATURE BUS.  DIESEL GENERATOR 21 AUTOMATICALLY STARTED    |
| AND BEGAN SUPPLYING POWER TO THE BUS.  THE LOSS OF OFFSITE POWER SIGNAL      |
| RESULTED IN THE ACTUATION OF THE FOLLOWING TRAIN 'A' EQUIPMENT:  ESSENTIAL   |
| COOLING WATER, COMPONENT COOLING WATER, AUXILIARY FEEDWATER, ESSENTIAL       |
| CHILLED WATER, CONTROL ROOM HVAC AND FUEL HANDLING BUILDING HVAC.            |
|                                                                              |
| "ESSENTIAL CHILLER 22A STARTED ON THE LOSS OF POWER SIGNAL BUT WAS           |
| SUBSEQUENTLY DECLARED INOPERABLE DUE TO HIGH OIL TEMPERATURE."               |
|                                                                              |
| OPERATORS WERE ATTEMPTING TO TRANSFER POWER ON 13.8KV BUS "2F" WHEN THE      |
| SUPPLY BREAKER OPENED DUE TO OPERATOR ERROR.  ALL CONTROL RODS INSERTED      |
| FOLLOWING THE TRIP.  OFFSITE POWER HAS BEEN RESTORED TO THE "2F" BUS AND THE |
| DIESEL GENERATOR RETURNED TO STANDBY.  AN EVENT RESPONSE TEAM IS EVALUATING  |
| THE TRIP.  THE LICENSEE ANTICIPATES RESTORING THE "A" RCP IN APPROXIMATELY   |
| TWO HOURS.                                                                   |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021